• Title/Summary/Keyword: Combustion Stability Test

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A Study of mixing characteristics of unlike impinging streams doublet injector (이유체 충돌 분사기의 혼합특성에 관한 연구)

  • Han, Jae-Seob;Kim, Seon-Jin;Kim, Yoo
    • Journal of the Korean Society of Propulsion Engineers
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    • v.4 no.4
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    • pp.36-41
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    • 2000
  • Mixing characteristics of unlike impinging streams double injectors have a great effect on combustion stability and combustion efficiency for liquid rocket engine. In this study a cold test was carried out, using water and TCE as simulants, in order to examine the effect of design parameters such as impingement angle, orifice diameter ratio and momentum ratio on the mass distribution and mixing quality.

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Verification and Analysis of Characteristics of Mechanical Pulsation for Combustion Stability Study in a Model Chamber (모형 연소기의 연소 불안정성 연구용 섭동 장치의 기능 검증 및 분석)

  • Min, Yong-Ho;Sohn, Chae-Hoon
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2012.05a
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    • pp.28-30
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    • 2012
  • A mechanical pulsator is manufactured for study of combustion instabilities in a model chamber with impinging-jet injectors. Artificial disturbance is generated by the device and thereby, artificial instability can be examined experimentally. A sample F(fuel)-O(dxidizer)-O-F impinging-jet injector is adopted for the test. The model chamber was designed based on the methodologies proposed in the previous work regarding geometrical dimensions and operating conditions. Pressure fluctuation data, which is obtained from the dynamic pressure transducers installed in combustion chamber, is analyzed.

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Performance and Emission Characteristics of a Compression Ignition Engine Operated with LPG and Cetane Enhancing Additives (LPG/DTBP 혼합연료를 사용하는 압축착화 엔진의 부분부하 성능 및 배기특성에 관한 연구)

  • Lee, Seok-Hwan;Oh, Seung-Mook;Choi, Young;Kang, Kern-Yong
    • Transactions of the Korean Society of Automotive Engineers
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    • v.18 no.6
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    • pp.105-113
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    • 2010
  • In this study, a feasibility test of liquid petroleum gas (LPG) compression ignition (CI) engine has been carried out to study the effectiveness of cetane enhancing additive: Di-tertiary-butyl peroxide (DTBP). Performance and emissions characteristics of a CI engine fuelled with DTBP blended LPG fuel were examined. Also, the effect of EGR (exhaust gas recirculation) on the combustion and emissions characteristics has been investigated. Results showed that stable engine operation over a wide range of the engine loads was possible. Exhaust emissions measurements showed that hydrocarbon were decreased with the blended fuel at enhancing cetane number. Furthermore, the combustion stability of LPG with a cetane number improver was equivalent to that of commercial Diesel fuel. Increasing the EGR rate leads to deteriorate the IMEP (indicated mean effective pressure) and increase the ignition delay. It was found that the exhaust emissions with the EGR resulted in a very large reduction in nitrogen oxides at the expense of higher THC and CO emissions. Considering the results of engine performance and exhaust emissions, LPG blended fuel of enhancing cetane number could be used as an alternative fuel for diesel in a CI engine.

Development of 30-Tonf LOx/Kerosene Rocket Engine Combustion Devices(II) - Gas Generator (추력 30톤급 액체산소/케로신 로켓엔진 연소장치 개발(II)-가스발생기)

  • Choi, Hwan-Seok;Seo, Seong-Hyeon;Kim, Young-Mog;Cho, Gwang-Rae
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.37 no.10
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    • pp.1038-1047
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    • 2009
  • The development process of a gas generator for a 30-tonf pump-fed space liquid rocket engine is described. Starting from the development of an injector, followed by subscale and full-scale test specimens, the development of LOx/kerosene fuel-rich gas generator has been concluded successfully. Various analytical methods have been utilized in the course of design and the performance requirements have been verified experimentally through ignition tests, combustion performance and stability assessment tests and duration tests. The gas generator has proven its workability and stability within a defined operation window of varying chamber pressure and mixture ratio and demonstrated compliance to the performance and life time requirements.

Combustion Characteristics and Thermal Properties for Wood Flour-High Density Polyethylene Composites (목분-고밀도폴리에틸렌 복합체의 연소성 및 열적특성)

  • Shin, Baeg-Woo;Chung, Kook-Sam
    • Fire Science and Engineering
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    • v.26 no.1
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    • pp.89-95
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    • 2012
  • In this study, we were manufactured wood flour-HDPE composites by modular co-rotating twin screw extruder with L/D ratio of 42. We was measured cone calorimeter test and thermogravimetric analysis (TGA) to find the combustion characteristics and thermal properties for wood flour-HDPE composites. We then evaluated the effect of three additive-type flame retardants on fire resistance performance. The cone calorimeter test showed that the heat release rate (HRR) of untreated composites was the highest Peak HRR ($446.6kW/m^2$) as well as Mean HRR ($185.5kW/m^2$). From the TGA, it was shown that composites added flame retardants began early thermal decomposition and improved thermal stability.

Design and Experimental Verification of Uni-Injector Using Gas Methane and Lox as Propellants (가스메탄/액체산소를 추진제로 하는 단일 인젝터 설계 및 실험적 검증)

  • Jeon, Jun Su;Min, Ji Hong;Jang, Ji Hun;Ko, Young Sung;Kim, Sun Jin
    • Transactions of the Korean Society of Mechanical Engineers B
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    • v.37 no.3
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    • pp.275-283
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    • 2013
  • An injector that uses methane gas ($CH_4$) and liquid oxygen ($LO_x$) as propellants was designed to verify the combustion characteristics of an engine that uses methane, which is one of the next-generation propellants. A swirl/shear coaxial-type injector was used, and flow analysis was performed using Fluent to determine the main design parameters of the injector. A hydraulic test was performed to understand the atomization and spray pattern characteristics of the injector. Next, a combustion test was performed at the design point to understand the ignition and combustion stability. Additional combustion tests were performed according to the O/F ratio to investigate the combustion characteristics and stabilities using the characteristic exhaust velocity ($C^*$) and fluctuation of the chamber pressure. The experimental results showed that the combustion efficiency was greater than 90%, and the pressure fluctuation was lower than 2% under all conditions.

Effect of Ethanol-gasoline Blending Ratio on Lean Combustion and Exhaust Emissions Characteristics in a SI Engine Fueled with Bioethanol (바이오에탄올 SI 엔진에서 에탄올-가솔린 연료 혼합비율에 따른 희박연소 및 배기 특성)

  • Yoon, Seung-Hyun;Kim, Dae-Sung;Lee, Chang-Sik
    • Transactions of the Korean Society of Automotive Engineers
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    • v.19 no.1
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    • pp.82-88
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    • 2011
  • Lean combustion and exhaust emission characteristics in a ethanol fueled spark-ignited engine according to ethanol-gasoline fuel blending ratio were investigated. The test engine was $1591cm^3$ and 10.5 of compression ratio SI engine with 4 cylinders. In addition, lambda sensor system was connected with universal ECU to control the lambda value which is varied from 1.0 to 1.5. The engine performance and lean combustion characteristics such as brake torque, cylinder pressure and rate of heat release were investigated according to ethanol-gasoline fuel blending ratio. Furthermore, the exhaust emissions such as carbon monoxide (CO), unburned hydrocarbon (HC), nitrogen oxides ($NO_x$) and carbon dioxide ($CO_2$) were measured by emission analyzers. The results showed that the brake torque, cylinder pressure and the stability of engine operation were increased as ethanol blending ratio is increased. Brake specific fuel consumption (BSFC) was increased in higher ethanol blending ratio while brake specific energy consumption (BSEC) was decreased in higher ethanol blending ratio. The exhaust emissions were decreased as ethanol blending ratio is increased under overall experimental conditions, however, some specific exhaust emission characteristics were mainly influenced by lambda value and ethanol-gasoline fuel blending ratio.

Analysis on Initial Stability Test Results of Underwater Vehicle Using the HR Propulsion System (HR추진기관을 이용한 수중운동체의 초기안정성 시험 결과 분석)

  • Hwang, Heeseong;Kim, Hakseong;You, Youngjoon
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2017.05a
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    • pp.1142-1143
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    • 2017
  • In this paper, Underwater propulsion test of SWASH(Small Waterplane Area Single Hull) type underwater vehicle with hybrid rocket system is performed. Watertight structure is applied to prevent a combustion chamber from water, and the control logic is constructed by setting the watertight ignition sequence. As a results, It is confirmed that the ignition is stable in water, and the propulsion system works well along the configured control sequence.

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Part Load Performance Characteristics according to Port Masking (포트 마스킹에 따른 엔진 부분부하 성능 특성)

  • Kim, Hyeong-Sig;Kim, In-Ok;Park, Chan-Jun;Ohm, In-Yong
    • Transactions of the Korean Society of Automotive Engineers
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    • v.19 no.2
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    • pp.42-49
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    • 2011
  • To expand lean misfire limit and improve combustion stability, the effects of port masking were estimated to secure basic data for applying the mechanism to SI engine instead of asymmetrical port and port throttling devises. For this purpose, various shapes and ratios of masking plates were mounted between port and manifold. The masking effects were evaluated by mixture response test under various load and speed conditions. The results showed that lean misfire limits were expended and fast combustion was observed for all masking shapes and ratios, especially, the effect of diagonal 1/4 masking was remarkable. In conclusion, the port masking method could be easily applied to engine without redesign of port for improving part load performance.

Analysis of Pressure Fluctuations in 1/2.5-scale Thrust Chamber for 75 tonf-class Engine (75톤급 엔진 1/2.5-scale 연소기 압력 섭동 분석)

  • Ahn, Kyu-Bok;Kang, Dong-Hyuk;Kim, Mun-Ki;Lim, Byoung-Jik;Kim, Jong-Gyu;Lee, Kwang-Jin;Seo, Seong-Hyeon;Han, Yeoung-Min;Choi, Hwan-Seok
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2010.05a
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    • pp.5-9
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    • 2010
  • In the paper, the dynamic characteristics obtained from hot-firing tests of 1/2.5-scale thrust chamber for 75 tonf-class liquid rocket engine were described. To investigate the dynamic characteristics by engine start transient period and chamber pressure variation, hot-firing tests were performed in the chamber pressures of 30 bar and 60 bar. According to these variations, combustion stability in the combustion chamber was examined.

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