• Title/Summary/Keyword: Heat Exchange Devices

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Cause of and Solution for Damage to STS310S Tube in Heat Exchange Devices (열교환기 STS310S 튜브의 손상 원인 및 대책)

  • Kim, Jin Wook;Kim, Seon Hwa;Jeong, Jin Hyuk;Kim, Young Soo;Nam, Ki Woo
    • Transactions of the Korean Society of Mechanical Engineers A
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    • v.39 no.2
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    • pp.187-193
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    • 2015
  • The STS310S tube has excellent heat transfer ability and is widely used as the material for heat transfer tubes in heat exchange devices. Mixtures of gas and water flow inside the tube whereas hot flame flows outside it. In this environment, the material of the tube may undergo embrittlement, which can cause leakage. Cracks can propagate from the inside of the tube to its outside and result in brittle fracture. This study identified the cause of brittle fracture in the STS310S tube through experiments and discussion, and proposed solutions to prevent fracture.

Enhancement of heat exchange using On-chip engineered heat sinks

  • Chong, Yonuk
    • Progress in Superconductivity and Cryogenics
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    • v.19 no.4
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    • pp.18-21
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    • 2017
  • We report a method for improving heat exchange between cryo-cooled large-power-dissipation devices and liquid cryogen. Micro-machined monolithic heat sinks were fabricated on a high integration density superconducting Josephson device, and studied for their effect on cooling the device. The monolithic heat sink showed a significant enhancement of cooling capability, which markedly improved the device operation under large dc- and microwave power dissipation. The detailed mechanism of the enhancement still needs further modeling and experiments in order to optimize the design of the heat sink.

Aluminum and Plastic Heat Exchange Element : A Performance Comparison for Cooling of Telecommunication Cabinet (통신 함체 냉각용 알루미늄과 플라스틱 열교환 소자의 성능 비교)

  • Kim, Nae-Hyun
    • Korean Journal of Air-Conditioning and Refrigeration Engineering
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    • v.29 no.6
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    • pp.279-288
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    • 2017
  • Heat generation rate in a telecommunication cabinet increases due to the continued usage of mobile devices. Insufficient removal of heat intensifies the cabinet temperature, resulting in the malfunction of electronic devices. In this study, we assessed both aluminum and plastic heat exchangers used for cooling of the telecommunication cabinet, and compared the results against theoretical predictions. The aluminum heat exchanger was composed of counter flow parallel channels of 4.5 mm pitch, and the plastic heat exchangers were composed of cross flow triangular channels of 2.0 mm pitch. Samples were made by installing two plastic heat exchangers in both series and parallel. Results showed that the heat transfer rate was highest for the series cross flow heat exchanger, and was least for the aluminum heat exchanger. The temperature efficiency of the series cross flow heat exchanger was 59% greater than that of the aluminum heat exchanger, and was 4.3% greater than that of the parallel cross flow heat exchanger. In contrast, the pressure drop of the parallel cross flow heat exchanger was significantly lower than other samples. The heat exchange efficiency was also the largest for the parallel cross flow heat exchanger. The theoretical analysis predicted the temperature efficiency to be within 3.3%, and the pressure drop within 6.1%.

Heat Exchange Performance of Improved Heat Recovery System (개량형 열회수 시스템의 열교환 성능)

  • Suh, Won-Myung;Yoon, Yong-Cheol;Kwon, Jin-Keun
    • Journal of Bio-Environment Control
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    • v.12 no.3
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    • pp.107-113
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    • 2003
  • This study was carried out to improve the performance of pre-developed heat recovery devices attached to exhaust-gas flue connected to combustion chamber of greenhouse heating system. Four different units were compared in the aspect of heat recovery performance; A-, B-, and C-types are exactly the same with the old ones reported in previous studies. D-type newly developed in this experiment is mainly different with the old ones in its heat exchange area and tube thickness. But airflow direction(U-turn) and pipe arrangement are similar with previous three types. The results are summarized as follows; 1. System performances in the aspect of heat recovery efficiency were estimated as 42.2% for A-type, 40.6% for B-type, 54.4% for C-type, and 69.2% for D-type. 2. There was not significant improvement of heat recovering efficiency between two different airflow directions inside the heat exchange system. But considering current technical conditions, straight air flow pattern has more advantage than hair-pin How pattern (U-turn f1ow). 3. The main factors influencing on heat recovery efficiency were presumably verified to be the total area of heat exchange surface, the thickness of ail-flow pipes, and the convective heat transfer coefficient influenced by airflow velocity under the conditions of allowable pipe durability and safety. 4. Desirable blower capacity for each type of heat recovery units were significantly different to each other. Therefore, the optimum airflow capacity should be determined by considering in economic aspect of electricity required together with the optimum heat recovery performance of given heat recovery systems.

Heat Exchange Element Made of Plastic for Cooling of Telecommunication Cabinet (통신 함체 냉각용 플라스틱 재질의 열교환 소자)

  • Kim, Nae-Hyun
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.18 no.1
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    • pp.702-708
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    • 2017
  • The heat generation rate in a telecommunications cabinet keeps increasing due to the increased usage of mobile devices. Insufficient removal of the heat increases the cabinet temperature, which results in the malfunction of the electronic devices. In this study, tests were conducted on aluminum and plastic heat exchangers for cooling a telecommunications cabinet, and the results were compared with theoretical predictions. The aluminum heat exchanger comprised counter flow parallel channels with 4.5-mm pitch, and the plastic heat exchangers comprised cross or cross-counter flow triangular channels with 2.0-mm pitch. The volume of the cross flow heat exchanger was the same as that of the aluminum heat exchanger, and the volume of the cross-counter heat exchanger was 33% larger than that of the aluminum heat exchanger. The results show that the heat transfer rate is the highest for the cross-counter heat exchanger and lowest for the aluminum one. The temperature efficiency of the cross-counter heat exchanger was 56% higher than that of the aluminum one and 20% higher than that of the cross flow heat exchanger. The pressure drop of the cross-counter heat exchanger was approximately the same as that of the aluminum one. The heat exchange efficiency was the highest for the cross-counter heat exchanger and lowest for the cross flow heat exchanger. The theoretical analysis somewhat overestimated or underestimated the data.

Degradation of Ion-exchange Soda-lime Glasses Due to a Thermal Treatment (이온강화 소다라임 유리의 열처리에 따른 강화 풀림현상)

  • Hwang, Jonghee;Lim, Tae-Young;Lee, Mi Jai;Kim, Jin-Ho
    • Journal of the Korean Ceramic Society
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    • v.52 no.1
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    • pp.23-27
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    • 2015
  • Recently, the use of ion-exchange strengthened glass has increased sharply, as it is now used as the cover glass for smart phone devices. Therefore, many researchers are focusing on methods that can be used to strengthen ion-exchange glass. However, research on how the improved strength can be maintained under thermal environment of device manufacturing is still insufficient. We tested the degradation of the characteristics of ion-exchange soda-lime glass samples, including their surface compressive stress characteristics, the depth of the ion-exchange layer (DOL), flexural strength, hardness, and modulus of rupture (MOR) values. Degradation of the characteristics of the ion-exchange glass samples occurred when they were heat-treated at a temperature that exceeded $350^{\circ}C$.

Cooling Performance Characteristics of High-Performance Heat Pump with VI Cycle Using Re-Cooler (재냉기를 이용한 고성능 VI(Vapor Injection)사이클 열펌프의 냉방 성능특성에 관한 연구)

  • Lee, Jin-Kook;Choi, Kwang-Hwan
    • Journal of Advanced Marine Engineering and Technology
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    • v.39 no.6
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    • pp.592-598
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    • 2015
  • In this study, we experimentally investigate the performance characteristics of a high-performance summer-cooling heat pump for an R410A by applying an air-cooled-type vapor-injection (VI) cycle. The devices used for the experiment consist of a VI compressor, condenser, oil separator, plate-type heat-exchanger, economizer, evaporator, and re-cooler. The experimental conditions employed for the cooling performance were divided into three cycles. First, in Cycle A, we apply a VI cycle and with no heat exchange between the evaporator outlet refrigerant and the VI cycle suction refrigerant in the re-cooler. For Cycle B, there is heat exchange, and for Cycle C, there is neither a VI cycle nor heat exchange between the evaporator outlet refrigerant and the VI cycle suction refrigerant. From the analysis results, we observe that the performance was highest in the VI cycle with heat exchange between the evaporator outlet refrigerant and the VI cycle suction refrigerant (Cycle B), while it was lowest in Cycle C without application of the VI cycle. Moreover, the cooling coefficient of Performance ($COP_C$) averaged 3.5 in Cycle B, which was 8.6% higher than the corresponding value in Cycle A, and 33% higher than that in Cycle C.

The Effect of Cooling Efficiency on Fouling by EGR Cooler Internal Shape (EGR Cooler 내부 형상에 따른 Fouling이 냉각 성능에 미치는 영향)

  • Nam, Youn-Woo;Oh, Kwang-Chul;Lee, Chun-Hwan;Lee, Chun-Beom;Lee, Won-Nam
    • Transactions of the Korean Society of Automotive Engineers
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    • v.19 no.1
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    • pp.101-108
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    • 2011
  • Understanding the exhaust gas recirculation (EGR) cooler fouling in diesel engine is important factor in the durability characteristic of a EGR system. We develope a test rig and PM feeder using carbon black to examine the effect of fouling on EGR cooler devices those were consisted of flat and shell & tube type. The EGR cooler fouling process is a complex interaction involving heat exchanger shape, boundary condition, constitutes, chemistry and operating mode. As the soot deposited to EGR cooler, these formed a thin deposit layer that was less heat exchange than the fresh status of tube enclosing the exhaust gas, resulting in lower heat exchange effectiveness in both type coolers. But these deposits caused different results in pressure drop, it is increased in flat type, but decreased in Shell & tube type of EGR cooler. A cause was estimated from a change of the flow structure and a decrease of contact area as the EGR cooler fouling.

Development and Research of Thermal Management Equipment for Efficiency Enhancement of PEMFC Systems (PEMFC 시스템 효율 향상을 위한 열 관리 설비 개발 및 연구)

  • JAEHWAN KIM;JISEUNG LEE;INSEAK KANG;HYUNCHUL JU
    • Transactions of the Korean hydrogen and new energy society
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    • v.35 no.2
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    • pp.205-215
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    • 2024
  • This study introduced a direct contact heat exchanger to enhance the efficiency of polymer electrolyte membrane fuel cells (PEMFCs) systems. According to previous research, 28% of the operating costs of fuel cell systems are attributed to heat exchanger devices, prompting the design of a direct contact heat exchanger to address this issue. Optimal configurations were determined through computational fluid dynamics analysis and experimental device fabrication, and the enhanced heat exchange performance of the heat exchanger was experimentally confirmed. Through this, the contribution of the direct contact heat exchanger to the heat management and efficiency enhancement of PEMFC systems was established.

A Study on the Characteristics of Heating Performance of High-Performance Heat Pump with VI cycle using Re-Heater (재열기를 사용한 고성능 VI 사이클 열펌프의 난방 성능 특성에 관한 연구)

  • Lee, Jin-Kook;Choi, Kwang-Hwan
    • Journal of Power System Engineering
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    • v.19 no.4
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    • pp.69-75
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    • 2015
  • In this study, the characteristics of heating performance of a high-performance air-cooled heat pump with vapor-injection(VI) cycle using re-heater was investigated experimentally. Devices used in the experiment is consist of a VI compressor, condenser, oil separator, refrigerant (economizer outlet refrigerant) re-heater, economizer, evaporator. And R410A was used as a working fluid. The experiment was conducted with two cycles(cycles A and B) for investigating heating performance. In case of cycle B, heat exchange was conducted by re-heater between outlet refrigerant of compressor and suction refrigerant of the VI system(Fig.1, re-heater). But the re-heater was not used in case of cycle A. As a result of this experiment, discharge temperature of refrigerator in compressor was shown higher value, when the cycle B was conducted, because of the heat exchange between suction refrigerant of VI cycle and outlet refrigerant of compressor in the re-heater than cycle A that was not use re-heater. it means that liquid hammer and the decrement of heating performance can be decreased by using re-heater. Also, Heating coefficient of performance(COPh) was shown about 2.98 in Cycle B which was 4% higher than Cycle A and from these results, It was confirmed that the improvement of the heating performance of heat pump with VI cycle can be achieved by applying re-heater.