• Title/Summary/Keyword: ingot

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A Study on the Reduction of Segregation in Large 12%Cr Steel Ingot (12%Cr 대형강괴(大型鋼塊)의 편석경감(偏析輕減)에 관(關)한 연구(硏究))

  • Eun, Ok-Ki;Chang, Yun-Souk
    • Journal of Korea Foundry Society
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    • v.10 no.6
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    • pp.520-527
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    • 1990
  • In order to reduce segregation in 12%Cr steel ingots of 60-100tons, numerical analysis by computer was applied to simulate solidification profiles and the profiles of liguid-solid coexisting zone in accordance with the ratios of H(Height) /D(diameter) of 100-ton ingot. The result is that the ratio of L(vertical length) /D(diameter) of liquid-solid coexisting zone was reduced in proportion to the decrease of H/D ratio. With the reduced H/D ratio(0.92) of ingot, the segregation in 60-ton ingot of 12% Cr steel can be much reduced and recovery was also improved by reducing ingot weight.

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Study on Internal Void Closure in Slab ingot during Hot Plate Forging (열간 판재단조시 강괴 내부의 기공폐쇄에 관한 연구)

  • 조종래;김동권;김영득;이부윤
    • Transactions of Materials Processing
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    • v.5 no.1
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    • pp.18-26
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    • 1996
  • In order to investigate the effect of pre-cooling of ingot on void closure in hot plate forging the internal strain and stress distributions are examined quantitatively by using ABAQUS. Simula-tions are carried out on a large slab ingot having the same temperature and the temperature gradient induced by air-cooling. It is shown that pre-cooling produces little effect on the strain behavior but remarkable effect on the hydrostatic stress at the central zone of ingot. The main factors for crushing micro-voids are the effective strain and the time integral of hydrostatic stress in the region surrounding the voids. Based on regression analysis it was found that the distortion of void can be expressed as a polynomial function of the two factors.

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Assessment of Recrystallization Behavior in Ingot-Breakdown Process of Alloy 718 (Alloy 718의 잉고트 파쇄공정시 재결정거동에 대한 해석)

  • Yeom, J.T.;Lee, C.S.;Kim, J.H.;Kim, N.Y.;Park, N.K.
    • Proceedings of the Korean Society for Technology of Plasticity Conference
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    • 2007.10a
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    • pp.42-45
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    • 2007
  • Recrystallization behavior during ingot-breakdown process of Alloy 718 was investigated with finite element analysis and experimental approaches. In order to analyze microstructural changes during the cogging process of an Alloy 718 ingot, the side-pressing and heat treatment tests were performed at different temperatures and ram speed. From the side-pressing and heat treatment test results, it was found that microstructural changes during hot forging of Alloy 718 ingot greatly influenced on a close interaction between dynamic and static-recrystallization behaviors. A recrystallization model of Alloy 718 was used to predict the complex microstructural variation during continuous heating and forging processes of the cogging, and the predicted grain size and its distribution were compared with the actual cogged Alloy 718 billet.

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A STUDY ON THE PRESSING ACCURACY OF THE REUSED IPS-EMPERESS INGOT (재 사용된 IPS-empress ingot의 pressing accuracy에 관한 연구)

  • Song, Byung-Kwen;Park, Hyun-Bae;Oh, Sang-Chun;Jin, Tae-Ho
    • The Journal of Korean Academy of Prosthodontics
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    • v.35 no.2
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    • pp.357-364
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    • 1997
  • IPS-empress system is one of widely used all ceramic system. The purpose of this study was to determine the pressing accuracy of reused IPS%Empress ingot. 10 specimens were made using new ingot first, and using the rests of the specimen the another group of specimens were made next. finally, the third group of specimens were made with same procedure mentioned above. The results obtained in this study were as follows ; 1. The pressing accuracy of the first group of specimen was 96.1%, that of the second group was 95.4%, and that of the third group was 95.4%. There was no statistical significance among them, that is, the reuse of the IPS-Empress ingot did not influence on the pressing accuracy. 2. the common site of the defect in pressed ingot was central area at the margin opposite of sprue hole.

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Volume Expansion of TiMn2-type Hydrogen Storage Alloy with Hydrogenation (TiMn2계 수소저장합금의 수소화에 따른 부피팽창)

  • PARK, CHOONG-NYEON
    • Transactions of the Korean hydrogen and new energy society
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    • v.28 no.5
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    • pp.459-464
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    • 2017
  • The volume expansions of $Ti_{0.95}Zr_{0.05}V_{0.4}Mn_{1.45}Fe_{0.1}Cr_{0.05}$ alloy during hydrogenation with various conditions have been investigated. The theoretical volume expansion measured with XRD for this alloy with hydrogenation was 21%. The apparent volume expansion of this alloy ingot with hydrogenation was composed of two effects. One is a hydrogenation and the other is a pulverization. The apparent volume of free alloy powder was 1.8 times greater than that of an ingot, implying the pulverization effect on the apparent volume expansion is 80%. The apparent volume expansion of the alloy ingot with hydrogenation under a unconstrained condition was about 80 (${\pm}15$)%, much smaller than that of free alloy powder which expected as 118%. In addition, The apparent volume expansion of the alloy ingot with hydrogenation under a constrained condition(Al container) was about 50%, much smaller than that of the unconsrained. This reduced apparent volume expansion of the alloy ingot could be attributed to an arrangement of alloy powder keeping its original shape of the ingot even after hydrogenation.

Uranium ingot casting method with Uranium deposit in a Pyroprocessing (사용후핵연료 파이로 공정 중 우라늄 전착물의 잉곳 제조 방법)

  • Lee, Yoon-Sang;Cho, Choon-Ho;Lee, Sung-Ho;Kim, Jeong-Guk;Lee, Han-Soo
    • Journal of Nuclear Fuel Cycle and Waste Technology(JNFCWT)
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    • v.8 no.1
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    • pp.85-89
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    • 2010
  • The uranium ingot casting process is one of the steps which consolidate uranium deposits produced by electrorefiner as an ingot form in a pryprocessing technique. This paper introduces new design concept of the ingot casting equipment and the performance test results of the lab-scale ingot casting equipment fabricated based on the design concept. Casting equipment produces the uranium ingot by pouring an uranium melt into a mold by tilting a melting crucible. Also it is equipped with a cup which is able to continuously feed uranium deposits into a melting crucible. The productivity could be significantly enhanced by introducing the continuous operation concept.

Ingot-Breakdown Design of Tower Flange Material for Offshore Wind Turbine (해상풍력발전용 타워플랜지 소재의 잉고트 파쇄공정설계)

  • Yoo, G.Y.;Kang, N.H.;Kim, J.H.;Hong, J.K.;Lee, C.S.;Lee, J.M.;Kim, N.Y.;Yeom, J.T.
    • Transactions of Materials Processing
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    • v.21 no.7
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    • pp.412-419
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    • 2012
  • The ingot-breakdown scheme of a tower flange material (low-alloy steel) for offshore wind turbine was investigated using finite element (FE) simulations and experimental analyses. Based on compression test results of the low-alloy steel, a deformation processing map was generated using the superposition approach between the dynamic materials model (DMM) and Ziegler's instability criterion. The deformation processing map allowed determination of the optimum process conditions for the tower flange material. Within the FE simulations of the ingot breakdown process, the Cockcroft-Latham criterion, which considers ductile fracture, was used to predict the possibility of forming defects during the hot working process. In general, the critical value for the ductile fracture of steel is 0.74. During the ingot-breakdown under optimum process conditions, the actual tower flange forgings exhibited a relatively uniform shape without any forming defects.

Optimal Water-cooling Tube Design for both Defect Free Process Operation and Energy Minimization in Czochralski Process (무결정결함영역을 유지하면서 에너지를 절감하는 초크랄스키 실리콘 단결정 성장로 수냉관 최적 설계)

  • Chae, Kang Ho;Cho, Na Yeong;Cho, Min Je;Jung, Hyeon Jun;Jung, Jae Hak;Sung, Su Whan;Yook, Young Jin
    • Current Photovoltaic Research
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    • v.6 no.2
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    • pp.49-55
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    • 2018
  • Recently solar cell industry needs the optimal design of Czochralski process for low cost high quality silicon mono crystalline ingot. Because market needs both high efficient solar cell and similar cost with multi-crystalline Si ingot. For cost reduction in Czochralski process, first of all energy reduction should be completed because Czochralski process is high energy consumption process. For this purpose we studied optimal water-cooling tube design and simultaneously we also check the quality of ingot with Von mises stress and V(pull speed of ingot)/G(temperature gradient to the crystallization) values. At this research we used $CG-Sim^{(R)}$ S/W package and finally we got improved water-cooling tube design than normally used process in present industry. The optimal water-cooling tube length should be 200mm. The result will be adopted at real industry.