• 제목/요약/키워드: Process variation of offset

검색결과 33건 처리시간 0.026초

PHS용 Automatic Tuning 방법을 이용한 Complex Filter (A CMOS Complex Filter with a New Automatic Tuning Method for PHS Application)

  • 고동현;박도진;정성규;부영건;이강윤
    • 대한전자공학회논문지SD
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    • 제44권10호
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    • pp.17-22
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    • 2007
  • 이 논문에서는 PHS용 new automatic tuning 방법을 가지는 baseband complex bandpass filter를 제안하였다. DC offset 문제를 해결하기 위한 Low_IF 구조로 CMOS로만 집적된 PHS용 수신기를 설계하였다. ACS 특성을 만족시키기 위해 3차 Chebyshev complex filter를 이용하여 baseband를 선택할 수 있는 filter를 설계하였다. 새롭게 제시한 Comer frequency tuning 방법은 공정의 변화에 보상을 해주는 방식이고, MOS 스위치에 의한 노이즈 레벨을 감소시킨다. 이 filter는 CMOS 0.35um 공정이며, 전력소모는 12mW였다.

퍼지모델을 이용한 비선형 공정의 적응 모델예측제어에 관한 연구 (A Study on an Adaptive Model Predictive Control for Nonlinear Processes using Fuzzy Model)

  • 박종진;우광방
    • 한국지능시스템학회논문지
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    • 제6권2호
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    • pp.97-105
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    • 1996
  • 본 논문에서는 퍼지모델을 이용한 비선형 공정의 적응모델예측제어가 제안된다. 모델예측제어의 저긍구조는 순환 퍼지모델링을 통해 구현된다. 사용된 퍼지모델의 후건부가 입, 출력 변수의 선형식이기 때문에, 전체 공정의 모델을 구하고 이를 이용하여 미래 공정출력을 구한 후 비용함수를 최로로하는 제어법칙은 일반형 예측제어(GPC)와 같은 형태가 된다. 제안된 적응 퍼지모델 예측제어는 퍼지모델이 가지는 본래적인 비선형성으로 인해 비선형공정을 우수한 성능으로 제어한다. 공정제어입력의 변화량을 출력값으로 하는 적응 퍼지모델 예측제어(AFMPC)인 경우, 상수의 기준입력에 대해 정상상태가 없고 매우 우수한 성능을 보인다. 제안된 제어구조의 특성 및 성은 비선형 공정의 모의 실험에 의해 검증한다.

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Print Mottle : Causes and Solutions from Paper Coating Industry Perspective

  • Lee, Hak-Lae
    • 펄프종이기술
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    • 제40권5호
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    • pp.60-69
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    • 2008
  • The principal reasons for applying a pigment coating to paper are to improve appearance and printability. The pigment coating provides a surface that is more uniform and more receptive to printing ink than are the uncoated fibers and, in turn, both facilitates the printing process and enhances the graphic reproduction. The improvement in print quality is readily apparent, especially in image areas or when multiple colors are involved. Although pigment coating of paper is to improve the printability, coated paper is not completely free from printing defects. Actually there are a number printing defects that are observed only with the coated papers. Among the printing defects that are commonly observed for coated papers, print mottle during multi-color offset printing is one of the most concerned defects, and it appears not only on solid tone area but also half dot print area. There are four main causes of print mottle ranging from printing inks, dampening solution, paper, and printing press or its operation. These indicates that almost every factors associated with lithographic printing can cause print mottle. Among these variation of paper quality influences most significantly on print mottle problems in multicolor offset printing, and this indicates that paper is most often to be blamed for its product deficiency as far as print mottle problems are concerned. Furthermore, most of the print mottle problems associated with paper is observed when coated papers are printed. Uncoated papers rarely show mottling problems. This indicates that print mottle is the most serious quality problems of coated paper products. Overcoming the print mottle is becoming more difficult because the operating speeds of coating and printing machines are increasing, coating weights are decreasing, and the demands on high-quality printing are increasing. Print mottle in offset printing is caused by (a) nonuniform back trap of ink caused by a nonuniform rate of ink drying, referred as "back trap mottle, and (b) nonuniform absorption of the dampening solution. Furthermore, both forms of print mottle have some relationship to the structure of the coated layer. The surest way of eliminating ink mottling is to eliminate unevenness in the base paper. Coating solutions, often easier to put into practice, should, however, be considered. In this paper the principal factors influencing print mottle of coated papers will be discussed. Especially the importance of base paper roughness, binder migration, even consolidation of coating layers, control of the drying rate, types of binders, etc. will be described.

LC공진기의 MSL길이에 따른 VCO 발진 특성 (VCO Oscillation Characteristics by Varying the Length of the MSL of LC Resonator)

  • 이동희;정진휘
    • 한국전기전자재료학회논문지
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    • 제15권5호
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    • pp.412-418
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    • 2002
  • In this paper, the authors present the simulation results and the experimental considerations on the effects of the effects of the VCO oscillation characteristics caused by varying the length of the MSL and the composition capacitance of LC resonation circuity. Simulation was accomplished by nonlinear RF circuit simulator for designing and analyzing the RF characteristis of VCO. The samples with 3 different MSL lengths of which the length is 140mil, 280mil and 560mil respectively were fabricated by screen printing process. The oscillation frequency of each sample(VCO) was tuned to UHF band (750MHz~900MHz) by varying the capacitance of LC resonator circuit. The experimental results showed that the values of phase noise were -82, -93, -97[dBc/Hz] at 50[kHz] offset frequency, the pushing figures were 114, 94, 318[kHz] at applied voltage of $3\pm0.15$[V] and the harmonics were -21, -16, -13[dBc] for MSL lengths of 140mil 280mil, 560mil respectively. The frequency and output variation width were 779~898[MHz], -36~-33[dBm] for MSL with 140mil length; 818~836[MHz], -27.19~27.06[dBm] for 280mil; 751.54~751.198[MHz], -33.44~-33.31[dBm] for 560mil.

$\mu$-설계법에 의한 저속 박용디젤기관의 속도제어기 설계 (A speed controller design for low speed marine diesel engine by the $\mu$-synthesis)

  • 정병건;양주호;김창화
    • Journal of Advanced Marine Engineering and Technology
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    • 제19권1호
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    • pp.60-70
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    • 1995
  • In the field of marine transportation the energy saving is one of the most important factors for profit. In order to reduce the fuel oil consumption the ship's propulsion efficiency must be increased as much as possible. The propulsion efficiency depends upon a combination of an engine and a propeller. The propeller has better efficiency as lower rotational speed. This situation led the engine manufacturers to design the engine that has lower speed, longer stroke and a small number of cylinders. Consequently the variation of rotational torque became larger than before because of the longer delay-time in the fuel oil injection process and an increased output per cylinder. As this new trends the conventional mechanical-hydrualic governors for engine speed control have been replaced by digital speed controllers which adopted the PID control or the optimal control algorithm. But these control algorithms have not enough robustness to suppress the variation of the delay-time and the parameter pertubation. In this paper we consider the delay-time and the perturbation of engine parameters as the modeling uncetainties. Next we design the controller which has zero offset in steady state engine speed, based on the two-degree-of-freedom control theory and $\mu$-synthesis. Thd validity of the controller is investigated through the response simulation. We use a personal computer and an analog computer as the digital controller and the engine (plant) part respectively. And, we certify that the designed controller maintains its performance even though the engine parameters may vary.

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대형 저속 디젤기관의 속도제어를 위한 로바스트 서보 제어기 설계 (Design of Robust Servo Controller for Large Size Low Speed Diesel Engines)

  • 정병건;양주호;변정환
    • 수산해양기술연구
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    • 제33권1호
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    • pp.46-58
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    • 1997
  • The energy saving is one of the most important factors for profit in marine transportation. In order to reduce the fuel oil consumtion the ship's propulsion efficiency must be increased as possible. The propulsion efficiency depends upon a combination of an engine and a propeller. The propeller has better efficiency as lower rotational speed. This situation led the engine manufacturers to design the engine that has low speed, long stroke and a small number of cylinders. Consequently, the variation of rotational torque became larger than before because of the longer delay-time in fuel oil injection process and an increased output per cylinder. As this new trends the conventional mechanical-hydrualic governors for engine speed control have been replaced by digital speed controllers which adopted the PID control or the optimal control algorithm. But these control algorithms have not enough robustness to suppress the variation of the delay-time and the parameter perturbation. In this paper we consider the delay-time and the perturbation of engine parameters as the modeling uncetainties. Next we design the robust servo controller which has zero offset in steady state engine speed, based on H sub($\infty$) control theory. The validity of the controller was investigated through the response simulation. We used a personal computer and an analog computer as the digital controller and the engine (plant) part respectively. And, we could certify that the designed controller maintains its robust servo performance even though the engine parameters may vary.

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A 1.8 V 40-MS/sec 10-bit 0.18-㎛ CMOS Pipelined ADC using a Bootstrapped Switch with Constant Resistance

  • Eo, Ji-Hun;Kim, Sang-Hun;Kim, Mun-Gyu;Jang, Young-Chan
    • Journal of information and communication convergence engineering
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    • 제10권1호
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    • pp.85-90
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    • 2012
  • A 40-MS/sec 10-bit pipelined analog to digital converter (ADC) with a 1.2 Vpp differential input signal is proposed. The implemented pipelined ADC consists of eight stages of 1.5 bit/stage, one stage of 2 bit/stage, a digital error correction block, band-gap reference circuit & reference driver, and clock generator. The 1.5 bit/stage consists of a sub-ADC, digital to analog (DAC), and gain stage, and the 2.0 bit/stage consists of only a 2-bit sub-ADC. A bootstrapped switch with a constant resistance is proposed to improve the linearity of the input switch. It reduces the maximum VGS variation of the conventional bootstrapped switch by 67%. The proposed bootstrapped switch is used in the first 1.5 bit/stage instead of a sample-hold amplifier (SHA). This results in the reduction of the hardware and power consumption. It also increases the input bandwidth and dynamic performance. A reference voltage for the ADC is driven by using an on-chip reference driver without an external reference. A digital error correction with a redundancy is also used to compensate for analog noise such as an input offset voltage of a comparator and a gain error of a gain stage. The proposed pipelined ADC is implemented by using a 0.18-${\mu}m$ 1- poly 5-metal CMOS process with a 1.8 V supply. The total area including a power decoupling capacitor and the power consumption are 0.95 $mm^2$ and 51.5 mW, respectively. The signal-to-noise and distortion ratio (SNDR) is 56.15 dB at the Nyquist frequency, resulting in an effective number of bits (ENOB) of 9.03 bits.

2단계 자동 트랜스컨덕턴스 조절 기능을 가진 저전력, 광대역 전압제어 발진기의 설계 (A Low Power, Wide Tuning Range VCO with Two-Step Negative-Gm Calibration Loop)

  • 김상우;박준성;부영건;허정;이강윤
    • 대한전자공학회논문지SD
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    • 제47권2호
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    • pp.87-93
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    • 2010
  • 이 글은 공정, 전압, 온도 변화를 극복하기 위한 2단계 자동 트랜스컨덕턴스 조절 기능을 가진 저전력, 광대역 전압제어발진기의 설계에 관한 논문이다. 광대역에서 전압제어발진기를 발진시키기 위해, 디지털 자동 트랜스컨덕턴스 조절 루프와 아날로그 자동 진폭조절 루프가 사용되었다. 전압제어발진기의 출력 스윙 크기에 따라 트랜지스터의 바디전압을 조절하는 기능도 저전력 구현을 위해 설계되었다. 소모전류는 1.2 V 공급전압에서 2 mA에서 6 mA까지 1 mA 단위로 조절된다. 전압제어발진기의 튜닝 범위는 2.35 GHz에서 5 GHz까지 2.65 GHz로써 72%이다. 위상잡음은 중심주파수 3.2 GHz를 기준으로 1MHz 떨어진 지점에서 -117 dBc/Hz 이다.

가스 하이드레이트 부존층의 구조파악을 위한 탄성파 AVO 분석 AVO모델링, AVO역산 (Seismic AVO Analysis, AVO Modeling, AVO Inversion for understanding the gas-hydrate structure)

  • 김건득;정부흥
    • 한국신재생에너지학회:학술대회논문집
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    • 한국신재생에너지학회 2005년도 춘계학술대회
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    • pp.643-646
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    • 2005
  • The gas hydrate exploration using seismic reflection data, the detection of BSR(Bottom Simulating Reflector) on the seismic section is the most important work flow because the BSR have been interpreted as being formed at the base of a gas hydrate zone. Usually, BSR has some dominant qualitative characteristics on seismic section i.e. Wavelet phase reversal compare to sea bottom signal, Parallel layer with sea bottom, Strong amplitude, Masking phenomenon above the BSR, Cross bedding with other geological layer. Even though a BSR can be selected on seismic section with these guidance, it is not enough to conform as being true BSR. Some other available methods for verifying the BSR with reliable analysis quantitatively i.e. Interval velocity analysis, AVO(Amplitude Variation with Offset)analysis etc. Usually, AVO analysis can be divided by three main parts. The first part is AVO analysis, the second is AVO modeling and the last is AVO inversion. AVO analysis is unique method for detecting the free gas zone on seismic section directly. Therefore it can be a kind of useful analysis method for discriminating true BSR, which might arise from an Possion ratio contrast between high velocity layer, partially hydrated sediment and low velocity layer, water saturated gas sediment. During the AVO interpretation, as the AVO response can be changed depend upon the water saturation ratio, it is confused to discriminate the AVO response of gas layer from dry layer. In that case, the AVO modeling is necessary to generate synthetic seismogram comparing with real data. It can be available to make conclusions from correspondence or lack of correspondence between the two seismograms. AVO inversion process is the method for driving a geological model by iterative operation that the result ing synthetic seismogram matches to real data seismogram wi thin some tolerance level. AVO inversion is a topic of current research and for now there is no general consensus on how the process should be done or even whether is valid for standard seismic data. Unfortunately, there are no well log data acquired from gas hydrate exploration area in Korea. Instead of that data, well log data and seismic data acquired from gas sand area located nearby the gas hydrate exploration area is used to AVO analysis, As the results of AVO modeling, type III AVO anomaly confirmed on the gas sand layer. The Castagna's equation constant value for estimating the S-wave velocity are evaluated as A=0.86190, B=-3845.14431 respectively and water saturation ratio is $50\%$. To calculate the reflection coefficient of synthetic seismogram, the Zoeppritz equation is used. For AVO inversion process, the dataset provided by Hampson-Rushell CO. is used.

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In-situ Synchrotron Radiation Photoemission Spectroscopy Study of Property Variation of Ta2O5 Film during the Atomic Layer Deposition

  • Lee, Seung Youb;Jeon, Cheolho;Kim, Seok Hwan;Lee, Jouhahn;Yun, Hyung Joong;Park, Soo Jeong;An, Ki-Seok;Park, Chong-Yun
    • 한국진공학회:학술대회논문집
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    • 한국진공학회 2014년도 제46회 동계 정기학술대회 초록집
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    • pp.362-362
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    • 2014
  • Atomic layer deposition (ALD) can be regarded as a special variation of the chemical vapor deposition method for reducing film thickness. ALD is based on sequential self-limiting reactions from the gas phase to produce thin films and over-layers in the nanometer scale with perfect conformality and process controllability. These characteristics make ALD an important film deposition technique for nanoelectronics. Tantalum pentoxide ($Ta_2O_5$) has a number of applications in optics and electronics due to its superior properties, such as thermal and chemical stability, high refractive index (>2.0), low absorption in near-UV to IR regions, and high-k. In particular, the dielectric constant of amorphous $Ta_2O_5$ is typically close to 25. Accordingly, $Ta_2O_5$ has been extensively studied in various electronics such as metal oxide semiconductor field-effect transistors (FET), organic FET, dynamic random access memories (RAM), resistance RAM, etc. In this experiment, the variations of chemical and interfacial state during the growth of $Ta_2O_5$ films on the Si substrate by ALD was investigated using in-situ synchrotron radiation photoemission spectroscopy. A newly synthesized liquid precursor $Ta(N^tBu)(dmamp)_2$ Me was used as the metal precursor, with Ar as a purging gas and $H_2O$ as the oxidant source. The core-level spectra of Si 2p, Ta 4f, and O 1s revealed that Ta suboxide and Si dioxide were formed at the initial stages of $Ta_2O_5$ growth. However, the Ta suboxide states almost disappeared as the ALD cycles progressed. Consequently, the $Ta^{5+}$ state, which corresponds with the stoichiometric $Ta_2O_5$, only appeared after 4.0 cycles. Additionally, tantalum silicide was not detected at the interfacial states between $Ta_2O_5$ and Si. The measured valence band offset value between $Ta_2O_5$ and the Si substrate was 3.08 eV after 2.5 cycles.

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