• Title/Summary/Keyword: Turbo engine

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A Study on Windmilling Start Performance of Micro Turbo-jet Engine (초소형 엔진의 윈드밀링 시동 성능 해석)

  • Kim, Wan-Jo;Park, Hwi-Seob;Roh, Tae-Seong;Choi, Dong-Whan
    • Journal of the Korean Society of Propulsion Engineers
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    • v.12 no.2
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    • pp.15-23
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    • 2008
  • A numerical method based on the prediction of total pressure loss of major components of the engine has been developed for prediction of the windmilling start performance of micro-turbojet engine. The start performance in on/off design region has been analysed by applying this method to predict windmilling start-able regions of the centrifugal-type engine. The results of this analysis have been validated by comparing with the test data. The effect of each design parameters on windmilling start performance has been analysed for the enlargement of start-able regions.

Experimental Study of a Micro Turbo Jet Engine Performance and IR Signal with Nozzle Configuration (배기노즐 형상변화에 따른 마이크로 터보제트 엔진의 성능 및 적외선신호 실험연구)

  • Park, Gyusang;Kim, Sunmi;Choi, Seongman;Myoung, Rho-Shin;Kim, Woncheol
    • Journal of the Korean Society of Propulsion Engineers
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    • v.20 no.5
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    • pp.1-8
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    • 2016
  • Micro turbojet engine test and infrared signal measurement were conducted to understand the characteristics of the engine performance and infrared signal with the variants of the exhaust nozzle configuration. A cone type nozzle and five rectangle type nozzles which has aspect ratio from one to five were used for the experimental work. The results show that there are not much difference between cone and rectangle nozzles of the thrust and specific fuel consumption. However infrared signal from exhaust gas become smaller as increasing aspect ratio.

A Study of Valve-train Life Time Estimate in Engine Durability Test (2) (엔진내구시험을 통한 Valve Train 수명예측에 관한 연구 (2))

  • Kim, Jaejin;Lee, Hwanhui;Myung, Wanghee;Min, Byengdu
    • Transactions of the Korean Society of Automotive Engineers
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    • v.22 no.3
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    • pp.75-80
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    • 2014
  • In previous study, make an attempt to estimate exhaust valve seat and seat-ring wear acceleration factor for engine durability test with measuring and consideration of wear mechanism. But found abnormal initial wear rate in exhaust valve seat-ring. And have to improve exhaust valve seat-ring wear rate for reliability reason, because next GDI/Turbo engine is based on this engine and GDI/Turbo engine have higher combustion pressure and higher thermal load. In this study, Trying to find the cause of abnormal wear factor, improve valve-train durability by change specification & design of parts and verify variant parts for improving durability of valve-train. And then I would like to propose a design guide line of valve-train system in a reliability point of view, besides make a complement of previous study.

EGR Effects on Exhaust Gas of Heavy-Duty Turbo Charge Engine with Low Pressure Route System (저압방식을 적용한 대형과급기관의 배기가스에 관한 EGR효과)

  • 오용석
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.3 no.1
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    • pp.58-62
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    • 2002
  • The efforts of EGR on performance and emissions were investigated in this study. The engine used for the tests was a six-cylinder, 11 liter, and turbo-charged, heavy-duty diesel engine with a low pressure route ECR system. The volume of recirculated gas was controlled by a manually operated valve which was installed between the turbine outlet and compressor inlet. The experiments were performed at various engine speeds and loads while the ECR rates were set at 4% and 8%. Exhaust emissions with EGR system were compared with the baseline emissions.

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Sensor Fault Detection for Small Turboshaft Engine Considering Multiple Trim Conditions (다중 트림 상태를 고려한 소형 터보샤프트 엔진의 센서 고장 검출)

  • Seong, Sang-Man;Rhee, Ihn-Seok;Ryu, Hyeok
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2008.11a
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    • pp.192-195
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    • 2008
  • A sensor fault detection method for small turbo shaft engine considering multiple trim conditions is proposed. This engine is used in a helicopter. Firstly, under multiple trim conditions, we derive the linearized models from a nonlinear model which includes engine, rotor and feedback control loop. As a fault detection method, we adopt the Kalman filter based method. To keep continuity of estimates between the changes of trim conditions, we reconfigure the initial values of state variables at trim changes. We detect the faults with two steps that when the first filter does not alarm the faults for some sensors, the second filter is runned for other sensor. Via some simulations we show that the proposed method works well under multiple trim conditions.

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Development of Cryogenic Test Rig for Ball-Bearing and Evaluation of the Performance of the Prototype Ball-Bearing of Turbo pump (극저온 환경용 볼베어링 시험장치 개발 및 터보펌프용 볼베어링 시제품의 성능평가)

  • Jo, Jun Hyeon;Rhim, Yoon Chul;Lee, Sungchul;Kim, Choong Hyun
    • Tribology and Lubricants
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    • v.28 no.4
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    • pp.167-172
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    • 2012
  • The turbo pump of a liquid rocket engine is composed of three main parts: the oxidizer pump, fuel pump, and turbine. Liquid oxygen ($LO_X$) is the working fluid in the cryogenic environment in the oxidizer pump, but tests are usually performed using liquid nitrogen ($LN_2$), which has a boiling point similar to that of $LO_X$ but is comparatively safer and easier to use for the test. In this study, a bearing test rig is developed and its performance is evaluated using a cryogenic ball bearing with $LN_2$ as the working fluid. Verifying the performance of the bearing test rig is crucial for ensuring correct working of the turbo pump unit in the liquid rocket engine. A stable test rig for the bearing in a cryogenic environment makes the bearing technology enhance its reliability. The test results show that the system operates stably and the requirement of performance time of 500 s is met. The test results of temperature, motor speed, and torque are discussed. The developed cryogenic bearing test rig is expected to help in widening knowledge and expanding research on ball bearings in the future.

A Study on the Starter Control of the Turbo Generator (터보 제너레이터의 시동기 제어에 관한 연구)

  • 박승엽;노민식
    • Journal of Institute of Control, Robotics and Systems
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    • v.10 no.3
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    • pp.286-293
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    • 2004
  • This paper presents the result of a study on the starter control for a turbo generator. Because a starter in gear box type turbo-generator system is composed of gearbox and brush DC motor, it should be replaced with High Speed Generator(HSG)) in HSG type Turbo-generator. There-ore, it is necessary to design a new starting algorithm and starter. In gearbox type system, brush DC motor is rotated to the designed speed using low voltage-high current battery power. After brush DC motor speed is increased to several times by gearbox, gas turbine engine can be rotated to designed starting speed. If we implement a starter with High Speed Generator(HSG), it is necessary to drive high-speed generator to high-speed motor. High-speed generator with permanent magnet on rotor has a low leakage inductance fur driving high-speed rotation, and it is necessary high DC link voltage for inverter when High-speed generator is driven to high speed. This paper presents result of development of the boost converter for converting high voltage DC from low battery voltage and design of the inverter for controlling a high frequency current to be injected to motor winding. Also, we show performance of the designed starter by driving the turbo generator.

Development of T700/701K engine for KUH (한국형 기동 헬기 엔진 (T700/701K) 개발)

  • Kim, Jae-Hwan;Ahn, Iee-Ki;Lee, Dae-Sung;Sung, Ok-Suck;Sung, In-Kyung
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2010.11a
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    • pp.506-511
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    • 2010
  • This paper presents development activities of the T700/701K turbo-shaft engine for Korean Utility Helicopter(KUH). The T700/701K is the first rear-drive variant of the GE's T700 engine which is proven for military applications in the world. The main workscope of the development includes a modification from a front-drive engine to a rear-drive one, an performance enhancement of the power turbine and an incorporation of two channel FADEC(Full Authority Digital Engine Control) system for more reliable operation. The first engine run for development and qualification test was successfully completed in 2008. Since the PFRT(Preliminary Flight Rating Test) has been completed, the first flight of the engine installed in the first prototype of KUH has been successfully demonstrated in March, 2010 and the engine installation compatibility tests are being carried out during KUH flight test. The test and evaluation for qualification of the engine has been done except for the LCF test up to date.

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Development Trend of Korean Staged Combustion Cycle Rocket Engine (한국형 다단연소사이클 로켓엔진 개발 동향)

  • Kim, Chae-hyoung;Han, Yeoung Min;Cho, Namkyung;Kim, Seung-Han;Yu, Byungil;Lee, Kwang-Jin;So, Younseok;Woo, Seongphil;Im, Ji-Hyuk;Hwang, Chang Hwan;Lee, Jungho;Kim, Jin-han
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2017.05a
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    • pp.79-87
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    • 2017
  • Korea Aerospace Research Institute has being developed a staged combustion cycle rocket (SCCR) engine with high specific impulse to send a 3-ton class satellite into geostationary orbit while conducted Korean Space Launch Vehicle (KSLV) II project. The SCCR engine is different from the KSLV-II engine, which is open cycle engine using a gas-generator. The SCCR engine with closed cycle is composed of a pre-burner, a turbo pump, and a main combustor. The technology demonstration model (TDM0) was assembled and tested in the 7ton-class engine combustion test facility of Naro Space Center, and the combustion test was successfully conducted. Afterward engine-shaped SCCR engine model (TDM1) is being designed and developed for the next combustion test.

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