• Title/Summary/Keyword: feed-through

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Feed-through Noise Reduction Technique for MEMS Gyroscope (MEMS Gyroscope를 위한 feed-through 노이즈 제거 기법)

  • Park, Kyung-Jin;Kang, Seong-Mook;Baek, Chang-Wook;Kim, Ho-Seong
    • The Transactions of The Korean Institute of Electrical Engineers
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    • v.58 no.11
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    • pp.2247-2252
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    • 2009
  • Since the dimensions of MEMS gyroscope are very small compared to those of conventional gyroscope, MEMS gyroscope should be able to measure charge of pico-coulomb caused by very small change of electrodes gap. However, feed-through signal from driving electrodes to the sensing electrodes due to the electromagnetic coupling is much greater than the sensing signal, which degrades the sensitivity of MEMS gyroscope. This paper introduces the feed-through noise canceling technique using dummy port and confirms the feasibility of feed-through noise canceling experimentally. Experimental results shows that, when driving signal is 6 Vpp, 30 kHz, feed-through signal of vacuum packaged Si Gyroscope decreases from -53.2 dBm to -77.1 dBm by using feed-through reduction technique. Q-factor that could not be measured without noise reduction is measured to be about 2500 and resonance frequency to be 7.018 kHz.

Feed-through noise reduction technique for MEMS Gyroscope (MEMS Gyroscope를 위한 feed-through 노이즈 제거 기법)

  • Park, Kyung-Jin;Kang, Seong-Mook;Kim, Ho-Seong;Baek, Chang-Wook
    • Proceedings of the KIEE Conference
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    • 2009.07a
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    • pp.1503_1504
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    • 2009
  • MEMS 구조물은 ${\mu}m$단위의 크기로 만들어지므로 각속도계와 같이 정밀한 센서를 만들 때에는 노이즈 문제를 해결하지 않으면 신호를 측정할 수가 없다. MEMS 구조물의 미세한 진동에 의해 발생되는 수 pico-coulomb의 전하를 측정해야하므로 구동 신호가 검출 전극에서 Feed-through되어 나타나는 경우 그 크기가 구동에 의한 신호보다 100배 이상 크기 때문에 원하는 신호를 검출할 수 없다. 본 논문에서는 이러한 Feed-through 현상에 의한 노이즈를 줄이기 위하여 Guard-ring을 이용한 blocking 방법과 dummy port를 이용한 canceling 방법을 고안하고 Feed-through reduction 회로를 설계, 제작, 실험하여 그 효과를 확인하였다. 그 결과 구동신호가 6Vpp, 30kHz일 때, -53.186dBm이었던 Feed-through 신호가 -77.107dBm으로 줄어드는 것을 확인하였다. 또한 노이즈를 제거하지 않은 경우 측정할 수 없었던 Q-factor를 Feed-through reduction 회로를 사용하여 측정한 결과 진공 패키징된 Si 기반 자이로스코프가 공진주파수 약 7.018kHz에서 Q-factor가 약 2500임을 확인하였다.

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Modeling of the Axial Movement of Parts During Centerless Through-Feed Grinding

  • Kim, Kang
    • Journal of Mechanical Science and Technology
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    • v.17 no.7
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    • pp.1044-1053
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    • 2003
  • There are two major differences between the centerless infeed grinding process and the centerless through-feed grinding process. One is an axial movement of workpieces, and the other is that several workpieces are ground simultaneously and continuously by through-feeding. Because of these differences, through-feed ground parts inherently possess not only the roundness error but also the tapering error. The aims of the research reported in this paper are to examine this inherent tapering characteristic and to find the effects of grinding variables (center height angle, regulating wheel tilt angle, and shape of grinding wheel surface). To accomplish the objectives, experiments were carried out using two types of cylindrical workpiece shapes. Also, computer simulations were performed using the 3-D through-feed grinding model.

Study on Cause and Effect of SG Feed Water Ring Through-Wall Hole (증기발생기 급수링 관통손상 원인 및 영향 고찰)

  • Lee, Sung Ho;Lee, Yo Seob
    • Transactions of the Korean Society of Pressure Vessels and Piping
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    • v.11 no.1
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    • pp.61-68
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    • 2015
  • The function of Feed Water Ring is to provide the flow path from Feedwater Nozzle to inside of SG(steam generator). Significant amounts of general FAC on the outside of the Feed Water Ring are not likely due to the low flow velocities in this area. However, on the interior of the Feed Water Ring, there may be areas of local higher flow velocity which could lead to higher FAC rates. These may include the inlet tee from the Feedwater Nozzle into the Feed Water Ring, the areas where the Feed Water Ring changes diameter, and especially the entrance area to the J-Nozzles. In this paper, the results of root cause analysis of through-wall hole observed at domestic WH 51F SG Feed Water Ring and its effect on the integrity and performance of SG are described. And, the maintenance strategy for WH 51F SG Feed Water Ring and the monitoring strategy for Downcomer Feed Water Ring of CE System 80 SG are presented.

Design and Implementation of RSS feed search engine for Effective Contents Service (효과적인 콘텐츠 서비스를 위한 RSS피드 검색 엔진의 설계 및 구현)

  • Lee, Hae sung;Kwon, Joon Hee
    • Journal of Korea Society of Digital Industry and Information Management
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    • v.4 no.1
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    • pp.1-8
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    • 2008
  • In the Web 2.0, besides more gaining information on the web, the number of web sites that take advantage of RSS increases explosively. Commonly each users search RSS channels through the web search engine before registering RSS channel's url to the RSS reader. Users judge whether the site is RSS channel or not and register an RSS channel's url through theirs interests. Because accomplished by users themselves, those processes conflict to user's convenience and quick consumption of information. Techniques of current search engines can't provide users with reliable RSS feed information as search results. In this paper, we analysis appropriateness of current search engines' techniques that offer users RSS feed search service and discuss their limitations. Also, we make up RSS feed database through classification of RSS tag being possible to search RSS feed information effectively and apply update rate of each RSS channel's feed to ranking algorithm providing more reliable search results.

Gate Driving Methods to Compensate Feed-Through Voltage for Large Size, High Quality TFT-LCD (대면적 고화질 TFT-LCD의 Feed-through 전압 보상을 위한 Gate Driving 방법)

  • 정순신;윤영준;박재우;최종선
    • Proceedings of the Korean Institute of Electrical and Electronic Material Engineers Conference
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    • 1999.11a
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    • pp.99-102
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    • 1999
  • In recent years, attempts have been made to greatly improve the display quality of active-matrix liquid crystal display devices, and many techniques have been proposed to solve such problems as gate signal delay, feed-through voltage and image sticking. To improve these problems which are caused by the fried-through voltage, we have evaluated new driving methods to reduce the fled-through voltage. Two level gate-pulse was used for the gate driving of the cst-on-common structure pixels. And two-gate line driving methods with the optimized gate signals were applied for the cst-on-gate structure pixels. These gate driving methods were better feed-through characteristics than conventional simple gate pulse. The evaluation of the suggested driving methods were performed by using a TFT-LCD array simulator PDAST which can simulate the gate, data and pixel voltages of a certain pixel at any time and at any location on a TFT array. The effect of the new driving method was effectively analyzed.

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Temperature control for once through boiler (관류형 보일러의 온도제어)

  • 김은기
    • 제어로봇시스템학회:학술대회논문집
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    • 1991.10a
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    • pp.900-904
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    • 1991
  • It is important and difficult to control the steam temperature in the once through boiler. Generally, steam temperature of once through boiler not only is controlled by boiler spray water flow, but also is influenced by feed water flow and fuel flow. So we have to make the same gain of fuel flow controller and feed water flow controller. This paper is shown the design and test of steam temperature and feed water flow control system for once through boiler in pusan thermal power plant.

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볼엔드밀 절삭공정의 절삭력 디지털 제어

  • 이천환;이건복
    • Proceedings of the Korean Society of Precision Engineering Conference
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    • 1992.10a
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    • pp.198-203
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    • 1992
  • There are two important variables in machining process control, which are feed and cutting speed. It is possible to improve the machining accuracy and the productivity by maintaining the optimal feed and cutting speed. IN this work, a controller is designed to achieve on-line cutting force control based on the modeling of cutting process dynamics established through step response test. Two schemes are proposed and implemented. The first is feed control under the constant spindle speed and the second is spindle speed control under the constant feed. Finally, both are proved to work properly through simulation and experimentation.

Optimized Gate Driving to Compensate Feed-through Voltage for $C_{ST}-on-Common$

  • Jung, Soon-Shin;Yun, Young-Jun;Park, Jae-Woo;Roh, Won-Yeol;Choi, Jong-Sun
    • 한국정보디스플레이학회:학술대회논문집
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    • 2000.01a
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    • pp.73-74
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    • 2000
  • In recent years, attempts have been made to greatly improve the display quality of active-matrix liquid crystal display devices, and many techniques have been proposed to solve such problems as gate signal delay, feed-through voltage and image sticking[1-3]. To improve these problems which are caused by the feed-through voltage, we have evaluated new driving methods to reduce the feed-through voltage. Two level gate-pulse was used for the gate driving of the cst-on-common structure pixels. These gate driving methods offer better feed-through characteristics than conventional simple gate pulse. Optimized step signal will compensate by step pulse time and voltage. The evaluation of the suggested driving methods were performed by using a TFT-LCD array simulator PDAST which can simulate the gate, data and pixel voltages of a certain pixel at any time and at any location on a TFT array. The effect of the new driving method was effectively analyzed.

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Modeling of the Centerless Through-feed Grinding Process

  • Kim, Kang
    • Journal of Mechanical Science and Technology
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    • v.17 no.7
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    • pp.1036-1043
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    • 2003
  • A computer simulation method for investigating the form generation mechanism in the centerless through-feed grinding process is described. The length of the contact line and the magnitude of the grinding force between the grinding wheel and workpieces, vary with the change in the axial location of the current workpiece during grinding. Thus, a new coordinate system and a grinding force curve of previous and/or following workpieces are introduced to treat the axial motion. Experiments and computer simulations were carried out using four types of cylindrical workpiece shapes. To validate this model, simulation results are compared with the experimental results.