• Title/Summary/Keyword: plating process

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Effect of drawbead process parameters on the drawing characteristics of sheet metals for automotive parts (자동차용 판재 성형시 드로우비드 공정인자별 인출특성에 대한 연구)

  • 김원태;이동활;강우순;서만석;문영훈
    • Proceedings of the Korean Society for Technology of Plasticity Conference
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    • 2003.10a
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    • pp.140-143
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    • 2003
  • The drawbead is an important part in sheet metal forming for automotive part and its effect is affected by various process parameters. Therefore in this study, drawbead friction test was performed at various process parameters - panels (cold rolled and galvanized sheet steel), lubricants (having three different viscosities), bead materials(steel, iron) and surface treatment of bead (Cr plating). Circular shape bead has been used for the test. The results show that friction and drawing characteristics were mainly influenced by the nature of zinc coating, viscosity of lubricants, surface treatment of a bead and hardness of coated layer.

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Fabrication of Fine Metal Mask using Electroforming process (전주공정을 이용한 파인메탈마스크 제작)

  • Kang, D.C.;Kim, H.Y.;Jeon, B.H.
    • Proceedings of the Korean Society for Technology of Plasticity Conference
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    • 2006.05a
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    • pp.314-317
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    • 2006
  • Electroformed part is widely used in modem manufacturing industries, especially semi-conductor division. It is basically a specialized form of electroplating. So, it has very similar parameters with electroplating. The object of this study is development of the fine metal mask by electroforming process. In this paper considered two parameters. The first is relationship of UV exposure and soft baking time. The other one is thickness uniformity of electroformed parts by distance of between electrodes. This paper presents the fabrication method of fine metal mask by electroforming process.

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A Study on the Improvement of Double Injection-molding Keypad Process (이중 사출 키패드 성형 공정 개선에 관한 연구)

  • Hong, Min-Sung;Lee, Ji-Hoon;Shin, Soo-Hyun
    • Journal of the Korean Society of Manufacturing Technology Engineers
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    • v.20 no.5
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    • pp.659-665
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    • 2011
  • Recently, the plastic resin such as PC, ABS are widely used in IT market. Especially, in most cases the keypads mounted on the mobile phone are the dual-injection-plated type. Environmental regulation is based on the quality of injection-molded products and the minimum process steps are required to avoid the plating defects. Various parameters to produce the injection-molded plastic products make it difficult to obtain the desired stability. However, the past experience and the use of CAE analysis make it possible to predict the problems occurred in injection molding process. Especially, the problems of the weld lines such as runner balancing, bending, deformation and forming defects can be solved systematically and minimized by CAE analysis. Through this study, the non-uniform volumetric shrinkage and the difference in temperature distribution induce the deformation and the high value of stress causes the problems such as crack.

Fabrication of the 20{\mu}m$-height Polyimide Microstructure Using $O_2$ RIE Process ($O_2$ RIE 공정을 이용한 20{\mu}m$ 두께의 폴리이미드 마이크로 구조물의 제작)

  • Baek, Chang-Wook;Kim, Yong-Kweon
    • Proceedings of the KIEE Conference
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    • 1995.11a
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    • pp.600-602
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    • 1995
  • Using the $O_2$ RIE process, 20{\mu}m$-height polyimide microstructures are fabricated. In LIGA-like process, metal microstructure can be formed by the electroplating using these polyimide microstructures as a plating mould. Reactive ion Etching technique using oxygen gas is used for the patterning of polyimide. The etching rate of the polyimide is increased with increased pressure and RF power. The anisotropic vertical sidewall can be obtained at low pressure, but the etched surface state is not so good yet. "Micrograss", which is formed during the RIE and disturbs uniform electroplating, can be removed effectively by the wet itching of the chromium sacrificial layer. More studies about the improvement of an etched surface state and the removal of microsgrass are needed.

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Silicon Solar Cell Efficiency Improvement with surface Damage Removal Etching and Anti-reflection Coating Process (표면결함식각 및 반사방지막 열처리에 따른 태양전지의 효율 개선)

  • Cho, Chan Seob;Oh, Jeong Hwa;Lee, Byeungleul;Kim, Bong Hwan
    • Journal of the Semiconductor & Display Technology
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    • v.13 no.2
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    • pp.29-35
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    • 2014
  • In this study general solar cell production process was complemented, with research on improvement of solar cell efficiency through surface structure and thermal annealing process. Firstly, to form the pyramid structure, the saw damage removal (SDR) processed surface was undergone texturing process with reactive ion etching (RIE). Then, for the formation of smooth pyramid structure to facilitate uniform doping and electrode formation, the surface was etched with HND(HF : HNO3 : D.I. water=5 : 100 : 100) solution. Notably, due to uniform doping the leakage current decreased greatly. Also, for the enhancement and maintenance of minority carrier lifetime, antireflection coating thermal annealing was done. To maintain this increased lifetime, front electrode was formed through Au plating process without high temperature firing process. Through these changes in two processes, the leakage current effect could be decreased and furthermore, the conversion efficiency could be increased. Therefore, compared to the general solar cell with a conversion efficiency of 15.89%, production of high efficiency solar cell with a conversion efficiency of 17.24% was made possible.

The Microstructure of Magnetite Coated on Honeycomb and Characteristics of CO2 Decomposition (허니컴에 코팅한 마그네타이트의 미세구조 및 CO2 분해특성)

  • 윤용운;김은배;이병하;고태경;오재희
    • Journal of the Korean Ceramic Society
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    • v.41 no.5
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    • pp.410-416
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    • 2004
  • In this study, we fabricated magnetite coated on a cordierite honeycomb which has complex shape by ultrasound-enhanced ferrite plating. The effects of the plating condition on the formation of the magnetite and its microstructure were investigated. The magnetite coated on the honeycomb became an oxygen-deficient ferrite by H$_2$ gas reduction, then the effects of the molar concentrations of ammonium acetate for $CO_2$ gas decomposition have been studied. As the molar concentration of a pH buffer($CH_3$COONH$_4$, 0.1946∼0.3892 M) solution increased, the average particle size increased about 200∼250 nm. The magnetite coated on the honeycomb was reduced by H$_2$ gas for 2 h at 30$0^{\circ}C$. The inner pressure change in the cell began to occur at 315∼34$0^{\circ}C$. The H$_2$-Reduced magnetite coated on the honeycomb at 35$0^{\circ}C$ contained an oxygen deficient magnetite and $\alpha$-Fe phase. The thermogravimetric analysis with H$_2$ reduction and $CO_2$ decomposition were carried out with the magnetite coated on the honeycomb. A weight loss in process of H$_2$ reduction occurred between 32$0^{\circ}C$ and 34$0^{\circ}C$, while a weight gain was observed during the $CO_2$ decomposition.

Clinical Aspects among Platers (도금공(鍍金工)에 대한 임상적(臨床的) 관찰(觀察))

  • Kim, Doo-Hie
    • Journal of Preventive Medicine and Public Health
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    • v.10 no.1
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    • pp.16-24
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    • 1977
  • This is a result of clinical examination for workers working with Chromic acid and Chromium compounds in the plating room of their companies. I selected two companies that the plating process and the kinds of plating were similar. One (SW Co.) was more or less improved the operating environment with the ventilation machine so on and another (SR Co.) did not it so. The former was examined at March 29th 1977, the latter was at June 28th 1976. But the respiratory communicable diseases, flue or common cold so on were not spreaded there at that time. The clinical aspects were compared between the group of SW, and SR. The swelling and hyperemic signs of nasal mucous membrane and the experience of nasal bleeding were about 50%, generally, in all the groups. The following problem was dizziness or vertigo. The nasal signs in the group of SW (improved ventilation of the room air) were relatively weak, but in another, it was some what severe; - there was necrotic sign with thick nasal clast. They were only used of gauze mask when the vapors of various solvents were deeply full in the room. And there was very high rate of bronchial signs, sputum or coughing in the group of SW improved ventilation so called, than another one. I suppose that it means chronic inflammatory change of the bronchial mucous membrane with deeper signs, due to the individual protectors were carelessly or not used according to the improving of the operating environment. Theses nasal signs mentioned the above were not nearly in the other groups had not been done the Chromium plating. The Status of RBC, Hb and Ht, of urine protein and urobilinogen were mostly in normal range. But the number of WBC was more or less showed with a positive correlation to the working duration.

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Optimization of Electrolysis Using Sacrificial Electrode for the Treatment of Electroless Nickel Plating Wastewater (희생전극을 이용한 무전해 니켈 도금 폐수의 전기분해처리 최적화)

  • Kim, Young-Shin;Jeon, Byeong-Han;Cho, Soon-Haing
    • Journal of Korean Society of Environmental Engineers
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    • v.37 no.4
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    • pp.204-209
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    • 2015
  • The effluent limit of nickel from electroplating wastewater has been strengthened from 5 mg/L to 3 mg/L from 2014. However, currently applied treatment process for nickel plating wastewater is unable to meet the effluent limit, most of the treatment concept conducted by treatment plant is dilution with other metal bearing wastewater. This can cause very significant impact to the environment of nickel contamination. With this connection, the feasibility test has been conducted with the use of electrolysis by using sacrificial electrodes. Experiments were conducted in synthetic and electroless nickel plating wastewater. Optimal condition of current density, pH were derived from the synthetic wastewater. It was found that the removal efficiency of nickel exceeded 94% at the operation condition of at pH 9 and the current density of $1{\sim}2mA/cm^2$. At this conditions, the iron sludge was generated very low amount. However, it was unsuccessful to meet the effluent limit by applying these treatment conditions to the real electroplating wastewater. This can be explained due to the matrix effect of other metals and anions contained real electroplating wastewater. From the result of further study, the optimal conditions for the real wastewater treatment were found out to be at pH 9, current density $6{\sim}7mA/cm^2$, for 5 minutes of operating time. At these conditions, 88% removal of nickel was achieved, which results the residual nickel concentration was below 3 mg/L.

A Study on Microstructure, Mechanical Properties, Friction and Adhesion of TiN Thin Films Coated on SKD61 and Radical Nitrided SKD61 Substrates by Arc Ion Plating (SKD61과 Radical Nitriding 처리된 SKD61 기판상에 Arc Ion Plating으로 증착된 TiN 박막의 미세구조 및 기계적 특성, 마찰 및 접착력에 관한 연구)

  • Joo, Yun-Kon;Yoon, Jae-Hong;Fang, Wei;Zhang, Shi-Hong;Cho, Tong-Yul;Ha, Sung-Sik
    • Journal of the Korean institute of surface engineering
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    • v.40 no.6
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    • pp.254-257
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    • 2007
  • TiN coating on tool steel has been widely used for the improvement of durability of tools. In this work, radical nitriding(RN) is carried out on SKD61 at $450^{\circ}C$ for 5 hours in the ammonia gas pressure $2.7{\times}10^3\;Pa$. The TiN coating is carried out by arc ion plating(AIP) with the process parameters: arc power 150 A, bias voltage -50V, coating time 40 minutes and nitrogen gas pressure $4{\times}10^3\;Pa$. Hardness, elastic modulus, friction coefficient and adhesion of TiN coating on substrates of both TiN/SKD61 and TiN/RN SKD61 coatings are investigated comparatively. The primary crystalline faces of TiN surface are(200) and(111) for TiN/SKD61 and TiN/RN SKD61 respectively. In addition to the primary phase, Fe phase exists in TiN/SKD61 coating, but not in TIN/RN SKD61. The hardness of TiN/RN SKD61 is about 700 Hv, 250 Hv(56%) higher than that of TiN/SKD61 at the near interface of TiN and substrates. At the TiN surface, hardness of TiN/RN SKD61 is 2,149 Hv, 71 Hv(3%) higher than that of TiN/SKD61. The elastic modulus of TiN coating is improved to 26.7 GPa(6%) by radical nitriding. The adhesion is improved by the RN coating showing no spalling. buckling and chipping on the scratch test track which are shown on the non-RN TiN/SKD61.

A Study on the Manufacturing Process of Fe-Ti Type Electrode for Ni/MH Secondary Battery (Ni/MH 2차전지용 Fe-Ti계 전극 제조공정에 대한 연구)

  • Joung, Sang-sik;Kim, Ki-won;Ahn, Hyo-jun;Joung, Soon-dol
    • Transactions of the Korean hydrogen and new energy society
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    • v.9 no.2
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    • pp.65-75
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    • 1998
  • Five different processes were selected and tested to find an useful method of manufacturing Fe-Ti type electrode. Initially, FeTi alloy was prepared by melting in plasma arc furnace and then powdered for shaping. Electroless Ni plating on these powder particles before shaping improved the discharge characteristics. The effects of heat-treatments on the electrode characteristics were also investigated. The discharge capacities of electrods were increased with the increasing heat-treatment temperatures. When heat treated at $1000^{\circ}C$ after shaping, the best results were acquired in the discharge capacity and cycle life. Both electroless Ni plating and heat-treatment were appeared to be crucial for the performance improvement of FeTi type electrode. Fe-Ti -Mn electrodes were prepared according to the process suggested in this study and tested to verify the promising effects of that.

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