• Title/Summary/Keyword: volume.

Search Result 27,760, Processing Time 0.058 seconds

Flow Resistance and Modeling Rule of Fishing Nets -1. Analysis of Flow Resistance and Its Examination by Data on Plane Nettings- (그물어구의 유수저항과 근형수칙 -1. 유수저항의 해석 및 평면 그물감의 자료에 의한 검토-)

  • KIM Dae-An
    • Korean Journal of Fisheries and Aquatic Sciences
    • /
    • v.28 no.2
    • /
    • pp.183-193
    • /
    • 1995
  • Assuming that fishing nets are porous structures to suck water into their mouth and then filtrate water out of them, the flow resistance N of nets with wall area S under the velicity v was taken by $R=kSv^2$, and the coefficient k was derived as $$k=c\;Re^{-m}(\frac{S_n}{S_m})n(\frac{S_n}{S})$$ where $R_e$ is the Reynolds' number, $S_m$ the area of net mouth, $S_n$ the total area of net projected to the plane perpendicular to the water flow. Then, the propriety of the above equation and the values of c, m and n were investigated by the experimental results on plane nettings carried out hitherto. The value of c and m were fixed respectively by $240(kg\cdot sec^2/m^4)$ and 0.1 when the representative size on $R_e$ was taken by the ratio k of the volume of bars to the area of meshes, i. e., $$\lambda={\frac{\pi\;d^2}{21\;sin\;2\varphi}$$ where d is the diameter of bars, 21 the mesh size, and 2n the angle between two adjacent bars. The value of n was larger than 1.0 as 1.2 because the wakes occurring at the knots and bars increased the resistance by obstructing the filtration of water through the meshes. In case in which the influence of $R_e$ was negligible, the value of $cR_e\;^{-m}$ became a constant distinguished by the regions of the attack angle $ \theta$ of nettings to the water flow, i. e., 100$(kg\cdot sec^2/m^4)\;in\;45^{\circ}<\theta \leq90^{\circ}\;and\;100(S_m/S)^{0.6}\;(kg\cdot sec^2/m^4)\;in\;0^{\circ}<\theta \leq45^{\circ}$. Thus, the coefficient $k(kg\cdot sec^2/m^4)$ of plane nettings could be obtained by utilizing the above values with $S_m\;and\;S_n$ given respectively by $$S_m=S\;sin\theta$$ and $$S_n=\frac{d}{I}\;\cdot\;\frac{\sqrt{1-cos^2\varphi cos^2\theta}} {sin\varphi\;cos\varphi} \cdot S$$ But, on the occasion of $\theta=0^{\circ}$ k was decided by the roughness of netting surface and so expressed as $$k=9(\frac{d}{I\;cos\varphi})^{0.8}$$ In these results, however, the values of c and m were regarded to be not sufficiently exact because they were obtained from insufficient data and the actual nets had no use for k at $\theta=0^{\circ}$. Therefore, the exact expression of $k(kg\cdotsec^2/m^4)$, for actual nets could De made in the case of no influence of $R_e$ as follows; $$k=100(\frac{S_n}{S_m})^{1.2}\;(\frac{S_m}{S})\;.\;for\;45^{\circ}<\theta \leq90^{\circ}$$, $$k=100(\frac{S_n}{S_m})^{1.2}\;(\frac{S_m}{S})^{1.6}\;.\;for\;0^{\circ}<\theta \leq45^{\circ}$$

  • PDF

Synthesis of a Dopamine Transporter Imaging Agent, N-(3-[$^{18}F$]fluoropropyl)-$2{\beta}$-carbomethoxy-$3{\beta}$-(4-iodophenyl)nortropane (도파민운반체 방사성추적자 N-(3-[$^{18}F$Fluoropropyl)-$2{\beta}$-carbomethoxy-$3{\beta}$-(4-iodophenyl)nortropane의 합성)

  • Choe, Yearn-Seong;Oh, Seung-Jun;Chi, Dae-Yoon;Kim, Sang-Eun;Choi, Yong;Lee, Kyung-Han;Kim, Byung-Tae
    • The Korean Journal of Nuclear Medicine
    • /
    • v.33 no.3
    • /
    • pp.298-305
    • /
    • 1999
  • Purpose: N-(3-[$^{18}F$]Fluoropropyl)-$2{\beta}$-carbomethoxy-$3{\beta}$-(4-iodophenyl)nortropane [$^{18}F$]FP-CIT) has been shown to be very useful for imaging the dopamine transporter. However, synthesis of this radiotracer is somewhat troublesome. In this study, we used a new method for the preparation of [$^{18}F$]FP-CIT to increase radiochemical yield and effective specific activity. Materials and Methods: [$^{18}F$]FP-CIT was prepared by N-alkylation of nor-${\beta}$-CIT (2 mg) with 3-bromo-1-[$^{18}F$]fluoropropane in the presence of $Et_3N$ (5-6 drops of $DMF/CH_3CN$, $140^{\circ}C$, 20 min). 3-Bromo-1-[$^{18}F$]fluoropropane was synthesized from $5{\mu}L$ of 3-bromo-1-trifluoromethanesulfonyloxypropane (3-bromopropyl-1-triflate) and $nBu_4N^{18}F$ at $80^{\circ}C$. The final compound was purified by reverse phase HPLC and formulated in 13% ethanol in saline. Results: 3-Bromo-1-[$^{18}F$]fluoropropane was obtained from 3-bromopropyl-1-triflate and $nBu_4N^{18}F$ in 77-80% yield. N-Alkylation of nor-${\beta}$-CIT with 3-bromo-1-[$^{18}F$]fluoropropane was carried out at $140^{\circ}C$ using acetonitrile containing a small volume of DMF as the solvents. The overall yield of [$^{18}F$]FP-CIT was 5-10% (decay-corrected) with a radiochemical purity higher than 99% and effective specific activity higher than the one reported in the literature based on their HPLC data. The final [$^{18}F$]FP-CIT solution had the optimal pH (7.0) and it was pyrogen-free. Conclusion: In this study, 3-bromopropyl-1-triflate was used as the precursor for the [$^{18}F$]fluorination reaction and new conditions were developed for purification of [$^{18}F$]FP-CIT by HPLC. We established this new method for the preparation of [$^{18}F$]FP-CIT, which gave high effective specific activity and relatively good yield.

  • PDF

The Comparative Study of on Pump CABG during Pulsatile $(T-PLS^{TM})$ and Nonpulsatile $(Bio-pump^{TM})$ Perfusion (관상동맥우회술 시 사용된 박동성펌프$(T-PLS^{TM})$와 비박동성펌프$(Bio-pump^{TM})$의 비교연구)

  • Park Young-Woo;Her Keun;Lim Jae-Ung;Shin Hwa-Kyun;Won Yong-Soon
    • Journal of Chest Surgery
    • /
    • v.39 no.5 s.262
    • /
    • pp.354-358
    • /
    • 2006
  • Background: Pulsatile pumps for extracorporeal circulation have been known to be better for tissue perfusion than non-pulsatile pumps but be detrimental to blood corpuscles. This study is intended to examine the risks and benefits of $T-PLS^{TM}$ through the comparison of clinical effects of $T-PLS^{TM}$ (pulsatile pump) and $Bio-pump^{TM}$ (non-pulsatile pump) used for coronary bypass surgery. Material and Method: The comparison was made on 40 patients who had coronary bypass using $T-PLS^{TM}\;and\;Bio-pump^{TM}$ (20 patients for each) from April 2003 to June 2005. All of the surgeries were operated on pump beating coronary artery bypass graft using cardiopulmonary extra-corporeal circulation. Risk factors before surgery and the condition during surgery and the results were compared. Result: There was no significant difference in age, gender ratio, and risk factors before surgery such as history of diabetes, hypertension, smoking, obstructive pulmonary disease, coronary infarction, and renal failure between the two groups. Surgery duration, hours of heart-lung machine operation, used shunt and grafted coronary branch were little different between the two groups. The two groups had a similar level of systolic arterial pressure, diastolic arterial pressure and mean arterial pressure, but pulse pressure was measured higher in the group with $T-PLS^{TM}\;(46{\pm}15\;mmHg\;in\;T-PLS^{TM}\;vs\;35{\pm}13\;mmHg\;in\;Bio-pump^{TM},\;p<0.05)$. The $T-PLS^{TM}$-operated patients tended to produce more urine volume during surgery, but the difference was not statistically significant $(9.7{\pm}3.9\;cc/min\;in\;T-PLS^{TM}\;vs\;8.9{\pm}3.6\;cc/min\;in\;Bio-pump^{TM},\;p=0.20)$. There was no significant difference in mean duration of respirator usage and 24-hour blood loss after surgery between the two groups. Plasma free Hb was measured lower in the group with $T-PLS^{TM}\;(24.5{\pm}21.7\;mg/dL\;in\;T-PLS^{TM}\;versus\;46.8{\pm}23.0mg/dL\;in\;Bio-pump^{TM},\;p<0.05)$. There was no significant difference in coronary infarction, arrhythmia, renal failure and morbidity rate of cerebrovascular disease. There was a case of death after surgery (death rate of 5%) in the group tested with $T-PLS^{TM}$, but the death rate was not statistically significant. Conclusion: Coronary bypass was operated with $T-PLS^{TM}$ (Pulsatile flow pump) using a heart-lung machine. There was no unexpected event caused by mechanical error during surgery, and the clinical process of the surgery was the same as the surgery for which $Bio-pump^{TM}$ was used. In addition, $T-PLS^{TM}$ used surgery was found to be less detrimental to blood corpuscles than the pulsatile flow has been known to be. Authors of this study could confirm the safety of $T-PLS^{TM}$.

Germination and Proteome Profile Characteristics of Wheat Seeds Treated under Different Concentrations of Abscisic Acid (Abscisic acid 농도에 따른 밀 종자의 발아와 단백질체의 발현 특성)

  • Jeong, Jae-Hyeok;Kim, Dae-Wook;Hwang, Woon-Ha;An, Sung-Hyun;Jeong, Han-Yong;Lee, Hyeon-Seok;Choi, In-Bea;Choi, Kyung-Jin;Yun, Jong-Tak;Yun, Song Joong
    • KOREAN JOURNAL OF CROP SCIENCE
    • /
    • v.63 no.1
    • /
    • pp.25-34
    • /
    • 2018
  • This study was conducted to investigate the germination and proteome profile characteristics of wheat seeds treated under various concentrations of abscisic acid (ABA). After-ripening, the seeds of three wheat cultivars (Baegjoong, Keumkang, and Uri) showing different levels of dormancy were used. Germination index and germination rate of the cultivars was higher than 0.95% and 98%, respectively, and these were not significantly different under 0, 10, 30, and $50{\mu}M$ ABA at 7 d after germination. However, the growth of the shoot and radicle was significantly inhibited at 10, 30, and $50{\mu}M$ ABA compared to that at $0{\mu}M$ ABA. Mean ABA content of the embryos of seeds germinated at 0 and $50{\mu}M$ ABA for 7 d was 0.8 and $269.0ngmg^{-1}DW$, respectively. Proteins extracted from embryos germinated for 4 d were analyzed by two-dimensional gel electrophoresis, and proteins showing a difference of 1.5-fold or greater in their spot volume relative to that of $0{\mu}M$ ABA were identified. The expression of four protein spots increased at $50{\mu}M$ ABA and two protein spots were detected only at $50{\mu}M$ ABA; these six proteins were all identified as globulin types. Conversely, the expression of three protein spots decreased at $50{\mu}M$ ABA and were identified as cytosolic glutamine sysnthetase, isocitrate dehydrogenase, and S-adenosylmethionine synthetase 2. In conclusion, ABA did not inhibit the germination rate regardless of pre-harvest sprouting characteristics of the cultivars. However, the growth of the shoot and radicle was significantly inhibited by ABA, most likely through the down regulation of glutamine, methyl group donor, and polyamines biosynthesis, among others, while accompanied by globulin accumulation in the embryos.

Experimental Study of Flip-Bucket Type Hydraulic Energy Dissipator on Steep slope Channel (긴구배수로 감세공의 Filp Bucket형 이용연구)

  • 김영배
    • Magazine of the Korean Society of Agricultural Engineers
    • /
    • v.13 no.1
    • /
    • pp.2206-2217
    • /
    • 1971
  • Spillway and discharge channel of reservoirs require the Control of Large volume of water under high pressure. The energies at the downstream end of spillway or discharge channel are tremendous. Therefore, Some means of expending the energy of the high-velocity flow is required to prevent scour of the riverbed, minimize erosion, and prevent undermining structures or dam it self. This may be accomplished by Constructing an energy dissipator at the downstream end of spillway or discharge channel disigned to dissipated the excessive energy and establish safe flow Condition in the outlet channel. There are many types of energy dissipators, stilling basins are the most familar energy dissipator. In the stilling basin, most energies are dissipated by hydraulic jump. stilling basins have some length to cover hydraulic jump length. So stilling basins require much concrete works and high construction cost. Flip bucket type energy dissipators require less construction cost. If the streambed is composed of firm rock and it is certain that the scour will not progress upstream to the extent that the safety of the structure might be endangered, flip backet type energy dissipators are the most recommendable one. Following items are tested and studied with bucket radius, $R=7h_2$,(medium of $4h_2{\geqq}R{\geqq}10h_2$). 1. Allowable upstream channel slop of bucket. 2. Adequate bucket lip angle for good performance of flip bucket. Also followings are reviwed. 1. Scour by jet flow. 2. Negative pressure distribution and air movement below nappe flow. From the test and study, following results were obtained. 1. Upstream channel slope of bucket (S=H/L) should be 0.25<H/L<0.75 for good performance of flip bucket. 2. Adequated lip angle $30^{\circ}{\sim}40^{\circ}$ are more reliable than $20^{\circ}{\sim}30^{\circ}$ for the safety of structures.

  • PDF

Evaluating efficiency of Split VMAT plan for prostate cancer radiotherapy involving pelvic lymph nodes (골반 림프선을 포함한 전립선암 치료 시 Split VMAT plan의 유용성 평가)

  • Mun, Jun Ki;Son, Sang Jun;Kim, Dae Ho;Seo, Seok Jin
    • The Journal of Korean Society for Radiation Therapy
    • /
    • v.27 no.2
    • /
    • pp.145-156
    • /
    • 2015
  • Purpose : The purpose of this study is to evaluate the efficiency of Split VMAT planning(Contouring rectum divided into an upper and a lower for reduce rectum dose) compare to Conventional VMAT planning(Contouring whole rectum) for prostate cancer radiotherapy involving pelvic lymph nodes. Materials and Methods : A total of 9 cases were enrolled. Each case received radiotherapy with Split VMAT planning to the prostate involving pelvic lymph nodes. Treatment was delivered using TrueBeam STX(Varian Medical Systems, USA) and planned on Eclipse(Ver. 10.0.42, Varian, USA), PRO3(Progressive Resolution Optimizer 10.0.28), AAA(Anisotropic Analytic Algorithm Ver. 10.0.28). Lower rectum contour was defined as starting 1cm superior and ending 1cm inferior to the prostate PTV, upper rectum is a part, except lower rectum from the whole rectum. Split VMAT plan parameters consisted of 10MV coplanar $360^{\circ}$ arcs. Each arc had $30^{\circ}$ and $30^{\circ}$ collimator angle, respectively. An SIB(Simultaneous Integrated Boost) treatment prescription was employed delivering 50.4Gy to pelvic lymph nodes and 63~70Gy to the prostate in 28 fractions. $D_{mean}$ of whole rectum on Split VMAT plan was applied for DVC(Dose Volume Constraint) of the whole rectum for Conventional VMAT plan. In addition, all parameters were set to be the same of existing treatment plans. To minimize the dose difference that shows up randomly on optimizing, all plans were optimized and calculated twice respectively using a 0.2cm grid. All plans were normalized to the prostate $PTV_{100%}$ = 90% or 95%. A comparison of $D_{mean}$ of whole rectum, upperr ectum, lower rectum, and bladder, $V_{50%}$ of upper rectum, total MU and H.I.(Homogeneity Index) and C.I.(Conformity Index) of the PTV was used for technique evaluation. All Split VMAT plans were verified by gamma test with portal dosimetry using EPID. Results : Using DVH analysis, a difference between the Conventional and the Split VMAT plans was demonstrated. The Split VMAT plan demonstrated better in the $D_{mean}$ of whole rectum, Up to 134.4 cGy, at least 43.5 cGy, the average difference was 75.6 cGy and in the $D_{mean}$ of upper rectum, Up to 1113.5 cGy, at least 87.2 cGy, the average difference was 550.5 cGy and in the $D_{mean}$ of lower rectum, Up to 100.5 cGy, at least -34.6 cGy, the average difference was 34.3 cGy and in the $D_{mean}$ of bladder, Up to 271 cGy, at least -55.5 cGy, the average difference was 117.8 cGy and in $V_{50%}$ of upper rectum, Up to 63.4%, at least 3.2%, the average difference was 23.2%. There was no significant difference on H.I., and C.I. of the PTV among two plans. The Split VMAT plan is average 77 MU more than another. All IMRT verification gamma test results for the Split VMAT plan passed over 90.0% at 2 mm / 2%. Conclusion : As a result, the Split VMAT plan appeared to be more favorable in most cases than the Conventional VMAT plan for prostate cancer radiotherapy involving pelvic lymph nodes. By using the split VMAT planning technique it was possible to reduce the upper rectum dose, thus reducing whole rectal dose when compared to conventional VMAT planning. Also using the split VMAT planning technique increase the treatment efficiency.

  • PDF

A Study on Developing Customized Bolus using 3D Printers (3D 프린터를 이용한 Customized Bolus 제작에 관한 연구)

  • Jung, Sang Min;Yang, Jin Ho;Lee, Seung Hyun;Kim, Jin Uk;Yeom, Du Seok
    • The Journal of Korean Society for Radiation Therapy
    • /
    • v.27 no.1
    • /
    • pp.61-71
    • /
    • 2015
  • Purpose : 3D Printers are used to create three-dimensional models based on blueprints. Based on this characteristic, it is feasible to develop a bolus that can minimize the air gap between skin and bolus in radiotherapy. This study aims to compare and analyze air gap and target dose at the branded 1 cm bolus with the developed customized bolus using 3D printers. Materials and Methods : RANDO phantom with a protruded tumor was used to procure images using CT simulator. CT DICOM file was transferred into the STL file, equivalent to 3D printers. Using this, customized bolus molding box (maintaining the 1 cm width) was created by processing 3D printers, and paraffin was melted to develop the customized bolus. The air gap of customized bolus and the branded 1 cm bolus was checked, and the differences in air gap was used to compare $D_{max}$, $D_{min}$, $D_{mean}$, $D_{95%}$ and $V_{95%}$ in treatment plan through Eclipse. Results : Customized bolus production period took about 3 days. The total volume of air gap was average $3.9cm^3$ at the customized bolus. And it was average $29.6cm^3$ at the branded 1 cm bolus. The customized bolus developed by the 3D printer was more useful in minimizing the air gap than the branded 1 cm bolus. In the 6 MV photon, at the customized bolus, $D_{max}$, $D_{min}$, $D_{mean}$, $D_{95%}$, $V_{95%}$ of GTV were 102.8%, 88.1%, 99.1%, 95.0%, 94.4% and the $D_{max}$, $D_{min}$, $D_{mean}$, $D_{95%}$, $V_{95%}$ of branded 1cm bolus were 101.4%, 92.0%, 98.2%, 95.2%, 95.7%, respectively. In the proton, at the customized bolus, $D_{max}$, $D_{min}$, $D_{mean}$, $D_{95%}$, $V_{95%}$ of GTV were 104.1%, 84.0%, 101.2%, 95.1%, 99.8% and the $D_{max}$, $D_{min}$, $D_{mean}$, $D_{95%}$, $V_{95%}$ of branded 1cm bolus were 104.8%, 87.9%, 101.5%, 94.9%, 99.9%, respectively. Thus, in treatment plan, there was no significant difference between the customized bolus and 1 cm bolus. However, the normal tissue nearby the GTV showed relatively lower radiation dose. Conclusion : The customized bolus developed by 3D printers was effective in minimizing the air gap, especially when it is used against the treatment area with irregular surface. However, the air gap between branded bolus and skin was not enough to cause a change in target dose. On the other hand, in the chest wall could confirm that dose decrease for small the air gap. Customized bolus production period took about 3 days and the development cost was quite expensive. Therefore, the commercialization of customized bolus developed by 3D printers requires low-cost 3D printer materials, adequate for the use of bolus.

  • PDF

Comparison and evaluation of volumetric modulated arc therapy and intensity modulated radiation therapy plans for postoperative radiation therapy of prostate cancer patient using a rectal balloon (직장풍선을 삽입한 전립선암 환자의 수술 후 방사선 치료 시 용적변조와 세기변조방사선치료계획 비교 평가)

  • Jung, hae youn;Seok, jin yong;Hong, joo wan;Chang, nam jun;Choi, byeong don;Park, jin hong
    • The Journal of Korean Society for Radiation Therapy
    • /
    • v.27 no.1
    • /
    • pp.45-52
    • /
    • 2015
  • Purpose : The dose distribution of organ at risk (OAR) and normal tissue is affected by treatment technique in postoperative radiation therapy for prostate cancer. The aim of this study was to compare dose distribution characteristic and to evaluate treatment efficiency by devising VMAT plans according to applying differed number of arc and IMRT plan for postoperative patient of prostate cancer radiation therapy using a rectal balloon. Materials and Methods : Ten patients who received postoperative prostate radiation therapy in our hospital were compared. CT images of patients who inserted rectal balloon were acquired with 3 mm thickness and 10 MV energy of HD120MLC equipped Truebeam STx (Varian, Palo Alto, USA) was applied by using Eclipse (Version 11.0, Varian, Palo Alto, USA). 1 Arc, 2 Arc VMAT plans and 7-field IMRT plan were devised for each patient and same values were applied for dose volume constraint and plan normalization. To evaluate these plans, PTV coverage, conformity index (CI) and homogeneity index (HI) were compared and $R_{50%}$ was calculated to assess low dose spillage as per treatment plan. $D_{25%}$ of rectum and bladder Dmean were compared on OAR. And to evaluate the treatment efficiency, total monitor units(MU) and delivery time were considered. Each assessed result was analyzed by average value of 10 patients. Additionally, portal dosimetry was carried out for accuracy verification of beam delivery. Results : There was no significant difference on PTV coverage and HI among 3 plans. Especially CI and $R_{50%}$ on 7F-IMRT were the highest as 1.230, 3.991 respectively(p=0.00). Rectum $D_{25%}$ was similar between 1A-VMAT and 2A-VMAT. But approximately 7% higher value was observed on 7F-IMRT compare to the others(p=0.02) and bladder Dmean were similar among the all plan(P>0.05). Total MU were 494.7, 479.7, 757.9 respectively(P=0.00) for 1A-VMAT, 2A-VMAT, 7F-IMRT and at the most on 7F-IMRT. The delivery time were 65.2sec, 133.1sec, 145.5sec respectively(p=0.00). The obvious shortest time was observed on 1A-VMAT. All plans indicated over 99.5%(p=0.00) of gamma pass rate (2 mm, 2%) in portal dosimetry quality assurance. Conclusion : As a result of study, postoperative prostate cancer radiation therapy for patient using a rectal balloon, there was no significant difference of PTV coverage but 1A-VMAT and 2A-VMAT were more efficient for dose reduction of normal tissue and OARs. Between VMAT plans. $R_{50%}$ and MU were little lower in 2A-VMAT but 1A-VMAT has the shortest delivery time. So it is regarded to be an effective plan and it can reduce intra-fractional motion of patient also.

  • PDF

The Benefit of Individualized Custom Bolus in the Postmastectomy Radiation Therapy : Numerical Analysis with 3-D Treatment Planning (유방전절제술 후 방사선치료를 위한 조직보상체 개발 및 3차원 치료계획을 통한 유용성 분석)

  • Cho Jae Ho;Cho Kwang Hwan;Keum Kichang;Han Yongyih;Kim Yong Bae;Chu Sung Sil;Suh Chang Ok
    • Radiation Oncology Journal
    • /
    • v.21 no.1
    • /
    • pp.82-93
    • /
    • 2003
  • Purpose : To reduce the Irradiation dose to the lungs and heart in the case of chest wail irradiation using an oppositional electron beam, we used an Individualized custom bolus, which was precisely designed to compensate for the differences In chest wall thickness. The benefits were evaluated by comparing the normal tissue complication probablilties (NTCPS) and dose statistics both with and without boluses. Materials and Methods : Boluses were made, and their effects evaluated in ten patients treated using the reverse hockey-stick technique. The electron beam energy was determined so as to administer 80% of the irradiation prescription dose to the deepest lung-chest wall border, which was usually located at the internal mammary lymph node chain. An individualized custom bolus was prepared to compensate for a chest wall thinner than the prescription depth by meticulously measuring the chest wall thickness at 1 emf intervals on the planning CT Images. A second planning CT was obtained overlying the individuailzed custom bolus for each patient's chest wall. 3-D treatment planning was peformed using ADAC-Pinnacle$^{3}$ for all patients with and without bolus. NTCPS based on 'the Lyman-Kutcher' model were analyzed and the mean, maximum, minimum doses, V$_{50}$ and V$_{95}$ for 4he heari and lungs were computed. Results .The average NTCPS in the ipsliateral lung showed a statistically significant reduction (p<0.01), from 80.2${\pm}$3.43% to 47.7${\pm}$4.61%, with the use of the individualized custom boluses. The mean lung irradiation dose to the ipsilateral iung was also significantly reduced by about 430 cGy, Trom 2757 cGy to 2,327 cGy (p<0.01). The V$_{50}$ and V$_{95}$ in the ipsilateral lung markedly decreased from the averages of 54.5 and 17.4% to 45.3 and 11.0%, respectively. The V$_{50}$ and V$_{95}$ In the heart also decreased from the averages of 16.8 and 6.1% to 9.8% and 2.2%, respectively. The NTCP In the contralateral lung and the heart were 0%, even for the cases with no bolus because of the small effective mean radiation volume values of 4.4 and 7.1%, respectively Conclusion : The use of an Individualized custom bolus in the radiotherapy of postrnastectorny chest wall reduced the NTCP of the ipsilateral lung by about 24.5 to 40.5%, which can improve the complication free cure probability of breast cancer patients.

The Effect of Deep Breathing Methods on Pulmonary Ventilatory Function of Patients Who experiened Upper-abdominal surgery (심호흡 방법에 따른 상복부 수술환자의 폐 환기능에 미치는 효과)

  • Hwang Jin-Hee;Park Hyung-Suk
    • Journal of Korean Academy of Fundamentals of Nursing
    • /
    • v.1 no.2
    • /
    • pp.129-147
    • /
    • 1994
  • The purpose of this study was to examine the effect of deep breathing exercise with Incentive Spirometer on the pulmonary ventilatory function of postoperative patients. This experiment was operated by quasi-experimental design which was compared pre-experimental measures with post-experimental ones. The subject of this study was 46 inpatients who were scheduled for elective upper abdominal surgery under the general anesthesia in P National University Hospital in Pusan and classified into the experimental group(23 patients) and control group(23 patients) by using Incentive Spirometer or unusing one. The data were collected from November, 1, 1993, to December, 31, 1993. The effects of the deep breathing exercise on the pulmonary ventilatory function were compared between experimental group who were recieved deep breathing exercise with Incentive Spirometer and control group who were recieved same method without Incentive Spirometer. The Forced Vital Capacity (FVC) and the First Second Forced Expiratory Volume ($FEV_1$) were represented as index of the pulmonary ventilatory function and those were measured by Vitalograph Compact. The collected data were analysed by SPSS/PC+ (percentage, average, standard deviation, chi-square test, t-test, and ANOVA). The results were as follow : (1) The $FVC_s$ of the experimental group were significantly increased in course of time, 24, 48, 72 hours after surgery(F=3.530, P=0.035). (2) The $FVC_s$ and $FEV_{1S}$ of the control group were significantly increased in course of time, 24, 48, 72 hours after surgery ($FVC_s$ : F=3.480, P=0.037, $FEV_{1S}$ : F=6. 153, P=0.004). (3) The FVC which was measured at 72 hours after surgery was significantly higher in the experimental group than in the control group(t=2.620, P=0.013). (4) The $FEV_{1s}$ which were measured at 24 and 72 hours after surgery were significantly higher in the experimental group than in the control group(24hr. : t=2.530, P=0.017, 72hr. : t=2.540, P=0.016). (5) Among general characteristics, sex was significant variable which influenced to effect of pulmonary ventilatory function. In conclusion, this study showed that the deep breathing exercise with Incentive Spirometer was more effective to recover the pulmonary ventilatory function after surgery than the deep breathing exercise without Incentive Spirometer.

  • PDF