The purpose of this paper is to analyze the causes of accidents related to the 3 phase 170 kV gas insulated switchgear of a power system collected from accident sites to secure data for the prevention of similar accidents and provide important points of view regarding diagnosis for the prevention of accidents involving gas insulated switchgears. The analysis results of the causes of accidents involving gas insulated switchgears showed deformation of the manipulation lever installed at the S-phase, disconnection of the insulation rod connection, melting of the upper conductor, a damaged tulip, damage to the lower spacer and the spacer at the breaker, etc. It is believed from this result that the potential for accidents has expanded due to accumulated energy as a result of repeated deterioration. The carbonization depth of a GIS was formed near the screw (T2, T3) used to secure the lower pole of the S-phase tulip. It is not known what has caused the screws to be extruded and melted. However, it is thought that an unbalanced electromagnetic force, micro-discharge, surface discharge, etc., have occurred at that point. In addition, even though 16 years have passed since its installation, there was no installation defect, act of arson, accidental fire, etc. General periodical inspection and diagnosis failed to find the factors causing the accidents. As a system contained in a closed metal container, it has a high risk factor. Therefore, it is necessary to design, install and operate a GIS in accordance with the standard operational procedure (SOP). In addition, it is necessary to apply conversion technology for periodical SF6 gas analysis and precision safety diagnosis. It is expected that tracking and managing these changes in characteristics by recording the results on the history card will provide a significant accident prevention effect.