• Title/Summary/Keyword: pipe-line foundation

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An Study on Efficiency and Application of Thermal Siphon in the Permafrost (영구동토 지대에서 Thermal Siphon의 효율성 연구)

  • Kang, Jae-Mo;Kim, Hak-Seung
    • Proceedings of the Korean Geotechical Society Conference
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    • 2009.09a
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    • pp.963-966
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    • 2009
  • A Construction of pipe line foundation and railroad, buildings in a permafrost area requires engineering technology of ground stabilization. In the permafrost area, thermal siphons have been used to stabilize foundation by eliminating the heat of ground to the air. the thermal siphon is a passive heat transfer device that operates by convection through vaporization and condensation. The heat transfer from ground to the air is driven by a temperature difference across the unit. A buried part in ground working as vaporizing function and upper part work as condensing. In this study, buried thermal siphon around the pipe lines laid in the Vladivostok site and measuring temperature variation. It is found that the thermal siphons freezing ground faster and decrease temperature variation in winter season.

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Corrosion Reduction Techniques of Pipe Line Net Using DVGW (DVGW이론에 따른 상수관망의 부식방지에 관한 연구)

  • Choo, Tai-Ho;Kim, Ha-Il;Je, Sung-Jin;Ok, Chi-Youl
    • The Journal of the Korea Contents Association
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    • v.6 no.11
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    • pp.310-316
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    • 2006
  • Leakage of waterworks pipe line net cause loss of water resources, additional foundation of pressurization facilities from pressure loss and soil weakening near leaked pipe line, etc.. This makes it difficult to maintain and manage waterworks pipe line net and so cause serious economic loss. The rate of accounted water can be improved by monitoring always water pressure and flux, and so on. from isolated region, preparing positively against leakage accident and preventing leakage from occurring. Actually after isolating region, average rate of accounted water in this region went up 88.94% by continuously monitoring control of water pressure and inflow rate. It is about 9.44% higher than that of Busan metropolitan city in 2003, 79.5%.

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Safety Factor of Rigid Sewer Pipe by Different Types of Foundation and Backfill (기초형식 및 뒤채움재 종류별 강성관용 하수관거의 안전율)

  • Lee, Kwan-Ho;Kim, Seong-Kyum
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.20 no.4
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    • pp.606-612
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    • 2019
  • The main causes of subsidence and sinkholes in the lower part of urban roads are sewage line foundation and inadequate compaction of backfill material. This leads to many problems, such as the breakage of joints in sewer pipes, poor connection, pipe breakage, and cracks. To solve this problem, the support factor related to the sewer foundation and the safety factor according to the excavation depth were evaluated. For the foundation of rigidity tolerance, crushed stone foundation, and abandoned concrete foundation, a recently newly developed site assembly-type lightweight plastic foundation were used. Backfill materials were applied on site (sandy soil and clayey soil) and fluid backfill was recycled onsite. To evaluate the depth of excavation and the safety factor of each sewer pipe foundation, the design load considering the load factor and the support factor was evaluated. The support coefficients were 0.377 for a crushed stone foundation, 0.243 and 0.220 for an abandoned concrete foundation ($180^{\circ}$ and $120^{\circ}$), and 0.231 for a lightweight plastic foundation and fluid backfill. Overall, the safety factor was low when using the crushed stone foundation, and the safety rate was the highest when the foreclosed concrete foundation ($180^{\circ}$) was used. In addition, when the combination of lightweight plastic and fluid backfill materials was used, the safety factor was higher than that of abandoned concrete foundation ($120^{\circ}$), which means that the newly developed lightweight plastic foundation can be used as another alternative base of a steel pipe.

Reduction Techniques of the Pipe Line net Using According to DVGW (DVGW이론에 따른 상수관망의 부식방지를 위한 정수처리방안)

  • Choo Tai-Ho;Kim Ha-Il
    • Proceedings of the Korea Contents Association Conference
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    • 2005.11a
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    • pp.115-118
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    • 2005
  • Leakage of waterworks pipe line net cause loss of water resources, additional foundation of pressurization facilities from pressure loss and soil weakening near leaked pipe line, etc. This is difficult to maintain and manage waterworks pipe line net and to cause serious economic loss. Rate of accounted water is better by monitoring always water pressure and flux, etc. from isolated region, positively dealing with leakage accident and preventing leakage from occurring. Actually after isolating region, average rate of accounted water in this region is 88.94% by continuously monitering control of water pressure and inflow rate. It is about 9.44% more than that of Busan metropolitan city in 2003, 79.5%.

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The Effects of Sand Compaction by Watering through Field Compaction Test and Numerical Analysis (현장 및 수치해석을 통한 모래 물다짐지반의 다짐효과 연구)

  • Chun, Byungsik;Jang, Younsoo;Kim, Kwanggyu;Park, Dukhyum;Sung, Hwadon
    • Journal of the Korean GEO-environmental Society
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    • v.8 no.6
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    • pp.13-19
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    • 2007
  • This study examines a cause for damage of synthetic resins straight pipe occurred after pipe construction of underground electric power duct pipelines of ${\bigcirc}$ section work, ${\bigcirc}$ line, ${\bigcirc}{\bigcirc}$ city railroad. For this, we analyzed a parameter used for plan and structural analysis through a literature review. And the site condition was analyzed in detail, and test construction of the pipe line that simulated the site pipe line and test on compaction by watering were performed. In addition, an examination on subsurface settlement influence of foundation ground through a structural safety and a numerical analysis of power transmission pipe line was performed. As a result of the performance, relative density gained by compaction by watering was more than average and relative degree of compaction according to technical specification standard showed the result of about 90% in the case of good compaction by watering.

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A Case Study on Cost-Benefit Analysis of the Septic Tank and Exclusive Sewage Pipe Line in Designing the large Building at Combined Sewer District (합류식 하수도 지역에 대형 건축물 설계시 정화조 및 전용오수관로의 비용편익분석 사례연구)

  • Oh, Hyun-Taek;Kim, Sung-Tai;Lim, Byung-In;Kang, Byong-Jun;Park, Kyoo-Hong
    • Journal of Digital Convergence
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    • v.17 no.6
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    • pp.169-175
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    • 2019
  • The aim of this study is to examine the relative economic benefits between the septic tank and exclusive sewage pipe line in designing the large building at combined sewer districts. With the case study of Lotte World Tower Building, we analyze a cost-benefit between two alternatives. The research results showed 2 years of payback period, about ₩6.17 billion of NPV, and 1.93 of B/C ratio for installing the exclusive sewage pipe line in comparison with septic tank. This results provide useful guidelines for policy establishment of the septic tank closure and for plausibility of installing exclusive sewage pipe line when constructing a large building. In the future, it will be necessary to consider additional cost-benefit analysis including burden charge borne by causers, the burden of management responsibility with a exclusive sewage pipe line, and the economic benefits of reducing odor.

Laboratory Loading Test of Light-Weight Prefabricated Plastic Foundation for Sewage Pipe Line (하수관거용 플라스틱 조립식 경량기초의 하중재하실험)

  • Lee, Dong-Hang;Lee, Kwan-Ho
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.13 no.6
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    • pp.2757-2762
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    • 2012
  • Sewage pipelines are one of important infra-structures. The main reasons of sewage pipelint failure are improper backfill materials and compaction controls in field. Especially, it is very difficult to compact the lower part of circula pipelines. In order to overcome these problems, the prefabricated light-weight plastic foundation was developed. Couple of load-displacement tests were carried out to get the characteristic of failure. From the limited laboratory loading tests, the use of prefabricated light-weight plastic foundation is an alternative to solve the difficulty of backfill materials and compaction control.

A Study on the Method of Analysis and Design of Benchmark Pile in Permafrost Area (영구동토지역에서의 수준말뚝의 안정성 검토 및 설계방법 연구)

  • Jo, Cheon-Hwan;Lee, Won-Je;Hong, Seong-Wan
    • Geotechnical Engineering
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    • v.9 no.2
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    • pp.15-26
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    • 1993
  • Frost heave on foundation(or ice jacking) is defined that foundation is uplifted by heav- ing force exerted around foundation from freezing of soils. This phenominon is often occurred in the light -weight structure e.g, small building, electro - telegraph pole, street light, pipe line, budge and reference point of survey. Frost heave is the most important factor in design of foundation of structure and the key issue in understanding mechanism of foundation in permafrost area. In this study is reviewed the state of the art on the analysis method of frost heave in USSR and is suggested the design method of benchmark pile. On the basis of above results, this study suggests a design chart able to do esign simply the benchmark pile in Yakutsk region.

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The Characteristic of Strength for a Lime Stone in Donghae Area and Harden Cement Milk of Super Injection Grouting (동해 석회암과 SIG 고결체의 강도특성)

  • Park, Young-Ho;Kim, Nak-Young;Hong, Sa-Myun;Yook, Jeong-Hoon;Kim, Ki-Seog
    • Proceedings of the Korean Geotechical Society Conference
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    • 2004.03b
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    • pp.137-145
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    • 2004
  • Limestone zone in korea have been distributed to diagonal line so that it is wide from the Gangwondo to the Jeonlanamdo. The limestone cavity and fractured zone were formed by chemical weathering. Limestone cavity and fractured zone was reinforced with cemented milk(w/c=60%)by high pressure jet grouting by tripple -pipe to establish bridge foundation on the ground condition like limestone cavity. To analyze property of limestone and solid of cement milk(w/c=65%), mixed solid of cement, core NX size in the limestone cavity and fractured zone and compressive strength. Seismic tomograpy exploration was pcrforn1cd to analyze deformation modulus of limestone. The analysis suggests that deformation modulus of limestone has effect on uniaxial compressive strength, seismic velocity, seismic elasticity modulus. Average static elasticity modulus of limestone is $5.08{\times}10^5kgf/cm^2$, cement and coal mixed solid is $0.25{\times}10^5kgf/cm^2$, $0.095{\times}10^5kgf/cm^2$. Average seismic velocity of limestone is 5.240m/sec, cement and coal mixed solid is 2,211.3m/sec, 1,447.5m/sec. Average uniaxial compressive strength of limestone was $1,221.3kgf/cm^2$ and limestone specimen mixed with cement milk and solid of cement milk mixed with coal were $125.22kgf/cm^2$, $35kgf/cm^2$ each other. Average friction angle of limestone was $49.14^{\circ}$ and limestone specimen mixed with cement milk and solid of cement milk mixed with coal were $38.39^{\circ}, 25.83^{\circ}$ each other. Average cohesion of limestone was $137.7kgf/cm^2$ and limestone specimen mixed with cement milk and solid of cement milk mixed with coal were $23.5kgf/cm^2$, $15.5kgf/cm^2$ each other. Average deformation modulus of limestone was $2.84{\times}10^5kgf/cm^2$ and limestone specimen mixed with cement milk and solid of cement milk mixed with coal were $0.4{\times}10^5kgf/cm^2, 0.12{\times}10^5kgf/cm^2$ each other. It was analyzed that the elasticity and uniaxial compressive strength, seismic velocity of solid of cement milk mixed limestone pieces and coal had an highly interrelation regardless of existence of limestones pieces and coal but it had shown that limestones had an lower interrelation. In case of field seismic velocity and deformation of limestone, SIC solid of cement milk mixed with coal and limestone pieces had an highly interrelation.

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Project of Improving Good Agriculture Practice and Income by Intergrated Agricultural Farming (미얀마 우수농산물 재배기술 전수사업)

  • Lee, Young-Cheul;Choi, Dong-Yong
    • Journal of Practical Agriculture & Fisheries Research
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    • v.16 no.1
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    • pp.193-206
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    • 2014
  • The objectives of the project are to increase farmers' income through GAP and to reduce the loss of agricultural produce, for which the Korean partner takes a role of transferring needed technologies to the project site. To accomplish the project plan, it is set to implement the project with six components: construction of buildings, installation of agricultural facilities, establishment of demonstration farms, dispatching experts, conducting training program in Korea and provision of equipments. The Project Management Committee and the Project Implementation Team are consisted of Korean experts and senior officials from Department of Agriculture, Myanmar that managed the project systematically to ensure the success of the project. The process of the project are; the ceremony of laying the foundation and commencing the construction of training center in April, 2012. The Ribbon Cutting Ceremony for the completion of GAP Training Center was successfully held under PMC (MOAI, GAPI/ARDC) arrangement in SAl, Naypyitaw on June 17, 2012. The Chairman of GAPI, Dr. Sang Mu Lee, Director General U Kyaw Win of DOA, officials and staff members from Korea and Myanmar, teachers and students from SAl attended the ceremony. The team carried out an inspection and fixing donors' plates on donated project machineries, agro-equipments, vehicles, computers and printer, furniture, tools and so forth. Demonstration farm for paddy rice, fruits and vegetables was laid out in April, 2012. Twenty nine Korean rice varieties and many Korean vegetable varieties were introduced into GAP Project farm to check the suitability of the varieties under Myanmar growing conditions. Paddy was cultivated three times in DAR and twice in SAl. In June 2012, vinyl houses were started to be constructed for raising seedlings and finished in December 2012. Fruit orchard for mango, longan and dragon fruit was established in June, 2012. Vegetables were grown until successful harvest and the harvested produce was used for panel testing and distribution in January 2013. Machineries for postharvest handling systems were imported in November 2012. Setting the washing line for vegetables were finished and the system as run for testing in June 2013. New water tanks, pine lines, pump house and electricity were set up in October 2013.