• Title/Summary/Keyword: waste aluminum dross

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Test Run for the Production of Aluminum Hydroxide by Recycling of Waste Aluminum Dross (알루미늄 폐드로스로부터 수산화알루미늄 생산 시운전 결과)

  • Lee Hooin;Park Ryungkyu;Kim Joonsoo
    • Resources Recycling
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    • v.13 no.2
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    • pp.47-53
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    • 2004
  • Waste aluminum dross is a major waste in the aluminum scrap smelters, and some metallic aluminum remains in the waste dross. In the previous study, waste aluminum dross was leached with sodium hydroxide solution to extract the remained aluminum into the solution, and aluminum hydroxide precipitate was recovered from the leached solution. A pilot plant was constructed and tested to demonstrate the developed technology. One thousand tons of waste aluminum dross could be processed, and about five hundred tons of aluminum hydroxide could be produced in the pilot plant. From the test run of the pilot plant, it was confirmed that the developed technology could be employed as a commercial scale and the produced aluminum hydroxide could be used for water treatment agent.

Preparation of Alum for Water Treatment Product Using Waste Aluminum Dross (알루미늄 폐드로스로부터 수처리응집제용 황산알루미늄 제조)

  • Park, Hyung-Kyu;Choi, Young-Yoon;Eom, Hyung-Choon;Bae, Dong-Su
    • Resources Recycling
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    • v.15 no.4 s.72
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    • pp.60-63
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    • 2006
  • Waste aluminum dross was leached with sulfuric acid to prepare alum used for water treatment product. The remained metallic aluminum in the waste aluminum dross was extracted into the solution to make aluminum sulfate solution. The solution could be used as alum for water treatment product after adjusting the required alumina concentration and the basicity. Comparing to the conventional method for alum using aluminum hydroxide, material cost could be saved in this method. Also, there is an additional merit in view of recycling of the waste aluminum dross by reducing the amount of waste dross to be landfilled.

Preparation of PAC for Water Treatment Chemicals Using Waste Aluminum Dross (알루미늄 폐드로스로부터 수처리응집제용 염화알루미늄 제조)

  • Park, Hyung-Kyu;Choi, Young-Yoon;Eom, Hyoung-Choon;Bae, Dong-Su
    • Resources Recycling
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    • v.15 no.5 s.73
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    • pp.52-56
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    • 2006
  • Waste aluminum dross was leached with hydrochloric acid to prepare PAC, poly aluminium chloride, used as water treatment chemicals. Metallic aluminum remained in the waste aluminum dross was dissolved into the hydrochloric acid solution. The solution could be used as PAC after adjusting the required alumina concentration and the basicity. Comparing to the conventional method far preparation of PAC using aluminum hydroxide, material cost could be saved in this method. Also, there is an additional merit in view of recycling of the waste aluminum dross by reducing the amount of waste dross to be landfilled.

Preparation of Alum and Poly Aluminum Chloride Using Waste Aluminum Dross (알루미늄 폐드로스를 재활용(再活用)한 Alum과 Poly Aluminum Chloride 제조(製造) 연구(硏究))

  • Park, Hyung-Kyu;Lee, Hoo-In;Choi, Young-Yoon
    • Resources Recycling
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    • v.16 no.5
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    • pp.3-7
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    • 2007
  • Waste aluminum dross was processed to prepare alum with sulfuric acid, and poly aluminum chloride(PAC) with hydrochloric acid. Metallic aluminum remained in the waste dross was dissolved into the sulfuric acid solution, and the solution could be used as alum for water treatment chemicals after adjusting the required alumina concentration and pH of the solution. Also, it was dissolved into the hydrochloric acid solution and processed to make PAC solution. Compared with the conventional method for preparation of alum and PAC using aluminum hydroxide, material cost could be saved in this method. Also, there is an additional merit in view of recycling of the waste aluminum dross by reducing the amount of waste disposed to landfill.

Test Run of the Pilot Plant for Recycling of the Waste Aluminum Dross (알루미늄 페드로스 재활용 파일롯트플랜트 시운전 결과)

  • Park, Hyung-Kyu;Lee, Hoo-In;Choi, Young-Yoon
    • Resources Recycling
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    • v.14 no.4 s.66
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    • pp.41-46
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    • 2005
  • Waste aluminum dross is a major waste in the aluminum scrap smelters and its major components are alumina and metallic aluminum. In this study, waste aluminum dross was leached with sodium hydroxide solution to extract the remained aluminum into the solution, and aluminum hydroxide was recovered from the leached solution. The dross residue generated at the leaching step was recycled into alumina base ceramic materials through a series of treatments such as washing, drying and roasting. Also, a pilot plant was constructed and tested to demonstrate the developed technology. Four tons of waste aluminum dross could be processed per day. From the test run of the pilot plant, it was confirmed that the developed technology could be applied to commercialization.

Preparation of Castable Refractories by Recycling of Aluminum Dross (알루미늄드로스를 재활용한 캐스타블내화물 제조)

  • Park Hyungkyu;Lee Hooin;Lee Jinyoung
    • Resources Recycling
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    • v.12 no.3
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    • pp.46-53
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    • 2003
  • Recycling of aluminum dross is an important issue in the secondary aluminum industries. In this study, aluminum dross generated in the domestic secondary aluminum industry was processed to use it as raw material for producing alumina refractories. Sample dross was classified according to its size. The dross smaller than 1 mm was leached with sodium hydroxide solution to extract the remained aluminum from the dross into the solution. and then aluminum hydroxide precipitate was recovered from the leach liquor. The waste residue in the leaching was washed, dried and roasted. Most remained metallic components in the residue was changed into oxide through the processes. The roasted dross was made into alumina castable refractories by mixing with aggregates and a binder. Bending strength of the tested castable specimen was over $25\;kg/\textrm{m}^2$ and compressive strength over $80\;kg/\textrm{cm}^2$, which satisfied the Korean Standard value respectively. From the results, it was suggested that this process could be applicable to recycling of aluminum dross.

Test Run of Pilot Plant for Recycling of the Leached Residue in the Processing of Waste Aluminum Dross (알루미늄 폐드로스 침출잔사 처리 파일롯트 플랜트 시운전 결과)

  • 박형규;이후인
    • Resources Recycling
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    • v.13 no.3
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    • pp.50-57
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    • 2004
  • Waste aluminum dross is a major waste in the aluminum scrap smelters and its components are mostly alumina and remained metallic aluminum. In the process to extract the remained aluminum from the waste dross by leaching with sodium hydroxide solution, residue is generated and its main component is alumina. This residue could be recycled into ceramic materials such as alumina castable refractories by going through a series of treatments such as washing, drying and roasting. In this study, a pilot plant was constructed and tested to demonstrate the developed technology. One thousand tons of waste aluminum dross could be processed, and about seven hundred tons of ceramic materials produced in the demonstration line. From the test run of the pilot plant, although it was confirmed that the developed technology could be applied to commercialization, several technical improvements were found to be necessary for reducing impurities such as Na, Fe and for reforming drying equipment.

The Preparation of porous ceramic material from aluminum waste dross (알루미늄 廢드로스를 活用한 세라믹 多孔體의 製造)

  • Kim, Ki-Seok;Park, Jay-Hyun;Park, Jai-Koo
    • Resources Recycling
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    • v.14 no.2
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    • pp.19-27
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    • 2005
  • The recycling possibility of aluminum waste dross(AWD) as a ceramic raw material of porous light-weight material was examined. A aluminum waste dross was washed 4-7 consecutive times and roasted at 900$^{\circ}% for 1hour as pre-treatments. The properties of the pre-treatment of aluminum waste dross was investigated. It was conformed by XRD result that the spinel crystalline was grown in AWD, after roasting. After the roasted AWD was ground in aqueous state, the sodium hexaphosphate(SHP) as a dispersant which is used for stabilizing the concentrated slurry was added to the AWD slurry. The porous material was prepared by slurry foaming method with surfactant at room temperature. The foamed slurry volumes were 2 and 3 times of the original slurry volume. The properties of porous material with extended volume of 3 times was following: the porosity was about 84%, bulk density was 0.59 g/cm$^3$, the range of pore was from 50 ${\mu}m$ to 500 ${\mu}m$ and mean pore size was about 200 ${\mu}m$. AWD porous material was sintered at 1150$^{\circ}C-1250$^{\circ}C. It was colcluded that AWD was sintered well at 1200$^{\circ}C from material surface observation by SEM.

Minimizing Zinc Consumption In Hot-Dip Galvanizing Lines

  • Bright, Mark;Ellis, Suzanne
    • Corrosion Science and Technology
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    • v.10 no.2
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    • pp.43-46
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    • 2011
  • Zinc consumption in a continuous galvanizing line is one of the highest operating cost items in the facility and minimizing zinc waste is a key economic objective for any operation. One of the primary sources of excessive loss of zinc is through the formation of top dross and skimmings in the coating pot. It has been reported that the top skimmings, manually removed from the bath, typically consist of more than 80% metallic zinc with the remainder being entrained dross particles ($Fe_2Al_5$) along with some oxides. Depending on the drossing practices and bath management, the composition of the removed top skimmings may contain up to 2 wt% aluminum and 1 wt% iron. On-going research efforts have been aimed at in-house recovery of the metallic zinc from the discarded top skimmings prior to selling to zinc recycling brokers. However, attempting to recover the zinc entrapped in the skimmings is difficult due to the complex nature of the intermetallic dross particles and the quality and volume of the recycled zinc is highly susceptible to fluctuations in processing parameters. As such, an efficient method to extract metallic zinc from top skimmings has been optimized through the use of a specialized thermo-mechanical process enabling a continuous galvanizing facility to conserve zinc usage on-site. Also, through this work, it has been identified that filtration of discrete dross particles has been proven effective at maintaining the cleanliness of the zinc. Future efforts may progress towards expanded utilization of filters in continuous galvanizing.