• 제목/요약/키워드: CLEANING

검색결과 3,875건 처리시간 0.031초

블라스트 표면처리가 하중비전달형 십자필렛 용접이음의 피로거동에 미치는 영향 (Effect of Blast Cleaning on Fatigue Behavior of Non-load-carrying Fillet Welded Cruciform Joints)

  • 김인태;정영수;김광진;이동욱
    • 한국강구조학회 논문집
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    • 제21권1호
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    • pp.55-62
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    • 2009
  • 강교 제작에는 강재 표면의 이물질 제거와 피복방식재료의 부착성 증대를 위하여 블라스트 표면처리가 실시되고 있다. 블라스트 표면처리는 쇼트나 그릿 등의 연마재를 압축공기로 분사하여 강재 표면에 충격을 가하는 표면처리법으로, 블라스트 처리에 의해 표면형상이 개선되고 압축잔류응력이 도입되어 용접이음의 피로수명이 향상될 것으로 예상된다. 본 연구에서는 하중비전달형 십자필렛 용접이음의 피로실험을 실시하여, 블라스트 표면처리가 용접이음의 피로거동에 미치는 영향을 실험적으로 검토하였다. 피로실험에는 용접 후 무처리 시험편(용접 그대로), 용접 후 블라스트 표면처리 한 시험편과 블라스트 처리 후 열처리에 의해 잔류응력을 제거한 시험편의 합계 3종류의 용접시험편을 대상으로 하였다. 그 결과 블라스트 표면처리에 의해 용접지단부의 곡률반경은 약 29% 증가하였으며, 용접지단부의 인장잔류응력이 제거되고 압축잔류응력이 도입되었다. 그리고 블라스트 처리에 의해 피로수명과 피로한계가 증가하였다. 피로수명은 응력범위가 낮을수록 더 크게 증가하였고, 피로한계는 약 1.5배 증가하였다.

고온화학세정환경에서 20 % EDTA 용액이 결함 전열관 (Alloy600)에 미치는 영향 (Effect of 20 % EDTA Aqueous Solution on Defective Tubes (Alloy600) in High Temperature Chemical Cleaning Environments)

  • 권혁철
    • Corrosion Science and Technology
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    • 제15권2호
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    • pp.84-91
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    • 2016
  • The transport and deposition of corrosion products in pressurized water nuclear reactor (PWR) steam generators have led to corrosion (SCC, denting etc.) problems. Lancing, mechanical cleaning and chemical cleaning have been used to reduce these problems. The methods of lancing and mechanical cleaning have limitations in removing corrosion products due to the structure of steam generator tubes. But high temperature chemical cleaning (HTCC) with EDTA is the most effective method to remove corrosion products regardless of the structure. However, EDTA in chemical cleaning aqueous solution and chemical cleaning environments affects the integrity of materials used in steam generators. The nuclear power plants have to perform the pre-test (also called as qualification test (QT)) that confirms the effect on the integrity of materials after HTCC. This is one of the series studies that assess the effect, and this study determines the effects of 20 % EDTA aqueous solution on defective tubes in high temperature chemical cleaning environments. The depth and magnitude of defects in steam generator (SG) tubes were measured by eddy current test (ECT) signals. Surface analysis and magnitude of defects were performed by using SEM/EDS. Corrosion rate was assessed by weight loss of specimens. The ECT signals (potential and depth %) of defective tubes increased marginally. But the lengths of defects, oxides on the surface and weights of specimens did not change. The average corrosion rate of standard corrosion specimens was negligible. But the surfaces on specimens showed traces of etching. The depth of etching showed a range on the nanometer. After comprehensive evaluation of all the results, it is concluded that 20 % EDTA aqueous solution in high temperature chemical cleaning environments does not have a negative effect on defective tubes.

이류체 노즐을 이용한 FPD 세정시스템 및 공정 개발 (Optimization of FPD Cleaning System and Processing by Using a Two-Phase Flow Nozzle)

  • 김민수;김향란;김현태;박진구
    • 한국재료학회지
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    • 제24권8호
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    • pp.429-433
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    • 2014
  • As the fabrication technology used in FPDs(flat-panel displays) advances, the size of these panels is increasing and the pattern size is decreasing to the um range. Accordingly, a cleaning process during the FPD fabrication process is becoming more important to prevent yield reductions. The purpose of this study is to develop a FPD cleaning system and a cleaning process using a two-phase flow. The FPD cleaning system consists of two parts, one being a cleaning part which includes a two-phase flow nozzle, and the other being a drying part which includes an air-knife and a halogen lamp. To evaluate the particle removal efficiency by means of two-phase flow cleaning, silica particles $1.5{\mu}m$ in size were contaminated onto a six-inch silicon wafer and a four-inch glass wafer. We conducted cleaning processes under various conditions, i.e., DI water and nitrogen gas at different pressures, using a two-phase-flow nozzle with a gap distance between the nozzle and the substrate. The drying efficiency was also tested using the air-knife with a change in the gap distance between the air-knife and the substrate to remove the DI water which remained on the substrate after the two-phase-flow cleaning process. We obtained high efficiency in terms of particle removal as well as good drying efficiency through the optimized conditions of the two-phase-flow cleaning and air-knife processes.

세정공정에 따른 Y2O3 코팅부품의 내플라즈마성 영향 (Influence of Plasma Corrosion Resistance of Y2O3 Coated Parts by Cleaning Process)

  • 김민중;신재수;윤주영
    • 한국표면공학회지
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    • 제54권6호
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    • pp.365-370
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    • 2021
  • In this research, we proceeded with research on plasma resistance of the cleaning process of APS(Atmospheric Plasma Spray)-Y2O3 coated parts used for semiconductor and display plasma process equipment. CF4, O2, and Ar mixed gas were used for the plasma environment, and respective alconox, surfactant, and piranha solution was used for the cleaning process. After APS-Y2O3 was exposed to CF4 plasma, the surface changed from Y2O3 to YF3 and a large amount of carbon was deposited. For this reason, the plasma corrosion resistance was lowered and contamination particles were generated. We performed a cleaning process to remove the defect-inducing surface YF3 layer and carbon layer. Among three cleaning solutions, the piranha cleaning process had the highest detergency and the alconox cleaning process had the lowest detergency. Such results could be confirmed through the etching amount, morphology, composition, and accumulated contamination particle analysis results. Piranha cleaning process showed the highest detergency, but due to the very large thickness reduction, the base metal was exposed and a large number of contaminated particles were generated. In contrast, the surfactant cleaning process exhibit excellent properties in terms of surface detergency, etching amount, and accumulated contamination particle analysis.

대전 목달동 출토 여산송씨 출토복식의 세척 (The Cleaning of Costumes of Yeosan Song's Family Excavated at Mokdal-dong in Daejeon)

  • 백영미;권영숙
    • 보존과학회지
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    • 제25권2호
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    • pp.219-231
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    • 2009
  • 본 연구는 대전에서 출토된 조선시대 초중기의 여산송씨가 출토복식을 보존처리함에 있어 출토복식의 세척처리 현황을 조사하고 본 출토복식의 세척과정을 보고하여 앞으로 출토복식의 세척방안에 대한 자료로 제공하고자 하는데 그 목적이 있다. 여산송씨 출토복식은 15세기의 남자복식과 16세기중후반의 남녀복식을 비교할 수 있는 좋은 자료가 되고 있다. 출토유물은 모두 184점이 출토되었으며 면, 견, 마, 교직물 등 다양한 직물이 있었다. 여산송씨 출토복식의 세척은 직물의 상태와 오염을 분석한 후 진공흡입에 의한 고형오염을 충분히 제거하고 습식세척과 건식세척방법을 시행하였으며 1, 2차로 진행되었다. 습식세척의 경우 음이온계 계면활성제(LAS)와 비이온계 계면활성제(Triton X-100)를 사용하였고 건식세척의 경우 n-hexane과 n-decane(4:6) 혼합용제 및 석유계 드라이클리닝용제를 사용하였다. 1차 세척 후 빠지지 않은 얼룩이 있는 면직물이나 마직물의 경우 표백처리를 실시하였으며 견직물 중 상태가 좋은 것은 유기용제에 의한 건식세척을 재실시하였다.

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세척제 용매 중독 사례와 국내·외 규제 검토를 통한 할로겐화 용매 세척제 사용의 문제점 고찰 (Review of Problems with Use of Halogenated Cleaning Solvents Revealed through Case Studies of Cleaning Solvent Poisoning and Analysis of Domestic and Overseas Regulations)

  • 이나루;이혜진;정수진;이도희;신아롬
    • 한국산업보건학회지
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    • 제33권4호
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    • pp.517-527
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    • 2023
  • Objectives: We examine cases of chemical poisoning that occurred in the cleaning of metal parts and the regulations on halogenated solvents in other countries and propose regulations necessary to prevent chemical poisoning from halogenated solvents. Methods: We collected cases of chemical poisoning through the website of the Korea Occupational Safety and Health Agency. A review of the literature was conducted focusing on regulations related to halogenated solvents in the United States and the European Union, particularly for cleaning metal parts. Among the Material Safety Data Sheets submitted to the government, MSDS containing eleven substances were extracted to confirm the composition and product use. We investigated cleaning methods for metal parts used in South Korea. For the hazard classification, the European Chemicals Agency or Japan's NITE's website was used. Results: In the case of poisoning, the cleaning methods involving trichloromethane were dipping and dry, which was not found in the literature. It was confirmed that many halogenated solvents and dimethyl carbonate were used for metal cleaning in South Korea. In vapor degreasing using TCE in the USA, even if the facility is strictly managed, such as by installing cooling coils in open cleaning facilities, the risk of exposure to TCE is considered to be not only carcinogenic but also a concern for acute and chronic effects. In comparison, exposure through Korean work methods such as dipping and drying operations is inevitably much higher. Conclusions: The transition to water-based cleaning with low-hazard chemicals should be a priority in the cleaning process. In the case of metal parts that require precise cleaning, if the use of a halogenated solvent is inevitable, a closed degreasing facility should be used to minimize exposure. The current regulations in the Occupational Safety and Health Act, the Chemical Substances Control Act, and the Air Environment Conservation Act do not require cleaning facilities to minimize emissions. To protect the health of workers using halogenated solvents to clean metal parts, regulations that require a fundamental reduction in exposure will be necessary.

지하역사 덕트 청소로봇 기술동향 및 개발 (Development of a Duct Cleaning Robot and Technology Trends for Subway Stations)

  • 정우태;박덕신
    • 한국철도학회:학술대회논문집
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    • 한국철도학회 2011년도 정기총회 및 추계학술대회 논문집
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    • pp.1335-1341
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    • 2011
  • Conserving clean air and removing contaminants and particular matters accumulated in the ventilation system of the subway stations are key issue for green railway environment. There is no national guideline or industrial regulations to sustain clean duct and ventilation system, which requires rapid reformation of cleaning procedure and system. In fact, accumulated various particular matters and dusts can occur secondary air contamination and become a primary health harm factor for subway passengers. This study investigates various duct cleaning technologies and trends. In additon, effective cleaning method with an automated robot device is proposed. In particular, current dust cleaning technologies and duct cleaning robots are analyzed based on their functions and feasibilities. The proposed design of automated device is expected to save the operating cost of subway HVAC system and sustain clean air environment.

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Leakage Current Reduction of Ni-MILC Poly-Si TFT Using Chemical Cleaning Method

  • Lee, Kwang-Jin;Kim, Doyeon;Choi, Duck-Kyun;Kim, Woo-Byoung
    • 한국재료학회지
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    • 제28권8호
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    • pp.440-444
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    • 2018
  • An effective cleaning method for Ni removal in Ni-induced lateral crystallization(Ni-MILC) poly-Si TFTs and their electrical properties are investigated. The HCN cleaning method is effective for removal of Ni on the crystallized Si surface, while the nitric acid treatment results decrease by almost two orders of magnitude in the Ni concentration due to effective removal of diffused Ni mainly in the poly-Si grain boundary regions. Using the HCN cleaning method after the nitric acid treatment, re-adsorbed Ni on the Si surfaces is effectively removed by the formation of Ni-cyanide complexions. After the cleaning process, important electrical properties are improved, e.g., the leakage current density from $9.43{\times}10^{-12}$ to $3.43{\times}10^{-12}$ A and the subthreshold swing values from 1.37 to 0.67 mV/dec.

마이크로 드릴비트 세척시스템의 유체-구조 연성해석 (Analysis of Fluid-Structure Interaction of Cleaning System of Micro Drill Bits)

  • 국연호;최현진
    • 한국기계가공학회지
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    • 제15권1호
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    • pp.8-13
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    • 2016
  • The micro drill bit automatic regrinding in-line system is a system that refurbishes drill bits used in a PCB manufacturing process. This system is able to refurbish drill bits with a minimum size of ø0.15-0.075mm that have previously been discarded. Beyond the conventional manual cleaning process using ultrasound, this system adopts a water jet cleaning system, making it capable of cleaning drill bits with a minimum size of ø0.15-0.075mm. This paper analyses various contact pressures applied to the surface of drill bits depending on the shooting pressure of the cleaning device and fluid velocity in order to optimize the nozzle location and to detect structural instability caused by the contact pressures.

TFT LCD 세정 방법에 대한 프로세스 개선에 관한 연구 (A Study on the Process Improvement in TFT LCD Cleaning)

  • 홍민성;김종민;강신재
    • 한국공작기계학회:학술대회논문집
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    • 한국공작기계학회 2004년도 춘계학술대회 논문집
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    • pp.269-274
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    • 2004
  • As next generation display, TFT LCD gets into the spotlight, and the bigger glass size is required. Currently, its display size is 1500 mm by 1870 mm at the six generation comparing with 300mm by 400 mm at the first one and the size is increasing continuously, which cause the difficulties to apply the cleaning operation including the general brush cleaning. In this study, water-jet cleaning operation has been introduced, which spent the less water them other cleaning methods. Throughout the experiment, is has been found the possible damage of the declined cell and the variation of the tilt bias angle depending upon the increasing time. In addition, the simulation predicts the glass bending of the display.

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