• Title/Summary/Keyword: Combustor Performance Test

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Combustion Performance Tests of High Pressure Subscale Liquid Rocket Combustors (고압 축소형 연소기의 연소 성능 시험)

  • Kim, Jong-Gyu;Lee, Kwang-Jin;Seo, Seong-Hyeon;Lim, Byoung-Jik;Ahn, Kyu-Bok;Han, Yeoung-Min;Choi, Hwan-Seok
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2007.04a
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    • pp.128-134
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    • 2007
  • Combustion performance and characteristics of high-pressure subscale liquid rocket combustors were studied experimentally. Four different models of combustor were considered in this paper. The high-pressure subscale combustor is composed of the mixing head, the water cooling cylinder and the nozzle. One model of the combustors employed regenerative cooling combustor in that the kerosene used for the chamber cooling is burned. This combustor was damaged due to a high frequency combustion instability occurred during a firing test. The results of the firing tests, comparison of performance, and characteristics of static and dynamic pressures of the combustors are described.

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Secondary Flow Characteristics in a Liquid Ramjet Combustor Using Stereoscopic PIV (Stereoscopic PIV 속도장 측정기법을 이용한 액체 램제트 연소기에서의 2차 재순환 유동장 특성)

  • Kim S. J.;Sohn C. H.
    • Journal of the Korean Society of Visualization
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    • v.3 no.1
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    • pp.58-62
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    • 2005
  • Flow characteristics at secondary recirculation zone in a liquid fuel ramjet combustor were investigated using CFD and Stereoscopic PIV method. The combustors have two rectangular inlets that form 90 degree each other. Three guide vanes were installed in each rectangular inlet to improve the flow stability. The tested angle of the air intakes was 60 degree. The experiments were performed in the water tunnel test with the same Reynolds number in the case of Mach 0.3 at inlet. The computational and experimental results showed that the secondary recirculation flow occurred at the front junction of inlet main stream and combustor chamber. The size of secondary recirculation regions are increased with approaching closer to the center of the combustor. Since the performance of combustor is closely dependent not only on the main recirculation in the dome region but also on the secondary recirculation flow in a junction region, the optimal angle of the air intakes should be considered the recirculation size as frame holder.

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Flow Characteristics of secondary recirculation region for using Stereoscopic PIV in a Liquid Fuel Ramjet Combustor (Stereoscopic PIV 속도장 측정기법을 이용한 액체 램제트 연소기에서의 2차 재순환 유동장 측정)

  • Kim S. J.;Choi J. H.;Park C. W.;Sohn C. h.
    • 한국가시화정보학회:학술대회논문집
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    • 2003.11a
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    • pp.115-120
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    • 2003
  • Flow characteristics at secondary recirculation zone in a liquid fuel ramjet combustor are investigated using CFD and 3-D Stereoscopic PIV method. The combustors have two rectangular inlets that form 90 degree each other. Three guide vanes were installed in each rectangular inlet to improve the flow stability. The tested angle of the air intakes was 60 degree. The experiments were performed in the water tunnel test with the same Reynolds number in the case of Mach0.3 at inlet. Both computational and experimental results showed the secondary recirculation flow occurred at the front junction of inlet main stream and combustor chamber. The size of secondary recirculation region increased with upon closer center of axial combustor. Since the performance of combustor depends on not only the main recirculation in the dome region but also the secondary recirculation flow in a junction region, the optimal angle of the air intakes should consider the recirculation size as frame holder.

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The Design and Hot-firing tests of a Water-cooled High Pressure Sub-scale Combustor (물냉각 고압 축소형 연소기의 설계 및 연소시험)

  • Lee, Kwang-Jin;Kim, Jong-Gyu;Lim, Byoung-Jik;Ahn, Kyu-Bok;Seo, Seong-Hyeon;Han, Yeoung-Min;Choi, Hwan-Seok
    • Journal of the Korean Society of Propulsion Engineers
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    • v.11 no.3
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    • pp.1-6
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    • 2007
  • A 3-tonf-class high pressure sub-scale combustor was designed and manufactured to study the performance improvement of combustor. The combustor consists of a combustion chamber with film cooling, thermal barrier coating and water cooling channels to prevent thermal demage of the hardware and an injector head with 37 coaxial swirl injectors. Hot-firing tests were carried out at the design point with varying flow rate for film cooling. The test result revealed that the increase of film cooling flow rate decreases the combustion performance, but in the cases of similar film cooling flow rates, the combustion performance is dependent on the mixture ratio of main injector excluding the film cooling flow rate.

Test and Evaluation for the Mixing Quality in the Premixer of DLE Combustor (DLE(Dry Low Emission) 연소기 예혼합기의 혼합성능 예측에 대한 시험 평가)

  • 최장수;박동준;우유철
    • Journal of the Korean Society of Propulsion Engineers
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    • v.2 no.2
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    • pp.99-107
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    • 1998
  • A test on venturi-type premixer of ASE120 engine combustor has been performed to evaluate its mixing performance. Cold air was supplied into the premixer through the fuel nozzle and mixed with the hot air from the compressor exit. The measured temperature of the mixed air was used to evaluate the mixedness. DOE(Design of Experiment) technique was utilized to make a test matrix of variables and to determine the optimum combination of variables, which was verified through a confirmation test.

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An Experimental Assessment of Combustion Stability of Coaxial Swirl Injectors and an Impinging Injector through Simulating Combustion Test (상압기상연소시험을 통한 동축형 스월 분사기와 충돌형 분사기의 연소 안정성 평가)

  • Park, Junhyeong;Kim, Hongjip
    • Journal of the Korean Society of Combustion
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    • v.22 no.1
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    • pp.46-52
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    • 2017
  • High-frequency combustion instabilities may occur during the development of feasible engine combustors. These instabilities can result in irreparable damages to the wall of combustors or the degradation of engine performance. So, it is essential to identify injectors that have high stability characteristics during the early stages of development. The objective of present study was to assess the stability of coaxial injectors and an impinging injector with different recess lengths in order to develop stable injectors optimally. Stability margin was evaluated based on the distance from operating condition to the unstable regions. A simulating combustion test method was used to analyze the stability of injectors. A small-scale combustion chamber was designed to simulate the first tangential acoustic mode of the actual combustor. Gaseous oxygen and a mixture of methane and propane were used as simulant propellants to satisfy their flow similarity to the actual propellants of a combustor in a liquid rocket combustor. The results indicated that injectors having small recess lengths showed relatively large combustion stability margins. For the injectors of large recess lengths, instability regions with large and super-large amplitude oscillations were observed. Thus, injector with shorter recess lengths had a higher stability than that of longer one due to the different mixing processes.

Combustion Test of Regenerative Cooling Combustor for Liquid Rocket Engine (실물형 재생냉각 액체로켓엔진 연소기(확대비3.5) 연소시험)

  • Yang, Seung-Ho;Kim, Hee-Tea;Kang, Dong-Hyuk;Ahn, Kyu-Bok;Seo, Seong-Hyeon;Han, Yeoung-Min;Choi, Hwan-Seok
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2007.11a
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    • pp.125-130
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    • 2007
  • Firing tests have been performed for a 30 tonf-class full-scale regeneratively cooled combustion chamber. It was the first model which has welded construction of the injection head and the combustion chamber. A number of firing tests have been performed to evaluate combustion efficiency, regenerative cooling performance and durability of the combustor. This paper describes the results of firing tests performed at the design and off-design conditions which correspond to the chamber pressure of 60 bar, 68 bar respectively and the O/F ratio of 2.5 and 2.8 respectively. The data at each test condition have provided successful results in terms of combustion performance, combustion stability and durability. The tests are considered to be quite meaningful in the sense that the technologies for kerosene regeneratively cooled combustion chamber are successfully proven.

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Development of Test Facility for Micro Gas Turbine (마이크로 가스터빈 시험 장치 개발)

  • Lim, Hyung-Soo;Choi, Bum-Seog;Park, Moo-Ryong;Hwang, Soon-Chan;Park, Jun-Young;Seo, Jeongmin;Bang, Je-Sung;Lim, Young-Chul;Oh, In-Kyun;Kim, Byung Ok;Cho, Ju Hyeong
    • The KSFM Journal of Fluid Machinery
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    • v.18 no.5
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    • pp.42-48
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    • 2015
  • To improve the core technology of the micro gas turbine, the performance test facility was developed. This paper is focusing on the explanation of the characteristics of micro gas turbine and its assist devices. Major part of micro gas turbine were radial type of compressor, annular type of combustor, radial type of turbine, thrust foil bearing, radial foil bearing and generator. The assist devices were consist of exhaust duct, inverter, data acquisition system, load bank and test cell. Before building up the test facility, the component test was previously conducted to confirm the component performance. After the test facility was prepared, the motoring test was conducted to investigate the rotor dynamic characteristics of the micro gas turbine. Also, the part load performance test was performed. With a developed micro gas turbine test facility, the improved core technology about the micro gas turbine can be suggested to the related industries.

Fabrication and Performance Test of MEMS Catalytic Combustors Using Photosensitive Glass Wafer (감광유리를 이용한 MEMS 촉매 연소기의 제작 및 성능 평가)

  • Jin, Jung-Kun;Kwon, Se-Jin
    • Transactions of the Korean Society of Mechanical Engineers A
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    • v.33 no.3
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    • pp.237-242
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    • 2009
  • MEMS catalytic combustors were fabricated to use in micro-power sources as a heat source. The combustor was fabricated by photolithography and anisotropic wet etching of photosensitive glass wafers. Two different catalyst loading methods were used to complete the fabrication of the combustors. For thin film type, the $Al_2O_3$ was washcoated on the surface of the combustion chamber as a catalyst support, and for packed-bed type, ceramic foam was inserted after Pt was coated. The volume of the combustors was 1.8 $cm^3$ and 16W of heat was generated using the fabricated combustors with hydrogen. The energy density of combustor was about 8.9 W/$cm^3$.

An Experimental Study on Low Nox Combustor Performance at High Pressure and Temperature for 20kW Class Microturbines (20kW급 마이크로터빈용 저공해 연소기의 고압고온 성능실험 연구)

  • Yoon, JeongJung;Oh, Jongsik;Lee, Heonseok
    • 유체기계공업학회:학술대회논문집
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    • 2002.12a
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    • pp.183-190
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    • 2002
  • In order to reduce NOx emissions in the 20kw class microturbines under development, the low NOx characteristics, as being an application to the lean premixed combustion technology, have been investigated. The study has been conducted at the conditions of high temperature and pressure. Air from a compressor with the temperature of 500K to 650K and the pressure of 0.3bar gauge to 0.7bar gauge, was supplied to the combustor through an air preheat-treatment. Sampling exhaust gases were measured at the immediate exit of the combustor. for the effect of temperature on NO and CO emissions. though NOx was increased, CO was decreased with increasing inlet air temperature. With increasing inlet air pressure, NOx and CO were increased also. NOx was decreased, but CO was increased with increasing inlet air mass flow rate. The test has been performed on the equivalent ratios of 0.10 to 0.25 in a lean region. NOx was increased with increasing equivalent ratios, but CO was decreased as an influence of flame temperature. In the very lean region of the equivalent ratio below 0.12, CO was increased suddenly, due to instability. As the results of this study, NOx and CO are found to be reduced to the similar level at the same time when operated at optimal conditions.

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