• Title/Summary/Keyword: helium leak

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Introduction to Helium Leak Detection Techniques for Cryogenic Systems

  • Kim, Heetae;Chang, Yong Sik;Kim, Wookang;Jo, Yong Woo;Kim, Hyung Jin
    • Applied Science and Convergence Technology
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    • v.24 no.4
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    • pp.77-83
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    • 2015
  • Many welding processes are performed to construct cryogenic system. Leak-tight for the cryogenic system is required at low temperature environment. Helium leak detection techniques are commonly used to find leak for the cryogenic system. The helium leak detection techniques for spraying, sniffing and pressurizing techniques are introduced. High vacuum is also necessary to use helium leak detector. So, types of fluid flow, effective temperature, conductance and pumping speed are introduced for vacuum pumping. Leak test procedure is shown for pipe welding, cryomodule and low temperature test. Cryogenic seals which include copper gasket, helicoflex gasket and indium are investigated.

Helium Leak Test for the PLS Storage Ring Chamber (포항가속기 저장링챔버의 헬륨누설검사)

  • Choi, M.H.;Kim, H.J.;Choi, W.C.
    • Journal of the Korean Society for Nondestructive Testing
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    • v.13 no.3
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    • pp.31-38
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    • 1993
  • The storage ring vacuum system for the Pohang Light Source (PLS) has been designed to maintain the vacuum pressure of $10^{-10}Torr$ which requires UHV welding to have helium leak rate less than $1{\times}10^{-10}Torr{\cdot}{\ell}/sec$. In order to develop new technique (PLS) welding technique), a prototype vacuum chamber has been welded by using Tungsten Inert Gas welding method and all the welded joints have been tested with a non-destructive method, so called helium leak detection, to investigate the vacuum tightness of the weld joints. The test was performed with a detection limit of $1{\times}10^{-10}Torr{\cdot}{\ell}/sec$ for helium and no detectable leaks were found for all the welded joints. Thus the performance of welding technique is proven to meet the criteria of helium leak rate required in the PLS Storage Ring. Both the principle and the procedure for the helium leak detection are also discussed.

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Consideration on the helium leak detection in a large vacuum chamber (대형 진공용기의 헬륨 누설검사 방법에 대한 고찰)

  • In, S.R.
    • Journal of the Korean Vacuum Society
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    • v.16 no.4
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    • pp.235-243
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    • 2007
  • Nowadays, in our country, large vacuum chambers for huge experimental facilities such as the tokamak fusion device, high power neural beam test stand, and space simulator have been constructed. In such a vacuum chamber of very large size, it is quite complicate to check on leakage quantitatively, while the probability of a leak is relatively high. To investigate the feasibility of applying reliably a helium leak detection to the huge vacuum chambers, and to find a reasonable methodology of choosing an optimum set-up for leak detection, several virtual constructions of the leak detection system have been analyzed by calculating the pressure distribution in the system and the helium level in the sensor part.

Effect of a Series Connection of a Bi-Electrolyte Hydrogen Sensor in a Leak Detector

  • Han, Hyeuk Jin;Park, Chong Ook;Hong, Youngkyu;Kim, Jong Suk;Yang, Jeong Woo;Kim, Yoon Seo
    • Journal of Sensor Science and Technology
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    • v.24 no.1
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    • pp.6-9
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    • 2015
  • Conventional leak detectors are widely based on helium gas sensors. However, the usage of hydrogen sensors in leak detectors has increased because of the high prices of helium leak detectors and the dearth in the supply of helium gas. In this study, a hydrogen leak detector was developed using solid-state hydrogen sensors. The hydrogen sensors are based on Park-Rapp probes with heterojunctions made by oxygen-ion conducting Yttria-stabilized zirconia and proton-conducting In-doped $CaZrO_3$. The hydrogen sensors were used for determining the potential difference between air and air balanced 5 ppm of $H_2$. Even though the Park-Rapp probe shows an excellent selectivity for hydrogen, the sensitivity of the sensor was low because of the low concentration of hydrogen, and the oxygen on the surface of the sensor. In order to increase the sensitivity of the sensor, the sensors were connected in series by Pt wires to increase the potential difference. The sensors were tested at temperatures ranging from $500-600^{\circ}C$.

Study on the Fugitive Emissions of a PFA Lined Ball Valve through Helium Leak Detection (PFA 라이닝 볼밸브의 헬륨누설 검출 및 비산배출에 관한 연구)

  • Lee, Won-Ho;Kim, Dong-Yeol;Lee, Jong-Chul
    • The KSFM Journal of Fluid Machinery
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    • v.19 no.4
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    • pp.39-42
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    • 2016
  • A PFA lined ball valve, which is machined with fluorinated resin PFA to its inner part for improving corrosion resistance, non-stickness, heat-resistance, has been widely used to the chemical/pharmaceutical industries, the semiconductor/LCD manufacturing processes, etc. with the high purity chemicals as working fluid. EPA stated that 60% of all fugitive emissions come from the valve stem packing in a typical petroleum or chemical processing plant. They monitor regulated components for leaks and maintain seal performance at acceptable levels. Korean industrial standards only deals with the bubble test for in-line leakage of valves, which has the detectable leak rate of $10^{-4}$ [$mbar{\cdot}L{\cdot}s^{-1}$], therefore, it is not sufficient to check fugitive emissions. In this study, we conducted Helium leak detection from a PFA lined ball valve and evaluated fugitive emissions according to ISO 15848-1, which has the detectable leak rate of $10^{-9}$ [$mbar{\cdot}L{\cdot}s^{-1}$], for manufacturing the high-reliable PFA lined ball valves against fugitive emissions.

Low Temperature Test of HWR Cryomodule

  • Kim, Heetae;Kim, Youngkwon;Lee, Min Ki;Park, Gunn-Tae;Kim, Wookang
    • Applied Science and Convergence Technology
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    • v.25 no.3
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    • pp.47-50
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    • 2016
  • Low temperature test for half-wave resonator (HWR) cryomodule is performed at the superfluid helium temperature of 2 K. The effective temperature is defined for non-uniform temperature distribution. Helium leak detection techniques are introduced for cryogenic system. Experimental set up is shown to make the low temperature test for the HWR cryomodule. The cooldown procedure of the HWR cryomodule is shown from room temperature to 2 K. The cryomodules is precooled with liquid nitrogen and then liquid helium is supplied to the helium reservoirs and cavities. The pressure of cavity and chamber are monitored as a function of time. The vacuum pressure of the cryomodule is not increased at 2 K, which shows leak-tight in the superfluid helium environment. Static heat load is also measured for the cryomodule at 2.5 K.

Development of Calibration System of Helium Permeation Type Standard Leaks (헬륨 투과형 표준리크 교정장치 개발)

  • Hong S.S.;Lim I.T.;Shin Y.H.
    • Journal of the Korean Vacuum Society
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    • v.15 no.4
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    • pp.347-353
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    • 2006
  • A helium permeation type standard leak calibration system has newly developed by using dynamic gas expansion method. The measurement range was extended lower to $10^{-6}$ Pa L/s for participating CCM (Consultative Committee for Mass and Related Quantities) standard leak key comparison. For the system, pressure ratios of high and ultra-high vacuum chamber and porous plug conductance for helium gas were determined. By using the system, a permeation type standard leak of $5.6{\times}10^{-4}$ Pa L/s range was calibrated. The calibration result showed that the difference between standard commercial leak was 11.1 %.

Prediction model of 4.5 K sorption cooler for integrating with adiabatic demagnetization refrigerator (ADR)

  • Kwon, Dohoon;Kim, Jinwook;Jeong, Sangkwon
    • Progress in Superconductivity and Cryogenics
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    • v.24 no.1
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    • pp.23-28
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    • 2022
  • A sorption cooler, which utilizes helium-4 as a working fluid, was previously developed and tested in KAIST. The cooler consists of a sorption pump and a thermosyphon. The developed sorption cooler aims to pre-cool a certain amount of the magnetic refrigerant of an adiabatic demagnetization refrigerator (ADR) from 4.5 K to 2.5 K. To simulate the high heat capacitance of the magnetic refrigerant, liquid helium was utilized not only as a refrigerant for the sorption cooling but also as a thermal capacitor. The previous experiment, however, showed that the lowest temperature of 2.7 K which was slightly higher than the target temperature (2.5 K) was achieved due to the radiation heat leak. This excessive heat leak would not occur when the sorption cooler is completely integrated with the ADR. Thus, based on the experimentally obtained pumping speed, the prediction model for the sorption cooler is developed in this study. The presented model in this paper assumes the sorption cooler is integrated with the ADR and the heat leak is negligible. The model predicts the amount of the liquid helium and the required time for the sorption cooling process. Furthermore, it is confirmed that the performance of the sorption cooler is enhanced by reducing the volume of the thermosiphon. The detailed results and discussions are summarized.

Assembly and Test of the In-cryostat Helium Line for KSTAR (KSTAR 저온용기 내부의 헬륨라인 설치 및 검사)

  • Bang, E.N.;Park, H.T.;Lee, Y.J.;Park, Y.M.;Choi, C.H.;Bak, J.S.
    • Journal of the Korean Vacuum Society
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    • v.16 no.2
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    • pp.153-159
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    • 2007
  • In-cryostat helium lines are under installation to transfer a cryogenic helium into cold components in KSTAR device. In KSTAR, three kinds of helium should be supplied into the cold components, which are supercritical helium Into superconduction(SC) magnet system, liquid helium into current lead system, and gas helium into thermal shields. Cryogenic helium lines consist of transfer lines outside the cryostat, in-cryostat helium lines, and electrical breaks. In-cryostat helium lines should be guaranteed of leak tightness for tong time operation at high internal helium pressure of 20 bar. We wrapped the helium line with multi-layer insulator(MLI) to reduce radiation heat and insulated the surface of the high potential part with prepreg tape. The electrical break was fabricated by brazing ceramic tube with stainless steel tube. To ensure the operation reliability at operation temperature, all the electrical break have been examined by the thermal cycle test at liquid nitrogen and by the hydraulic test at 30 bar. And additional surface insulation was prepared with prepreg tape to give structural safety. At present most of the in-cryostat helium lines have been installed and the final inspection test is progressing.