• 제목/요약/키워드: Hydrogen liquefaction

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액화천연가스(LNG)를 사용한 수소 생산 및 액화 공정 개발 (Design and Analysis of Hydrogen Production and Liquefaction Process by Using Liquefied Natural Gas)

  • 노원준;박시환;이인규
    • Korean Chemical Engineering Research
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    • 제59권2호
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    • pp.200-208
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    • 2021
  • 액체 상태의 수소는 기체 상태의 수소에 비해 수송이 용이하고 에너지 밀도가 높으며 폭발 위험성이 낮다. 하지만 수소 액화 공정은 냉각 사이클에 많은 양의 에너지가 소모된다. 반면에 액화천연가스(LNG; Liquefied Natural Gas)는 재기화 과정에서 다량의 냉열이 버려진다. 따라서 LNG 냉열을 회수하여 수소 냉각에 활용한다면 공정 효율을 높일 수 있다. 또한, 천연가스 개질을 통한 수소 생산은 가장 경제성 있는 방법으로 평가받고 있으며, 이러한 측면에서 LNG를 수소 생산의 원료로 사용할 수 있다. 본 연구에서는 LNG를 원료 및 냉열원으로 사용하여 수소를 생산 및 액화시키는 공정을 개발하고 열역학적 관점에서 공정을 평가하였다. 공정 개발을 위해 기존의 탄화 수소 혼합 냉매와 헬륨-네온 냉매를 이용한 수소 액화 공정을 비교 공정으로 선정하였다. 이후 LNG를 원료 및 수소 예냉의 냉열원으로 사용하는 새로운 공정을 설계하여 에너지 소모량 및 엑서지 효율 측면에서 기존 공정과 비교, 분석하였다. 제안된 공정은 기존 공정 대비 약 17.9%의 에너지 절감 및 11.2%의 엑서지 효율이 향상된 결과를 나타내었다.

대형 수소 액화 플랜트의 정량적 위험도 평가에 관한 연구 (Study on a Quantitative Risk Assessment of a Large-scale Hydrogen Liquefaction Plant)

  • 도규형;한용식;김명배;김태훈;최병일
    • 한국수소및신에너지학회논문집
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    • 제25권6호
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    • pp.609-619
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    • 2014
  • In the present study, the frequency of the undesired accident was estimated for a quantitative risk assessment of a large-scale hydrogen liquefaction plant. As a representative example, the hydrogen liquefaction plant located in Ingolstadt, Germany was chosen. From the analysis of the liquefaction process and operating conditions, it was found that a $LH_2$ storage tank was one of the most dangerous facilities. Based on the accident scenarios, frequencies of possible accidents were quantitatively evaluated by using both fault tree analysis and event tree analysis. The overall expected frequency of the loss containment of hydrogen from the $LH_2$ storage tank was $6.83{\times}10^{-1}$times/yr (once per 1.5 years). It showed that only 0.1% of the hydrogen release from the $LH_2$ storage tank occurred instantaneously. Also, the incident outcome frequencies were calculated by multiplying the expected frequencies with the conditional probabilities resulting from the event tree diagram for hydrogen release. The results showed that most of the incident outcomes were dominated by fire, which was 71.8% of the entire accident outcome. The rest of the accident (about 27.7%) might have no effect to the population.

Linde, Claude 및 Advanced 사이클을 이용한 질소액화공정 연구 (A Study on the Nitrogen Liquefaction Using Linde, Claude and Advanced Cycle)

  • 노상균
    • 한국수소및신에너지학회논문집
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    • 제33권3호
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    • pp.261-265
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    • 2022
  • In this paper, comparative studies between Linde, Claude and advanced cycle for the liquefaction of nitrogen have been completed. PRO/II with PROVISION release 2021. 1 from AVEVA company (Cambridge, UK) was used, and Peng-Robinson equation of the state model with Twu's alpha function was selected for the modeling of the condensation of nitrogen. When using Claude liquefaction, we can reduce the total compression power by 49.25% for the comparison of Linde cycle. And finally, we could conclude that 90.41% of total compression power was saved when using an advanced cycle being compared to Linde liquefaction cycle.

소형 수소액화기 설계 및 운전에 관한 연구 (Design and Operation of a Small-Scale Hydrogen Liquefier)

  • 백종훈;강상우;강형묵;나다니엘 갈소;김서영;오인환
    • 한국수소및신에너지학회논문집
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    • 제26권2호
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    • pp.105-113
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    • 2015
  • In order to accelerate hydrogen society in current big renewable energy trend, it is very important that hydrogen can be transported and stored as a fuel in efficient and economical fashion. In this perspective, liquid hydrogen can be considered as one of the most prospective storage methods that can bring early arrival of the hydrogen society by its high gravimetric energy density. In this study, a small-scale hydrogen liquefier has been designed and developed to demonstrate direct hydrogen liquefaction technology. Gifford-McMahon (GM) cryocooler was employed to cool warm hydrogen gas to normal boiling point of hydrogen at 20K. Various cryogenic insulation technologies such as double walled vacuum vessels and multi-layer insulation were used to minimize heat leak from ambient. A liquid nitrogen assisted precooler, two ortho-para hydrogen catalytic converters, and highly efficient heat pipe were adapted to achieve the target liquefaction rate of 1L/hr. The liquefier has successfully demonstrated more than 1L/hr of hydrogen liquefaction. The system also has demonstrated its versatile usage as a very efficient 150L liquid hydrogen storage tank.

응축형 수소 액화 시스템에 대한 LabVIEW 기반 데이터 저장 및 모니터링 프로그램 개발 (Development of LabVIEW-based Data Storage and Monitoring Program for a Condensed Hydrogen Liquefaction System)

  • 하동우;노현우;서영민;구태형;고락길
    • 한국수소및신에너지학회논문집
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    • 제34권5호
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    • pp.456-464
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    • 2023
  • In this study, a compact hydrogen liquefaction system was constructed with the aim of creating a data storage and monitoring program for liquid hydrogen production. This program was designed to receive and record signals from diverse control equipment through the LabVIEW software. A range of measurement instruments were devised to collect data, encompassing variables such as flow rate, pressure, temperature, and liquid level. As a result, it was possible to directly check the production of liquid hydrogen by obtaining various data of condensed liquid hydrogen. In addition, it was confirmed that long-term storage of liquid hydrogen is possible by developing automatic ON/OFF through the LabVIEW program.

장주기/대용량 수소저장을 위한 액체/고체기반 Slush 수소의 저장 비용 분석 (An Economic Analysis on Slush Hydrogen Containing Liquid and Solid Phase for Long-Term and Large-Scale Storage)

  • 박성호;이창형;류주열;황성현
    • 한국수소및신에너지학회논문집
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    • 제33권3호
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    • pp.247-254
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    • 2022
  • Slush hydrogen containing liquid and solid hydrogen is expected to achieve zero boil-off by suppressing boil-off gas because heat of fusion for solid absorbe the heat ingress from atmosphere. In this paper, quantitative analysis on storage cost considering specific energy consumption between 1,000 m3 class liquid hydrogen storage system with re-liquefaction and slush hydrogen storage system during equivalent zero boil off period. Even though approximately 50% of total storage capacity should be converted into solid phase during the initial cargo bunkering, total energy consumption to convert into slush hydrogen is relatively 25% less than re-liquefaction energy for boil off hydrogen during zero boil off period. That's because energy consumption of slush phase change take up only 1.8% of liquefaction energy. moreover, annual revenue requirement including CAPEX, OPEX and electric cost for slush hydrogen storage could be more reduced approximately 32.5% than those of liquid hydrogen storage and specific energy storage cost ($/kg-H2) could also be lowered by about 41.7% compared with liquid hydrogen storage.

Linde-Hampson 및 Claude 사이클을 이용한 산소액화공정 연구 (Study on the Oxygen Liquefaction Using Linde-Hampson and Claude Cycle)

  • 노상균
    • 한국수소및신에너지학회논문집
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    • 제33권4호
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    • pp.446-450
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    • 2022
  • In this paper, comparative studies between Linde-Hampson and Claude cycle for the liquefaction of oxygen have been completed. PRO/II with PROVISION release 2021. 1 from AVEVA company (Cambridge, UK) was used, and Peng-Robinson equation of the state model with Twu's alpha function was selected for the modeling of the condensation of oxygen. When using Claude liquefaction cycle, we could reduce the total compression power by 59.51% for the comparison of Linde-Hampson cycle.

페로브스카이트 촉매에 의한 액화수소의 올소-파라 수소변환특성에 관한 연구 (A Study on the Ortho-para Hydrogen Conversion Characteristics of Liquefied Hydrogen by Perovskite Catalysts)

  • 나인욱;김정현;;권순철;오인환
    • 한국수소및신에너지학회논문집
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    • 제26권1호
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    • pp.15-20
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    • 2015
  • During the liquefaction of hydrogen, the ortho hydrogen is converted into the para form with heat release that evaporates the liquefied hydrogen into the gaseous one backwards. The ortho-para conversion catalysts are usually used during liquefaction to avoid such boil-off. In order to compare and analyze the performance of the ortho-para hydrogen conversion catalysts, in-situ FT-IR device was designed and manufactured to measure the para hydrogen conversion rate in real-time. $LaFeO_3$ and $La_{0.7}Sr_{0.3}Cu_{0.3}Fe_{0.7}O_3$ perovskite catalysts were prepared by the citrate sol-gel method and their spin conversion characteristics from ortho to para hydrogen were investigated by in-situ FTIR spectroscopy at 17K. It was found that the spin conversion was affected by surface area, particle size, and crystallite size of the catalysts. Thus, the $La_{0.7}Sr_{0.3}Cu_{0.3}Fe_{0.7}O_3$ perovskite catalyst that had higher surface area, higher crystallite size, and smaller particle size than $LaFeO_3$ showed the better spin conversion property of 32.3% at 17K in 120min interaction with the perovskite catalysts.

셀룰로오스의 분해특성 및 연료물질 생성 (I) -열분해·액화반응- (Degradation Properties and Production of Fuels of Cellulose - Pyrolysis-Liquefaction -)

  • 이종집;이병학
    • 한국수소및신에너지학회논문집
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    • 제15권4호
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    • pp.333-340
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    • 2004
  • In this study, thermochemical degradation by pyrolysis-liquefaction of cellulose, the effects of reaction time, reaction temperature, conversion yield, degradation properties and degradation products were investigated . Experiments were performed in a tube reactor by varying reaction time from 20 to 80 min at $200{\sim}500^\circ{C}$. Combustion heating value of liquid products from thermochemical conversion processes of cellulose was in the range of 6,920~6,960cal/g. After 40min of reaction at $400^\circ{C}$ in pyrolysis-liquefaction of cellulose, the energy yield and mass yield was as high as 54.3% and 34.0g oil/100g raw material, respectively. The liquid products from pyrolysis-liquefaction of cellulose contained various kinds of ketones, phenols and furans. ketones and furans could be used as high-octane-value fuels and fuel additives. However, phenols are not valuable as fuels.

LNG 냉열을 이용한 공기액화분리시스템의 시뮬레이션 및 공정 해석 (Process Analysis and Simulation for System of Air Liquefaction Separation Using LNG Cold Energy)

  • 한단비;백영순
    • 한국수소및신에너지학회논문집
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    • 제30권3호
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    • pp.276-281
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    • 2019
  • The process of separating oxygen and nitrogen from the air is mainly performed by electric liquefaction, which consumes a lot of electricity, resulting in higher operating costs. On the other hand, when used for cold energy of LNG, electric power can be reduced compared to the electric Linde cycle. Currently, LNG cold energy is used in the cold refrigeration warehouse, separation of air-liquefaction, and LNG cold energy generation in Japan. In this study, the system using LNG cold energy and the Linde cycle process system were simulated by PRO/II simulators, respectively, to cool the elevated air temperature from the compressor to about $-183^{\circ}C$ in the air liquefaction separation process. The required amount of electricity was compared with the latent heat utilization fraction of LNG, the LNG supply pressure, and the LNG cold energy usage. At the air flow rate of $17,600m^3/h$, the power source unit of the Linde cycle system was $0.77kWh/m^3$, compared with $0.3kWh/m^3$.