• Title/Summary/Keyword: anchors

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Analysis of stability control and the adapted ways for building tunnel anchors and a down-passing tunnel

  • Xiaohan Zhou;Xinrong Liu;Yu Xiao;Ninghui Liang;Yangyang Yang;Yafeng Han;Zhongping Yang
    • Geomechanics and Engineering
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    • v.35 no.4
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    • pp.395-409
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    • 2023
  • Long-span suspension bridges have tunnel anchor systems to maintain stable cables. More investigations are required to determine how closely tunnel excavation beneath the tunnel anchor impacts the stability of the tunnel anchor. In order to investigate the impact of the adjacent tunnel's excavation on the stability of the tunnel anchor, a large-span suspension bridge tunnel anchor is utilised as an example in a three-dimensional numerical simulation approach. In order to explore the deformation control mechanism, orthogonal tests are employed to pinpoint the major impacting elements. The construction of an advanced pipe shed, strengthening the primary support. Moreover, according to the findings the grouting reinforcement of the surrounding rock, have a significant control effect on the settlement of the tunnel vault and plug body. However, reducing the lag distance of the secondary lining does not have such big influence. The greatest way to control tunnel vault settling is to use the grout reinforcement, which increases the bearing capacity and strength of the surrounding rock. This greatly minimizes the size of the tunnel excavation disturbance area. Advanced pipe shed can not only increase the surrounding rock's bearing capacity at the pipe shed, but can also prevent the tunnel vault from connecting with the disturbance area at the bottom of the anchorage tunnel, reduce the range of shear failure area outside the anchorage tunnel, and have the best impact on the plug body's settlement control.

Proposal and Performance Verification of a Seismic Adapter for Steel Brace Connections for In-plane Reinforcement of School Buildings (학교 건축물의 면내보강을 위한 강재브레이스 접합용 내진어댑터의 상세 제안 및 성능검증)

  • Seokjae Heo;Lan Chung;In-Kwan Paik
    • Journal of the Korea institute for structural maintenance and inspection
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    • v.27 no.6
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    • pp.162-171
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    • 2023
  • In this study, The details for a seismic adapter designed to easily connect concrete structures and reinforcement materials for the in-plane reinforcement of aged structures were proposed. Proposed seismic adapter was tested for performance using a dynamic simulation on a 2-story column-beam structure, scaled to half of the real size. The experimental results showed that the reinforced test specimens using the seismic adapter improved their energy dissipation capacity by 3.5 times compared to the non-reinforced specimens. It was confirmed that the seismic adapter experienced no damage within its general usage range, thus proving its effectiveness. Subsequently, upon loading until the limit of deformation (a deformation angle of 3.3%), it was observed that one of the M10 bolts connecting the adapter and the reinforcement at the lower part of the first floor broke. Considering this finding, when applying seismic retrofitting in real situations, emphasis should be placed on the design of the bolts and anchors connecting the seismic adapter. This aspect warrants further research for validation.

Active-Passive Ranging Method for Effective Positioning in Massive IoT Environment (대규모 IoT 환경에서의 효과적 측위를 위한 능동적-수동적 거리 추정 기법)

  • Byungsun Hwang;Seongwoo Lee;Kyoung-Hun Kim;Young-Ghyu Sun;Jin-Young Kim
    • The Journal of the Institute of Internet, Broadcasting and Communication
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    • v.24 no.3
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    • pp.41-47
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    • 2024
  • With the advancement and proliferation of the Internet of Things (IoT), a wide range of location-based services are being offered, and various ranging methods are being researched to meet the objectives of the required services. Conventional ranging methods involve the direct exchange of signals between tags and anchors to estimate distance, presenting a limitation in efficiently utilizing communication resources in large-scale IoT environments. To overcome these limitations, active-passive ranging methods have been proposed. However, there is a lack of theoretical convergence guarantees against clock drift errors and a detailed analysis of the characteristics of ranging estimation techniques, making it challenging to derive precise positioning results. In this paper, an improved active-passive ranging method that accounts for clock drift errors is proposed for precise positioning in large-scale IoT environments. The simulation results confirmed that the proposed active-passive ranging method can enhance distance estimation performance by up to 94.4% and 14.4%, respectively, compared to the existing active-passive ranging methods.

Behavior of simple precast high-strength concrete beams connected in the maximum bending moment zone using steel extended endplate connections

  • Magdy I. Salama;Jong Wan Hu;Ahmed Almaadawy;Ahmed Hamoda;Basem O. Rageh;Galal Elsamak
    • Steel and Composite Structures
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    • v.50 no.6
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    • pp.627-641
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    • 2024
  • This paper presents an experimental and numerical study to investigate the behavior of the precast segmental concrete beams (PSCBs) utilizing high-strength concrete (HSC) connected in the zone of the maximum bending moment using steel extended endplate connections (EECs). The experimental study consisted of five beams as follows: The first beam was the control beam for comparison, which was an unconnected one-piece beam made of HSC. The other four other beams consisted of two identical pieces of precast concrete. An important point to be noted is that at the end of each piece, a steel plate was used with a thickness of 10 mm. Moreover, this steel plate was welded to the lower and upper reinforcing bars of the beam. Furthermore, the steel plate was made to connect the two pieces using the technique of EECs. Several variables were taken in these four beams, whether from the shape of the connection or enhancing the behavior of the connection using the post-tensioning technique. EECs without stiffeners were used for some of the tested beams. The behavior of these connections was improved using stiffeners and shear bolts. To get accurate results, a comparison was made between the behaviors of the five beams. Another important point to be noted is that Abaqus and SAP2000 programs were used to investigate the behavior of PSCBs and to ensure the accuracy of the modeling process which showed a good agreement with the experimental results. Additionally, the simplified modeling using SAP2000 was able to model the nonlinear behavior of PSCBs connected using steel EECs. It was found that the steel pre-tensioned bolted EECs, reinforced with steel stiffeners and shear anchors, could be used to connect the precast HSC segmental beams via the internal pre-stressing technique.

Midterm outcomes of suture anchor fixation for displaced olecranon fractures

  • Michael J. Gutman;Jacob M. Kirsch;Jonathan Koa;Mohamad Y. Fares;Joseph A. Abboud
    • Clinics in Shoulder and Elbow
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    • v.27 no.1
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    • pp.39-44
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    • 2024
  • Background: Displaced olecranon fractures constitute a challenging problem for elbow surgeons. The purpose of this study is to evaluate the role of suture anchor fixation for treating patients with displaced olecranon fractures. Methods: A retrospective review was performed for all consecutive patients with displaced olecranon fractures treated with suture anchor fixation with at least 2 years of clinical follow-up. Surgical repair was performed acutely in all cases with nonmetallic suture anchors in a double-row configuration utilizing suture augmentation via the triceps tendon. Osseous union and perioperative complications were uniformly assessed. Results: Suture anchor fixation was performed on 17 patients with displaced olecranon fractures. Functional outcome scores were collected from 12 patients (70.6%). The mean age at the time of surgery was 65.6 years, and the mean follow-up was 5.6 years. Sixteen of 17 patients (94%) achieved osseous union in an acceptable position. No hardware-related complications or fixation failure occurred. Mean postoperative shortened disabilities of the arm, shoulder, and hand (QuickDASH) score was 3.8±6.9, and mean Oxford Elbow Score was 47.5±1.0, with nine patients (75%) achieving a perfect score. Conclusions: Suture anchor fixation of displaced olecranon fractures resulted in excellent midterm functional outcomes. Additionally, this technique resulted in high rates of osseous union without any hardware-related complications or fixation failures.

Arthroscopic Treatment of Metallic Suture Anchor Failures after Bankart Repair (Bankart 수술 후 발생한 금속 봉합 나사못 합병증의 관절경적 치료)

  • Shin, Sang-Jin;Jung, Jae-Hoon;Kim, Sung-Jae;Yoo, Jae-Doo
    • Journal of the Korean Arthroscopy Society
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    • v.10 no.1
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    • pp.70-76
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    • 2006
  • Purpose: This study presents 5 patients who had metallic anchor protrusion on glenoid after Bankart repair in anterior shoulder instability and reviewed the cause, clinical feature and arthroscopic removal technique. Method and Materials: 5 male with average age of 22 years (range 19 to 25 years) were included. 4 patients had arthroscopic Bankart repair and 1 patient had open repair for anterior shoulder instability. They had protruded metallic suture anchors on glenoid and the protruded suture anchors were removed arthroscopically using larger suture anchor empty inserter. Results: 4 patients had painful clicking sound with motion of abduction and external rotation and 1 patient showed shoulder instability. The ROM showed normal except mild degrees loss of external rotation. The position of protruded metallic anchor was 2, 3 and 5 O'clock in three patients and 4 O'clock in 2 patients. In 2 patients, the metallic suture anchor was malpositioned about 5mm off on the medial side from the anterior glenoid edge. All had Outerbrige classification Grade II-III chondral damage on humeral head and 1 patient showed glenoid cartilage destruction. None had shoulder instability after 2 years of follow-up. Constant score was 65 preoperatively and 89 postoperatively. ASES score was 67 preoperatively and 88 postoperatively. Conclusion: Symptoms of protruded suture anchor are not combined with instability. Most of symptoms were revealed from the rehabilitation period and confused with postoperative pain. Prompt diagnosis and early arthroscopic removal or impaction of protruded metallic suture anchor is recommended because of serious glenohumeral cartilage destruction. This is easy and simple and reproducible method to remove protruded metallic suture anchor arthroscopically.

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Temperature Compensation of Optical FBG Sensors Embedded Tendon for Long-term Monitoring of Tension Force of Ground Anchor (광섬유 센서 내장형 텐던을 이용한 그라운드 앵커의 장기 장력모니터링을 위한 온도보상)

  • Sung, Hyun-Jong;Kim, Young-Sang;Kim, Jae-Min;Park, Gui-Hyun
    • Journal of the Korean Geotechnical Society
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    • v.28 no.5
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    • pp.13-25
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    • 2012
  • Ground anchor method is one of the most popular reinforcing technology for slope in Korea. For the health monitoring of slope which is reinforced by permanent anchor for a long period, monitoring of the tension force of ground anchor is very important. However, since electromechanical sensors such as strain gauge and V/W type load cell are also subject to long-term risk as well as suffering from noise during long distance transmission and immunity to electromagnetic interference (EMI), optical FBG sensors embedded tendon was developed to measure strain of 7-wire strand by embedding FBG sensor into the center king cable of 7-wire strand. This FBG sensors embedded tendon has been successfully applied to measuring the short-term anchor force. But to adopt this tendon to long-term monitoring, temperature compensation of the FBG sensors embedded tendon should be done. In this paper, we described how to compensate the effect in compliance with the change of underground temperature during long-term tension force monitoring of ground anchors by using optical fiber sensors (FBG: Fiber Bragg Grating). The model test was carried out to determine the temperature sensitivity coefficient (${\beta}^{\prime}$) of FBG sensors embedded tendon. The determined temperature sensitivity coefficient ${\beta}^{\prime}=2.0{\times}10^{-5}/^{\circ}C$ was verified by comparing the ground temperatures predicted from the proposed sensor using ${\beta}^{\prime}$ with ground temperatures measured from ground thermometer. Finally, temperature compensations were carried out based on ${\beta}^{\prime}$ value and ground temperature measurement from KMA for the tension force monitoring results of tension type and compression type anchors, which had been installed more than 1 year before at the test site. Temperature compensated tension forces are compared with those measured from conventional load cell during the same measuring time. Test results show that determined temperature sensitivity coefficient (${\beta}^{\prime}$) of FBG sensors embedded tendon is valid and proposed temperature compensation method is also appropriate from the fact that the temperature compensated tension forces are not dependent on the change of ground temperature and are consistent with the tension forces measured from the conventional load cell.

Behavior and Capacity of Compression Lap Splice in Unconfined Concrete with Compressive Strength of 40 and 60 MPa (횡보강근이 없는 40, 60 MPa 콘크리트에서 철근 압축이음의 거동과 강도)

  • Chun, Sung-Chul;Lee, Sung-Ho;Oh, Bo-Hwan
    • Journal of the Korea Concrete Institute
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    • v.21 no.3
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    • pp.291-302
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    • 2009
  • A compression lap splice can be calculated longer than a tension lap splice in high strength concrete according to current design codes. New criteria for the compression lap splice including the effects of concrete strength are required for practical purpose of ultra-high strength concrete. Characteristics of compression lap splice have been extensively investigated and main parameters are derived. In addition, an experimental study has been conducted with column specimens in concrete strength of 40 and 60 MPa. The strength of the compression lap splice consists of bond and end bearing and two contributors are combined. Therefore, combined action of bond and end bearing should be assessed. Compared with tension splices, concrete strength significantly affects the strength of compression splices due to short splice length and existence of end bearing. Test results show that the splice strength can be evaluated to be proportional to square root of compressive strength of concrete. The stress states of concrete surrounding spliced bars govern the strengths of bond and end bearing. Because the axial stress of the concrete is relatively high, the splice strength is not dependent on clear spacing. End bearing strength is not affected by splice length and clear spacing and is expressed with a function of the square root of concrete strength. The failure mode of specimens is similar to side-face blowout of pullout test of anchors and the strength of end bearing can be evaluated using the equation of side-face blowout strength. Because the stresses developed by bond in compression splices are nearly identical to those in tension splices, strength increment of compression splices is attributed to end bearing only.

Pullout Characteristics of MC Anchor in Shale Layer (셰일지반에 설치된 MC앵커의 인발특성)

  • Lee, Bongjik;Kim, Josoon;Lee, Jongkyu
    • Journal of the Korean GEO-environmental Society
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    • v.13 no.1
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    • pp.53-61
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    • 2012
  • In this study, the research on MC anchor has been developed as composite type has done. MC anchor exerts bearing pressure on pre-bored hole where the end fixing device is expanded. Therefore, the uplift capacity is to be increased and it has the characteristics that the anchor body is not eliminated from the ground even if the grouting is not carried out properly. Furthermore, it reduces the loss of tension and raises the construction availability by inserting the reinforced bar as well as the anchor cable, while it can improve the long-term stability because the nail is expected to play the role when the loss of the anchor cable is occurred in a long-term. However, because the resistance mechanism of the compound anchor such as MC anchor is different from friction anchor, the estimation method of the uplift capacity by the frictional force of the ground and the grout is not proper. Particularly, in domestic cases, the problem to overestimate or underestimate the uplift capacity is expected because the design method considering the soil characteristics about the compound anchor has not been developed. Therefore, in this study, in order to evaluate the characteristics of MC anchor and a kind of compound anchor, we measured the uplift, the tension and the creep by nine anchors tests in shale ground that the fluctuation of the strength is great. In addition, we analyzed the test result comparing to the result of the general friction anchor and evaluated the characteristics of MC anchor movement to gather the results. As a result of the test, we found the effect that the uplift capacity is increased in shale ground comparing to the general friction anchor.

Numerical Analysis on Bearing Capacity of a Suction Bucket in Clay (수치해석을 이용한 점성토 지반에 설치된 버켓기초의 지지력 분석)

  • Le, Chi-Hung;Jeong, Jae-Uk;Kim, Sung-Ryul
    • Journal of the Korean Geotechnical Society
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    • v.27 no.10
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    • pp.25-33
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    • 2011
  • Suction buckets have been widely used for offshore structures such as anchors for floating facilities, and the foundations of offshore wind energy turbines. However, the design guidelines for suction buckets have not been clearly suggested. Therefore, this study performed the numerical analysis by using ABAQUS (2010) to evaluate bearing capacities and load-movement behaviors of the suction bucket in NC clay. For the numerical analysis, the depth ratio L/D (L=embedded length of skirt; D=diameter of a bucket) was varied from 0.25 to 1.0. The analysis results showed that the L/D ratio has a significant effect on the bearing capacity, and the vertical and horizontal capacities respectively increased by about 40% and 90%, when L/D ratio increased from 0.25 to 1.0. At the vertical loading, the bucket showed the similar failure mode with a deep foundation, so the shaft and toe resistances can be separately evaluated. At the horizontal loading, the bucket with L/D=O.25 showed the sliding failure mode and the bucket with $L/D{\geq}0.5$ showed the rotational failure mode.