• Title/Summary/Keyword: screw pumping system

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Optimization of Screw Pumping System (SPS) for Mass Production of Entrapped Bifidus

  • Ryu, Ji-Sung;Lee, Yoon-Jong;Choi, Soo-Im;Lee, Jae-Won;Heo, Tae-Ryeon
    • Food Science and Biotechnology
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    • v.14 no.5
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    • pp.566-571
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    • 2005
  • Process of screw-pumping system (SPS) was optimized for mass production of encapsulated bifidus. SPS entrapment device was composed of feeding component, with optimized nozzle size and length of 18G (0.91 cm) and 4 mm, respectively, screw pump, and 37-multi-nozzle. Screw component had five wing turns [radius (r)=26 to 15 mm] from top to bottom of axis at 78-degree angle from middle of the screw, and two wings were positioned at screw edge to push materials toward nozzle. For nozzle component, 37 nozzles were attached to 20-mm round plate. Air compressor was attached to SPS to increase productivity of encapsulated bifidus. This system could be operated with highly viscous (more than 300 cp) materials, and productivity was higher than $1128\;{\pm}\;30\;beads/min$. Viability of encapsulated bifidus was $5.45\;{\times}\;10^8\;cfu$/bead, which is superior to that of encapsulated bifidus produced by other methods ($2.51{\times}10^8\;cfu$/bead). Average diameter of produced beads was $2.048\;{\pm}\;0.003\;mm$. Survival rate of SPS-produced encapsulated bifidus was 90% for Simulator of the Human Intestinal Microbial Ecosystem test and 88% in fermented milk (for 14 days). These results show SPS is effective for use in development of economical system for mass production of viable encapsulated bifidus.

Study of industrial water calculation improvement by use Alternative Energy (대체에너지 사용시 공업용수 순환 개선을 위한 연구)

  • Choi, Do-Sun
    • The Journal of Korea Institute of Information, Electronics, and Communication Technology
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    • v.4 no.4
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    • pp.307-310
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    • 2011
  • In this paper we use general centrifugal pump instead of screw pump in alternative Energy system. This alternative Energy system with screw pump compared the volume flour of water pumping and efficiency. Screw pump is designed that it rotated without a toque in another Shaft. Futhermore it have noise and abrasion, The pump used in high pressure with fast rotate.

Screw Pumping System을 이용한 Algiante bead의 생산

  • Ryu, Ji-Seong;Lee, Yun-Jong;Yun, Yeong-Sil;Heo, Tae-Ryeon
    • 한국생물공학회:학술대회논문집
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    • 2003.04a
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    • pp.750-753
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    • 2003
  • A method for the mass production was designed by using a screw pumping system that can supply safe bifidobacteria. To prevent the inhibition of cell activity, various additives, which are able to preserve pore of an alginate bead, were used. When materials are sterilized, viscosity decreased below 300cp. Adding bifidobacteria, viscosity increased to 300cp. We manufactured various extrusion nozzles and tested mass productivity of the alginate bead. As a result, 18G, 4mm length sylinge with 13 multi-nozzle showed the best productivity which was about $308{\pm}3ea/min$.

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Development of the Underwater Cleaning Robot Platform for a Higher Efficiency (고효율 수중청소로봇 플랫폼 기술 개발)

  • Suh, Jin-Ho;Lee, Jung-Woo;Kim, Jong-Geol;Choi, Young-Ho;Choi, Il-Seop
    • Journal of Power System Engineering
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    • v.21 no.3
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    • pp.74-84
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    • 2017
  • This paper presents the development of the underwater cleaning robot platform for a higher efficiency in manufacturing industry. Human operators directly go into the cistern and clean sludge after drainage of the water so far. It is sometimes dangerous because of the harmful chemical materials from the product making process. In addition, it takes long time for water drainage and supplying it back. However, the robot cleaning operation does not need to drain water so that it could be applied to the sludge cleaning work at any time without the plant pause. Moreover, it can prevent the safety accidents because human operators are not necessary to enter directly the sludge cisterns. This paper shows the performance of cleaning work that can be applied in the industrial field through the design and development of underwater cleaning robot platform. And these results demonstrate that the developed underwater cleaning robot has great possibilities to clean other industrial water cisterns.

A Study of Electromagnetic Actuator for Electro-pneumatic Driven Ventricular Assist Device

  • Jung Min Woo;Hwang Chang Mo;Jeong Gi Seok;Kang Jung Soo;Ahn Chi Bum;Kim Kyung Hyun;Lee Jung Joo;Park Yong Doo;Sun Kyung
    • Journal of Biomedical Engineering Research
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    • v.26 no.6
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    • pp.393-398
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    • 2005
  • An electromechanical type is the most useful mechanism in the various pumping mechanisms. It, however, requires a movement converting system including a ball screw, a helical cam, or a solenoid-beam spring, which makes the device complex and may lessen reliability. Thus, the authors have hypothesized that an electromagnetic actuator mechanism can eliminate the movement converting system and that thereby enhance the mechanical reliability and operative simplicity of an electro­pneumatic pump. The purpose of this study was to show a novel application of electromagnetic actuator mechanism in pulsatile pump and to provide preliminary data for further evaluations. The electromagnetic actuator consists of stators with a single winding excitation coil and movers with a high energy density neodymium-iron-boron permanent magnet. A 0.5mm diameter wire was used for the excitation coil, and 1000 turns were wound onto the stators core with parallel. A prototype of extracorporeal electro-pneumatic pump was constructed, and the pump performance tests were performed using a mock system to evaluate the efficiency of the electromagnetic actuator mechanism. When forward and backward electric currents were supplied to the excitation coil, the mover effectively moved back and forth. The nominal stroke length of the actuator was 10mm. The actuator dimension was 120mm in diameter and 65mm in height with a mass of 1.4kg. The prototype pump unit was 150mm in diameter, 150mm in thickness and 4.5kg in weight. The maximum force output was 70N at input current of 4.5A and the maximum pump rate was 150 beats per minute. The maximum output was 2.0 L/minute at a rate of 80bpm when the afterload was 100mmHg. The electromagnetic actuator mechanism was successfully applied to construct the prototype of extracorporeal electro­pneumatic pump. The authors provide the above results as a preliminary data for further studies.