• Title/Summary/Keyword: conventional forming

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Methods for Suppressing Tearing of PET Coating During Forming of VCM Steel Sheet for Fabricating Washer (세탁기용 VCM 강판 성형시 PET 코팅층 찢김 저감방법)

  • Son, Young-Ki;Lee, Chan-Joo;Byeon, Sang-Doek;Kim, Myong-Dok;Kim, Byung-Min
    • Transactions of the Korean Society of Mechanical Engineers A
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    • v.35 no.9
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    • pp.1027-1033
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    • 2011
  • A VCM sheet is a metal sheet on which PET/PVC is coated for outer panels of home appliances. The purpose of this study is to obtain methods for suppressing PET tearing that occurs during the press forming of the VCM sheet. In order to identity the factors that minimize PET tearing, an FE analysis was performed. The occurrence of PET tearing cannot be predicted using the conventional forming limit diagram. PET is torn by friction between a die and sheet, which is caused by the thickening of material at a die corner. To reduce the thickening of material, the blank shape was re-designed and the thickened material at a flange was removed by a trimming process. The results of the FE-analysis involving modified process parameters showed that the thickness of the product at a die corner is distributed within the clearance of drawing and flangeforming process. A forming experiment was conducted to verify the proposed process parameters. A good final product was obtained without PET tearing of the VCM sheet.

Analysis on performance of grid-free compressive beamforming based on experiment (실험 기반 무격자 압축 빔형성 성능 분석)

  • Shin, Myoungin;Cho, Youngbin;Choo, Youngmin;Lee, Keunhwa;Hong, Jungpyo;Kim, Seongil;Hong, Wooyoung
    • The Journal of the Acoustical Society of Korea
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    • v.39 no.3
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    • pp.179-190
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    • 2020
  • In this paper, we estimated the Direction of Arrival (DOA) using Conventional BeamForming (CBF), adaptive beamforming and compressive beamforming. Minimum Variance Distortionless Response (MVDR) and Multiple Signal Classification (MUSIC) are used as the adaptive beamforming, and grid-free compressive sensing is applied for the compressive sensing beamforming. Theoretical background and limitations of each technique are introduced, and the performance of each technique is compared through simulation and real experiments. The real experiments are conducted in the presence of reflected signal, transmitting a sound using two speakers and receiving acoustic data through a linear array consisting of eight microphones. Simulation and experimental results show that the adaptive beamforming and the grid-free compressive beamforming have a higher resolution than conventional beamforming when there are uncorrelated signals. On the other hand, the performance of the adaptive beamforming is degraded by the reflected signals whereas the grid-free compressive beamforming still improves the conventional beamforming resolution regardless of reflected signal presence.

Effects of Application of Latex Coated Urea on Yield and Nitrogen-Use Efficiency for 10-day Old Seedling Machine Transplanted (Latex 피복요소시용(被覆尿素施用)이 어린모기계이앙(機械移秧) 벼의 질소이용효율(窒素利用效率)과 수량(收量)에 미치는 영향)

  • Yoo, Chul-Hyun;Kang, Seung-Weon;Shin, Bog-Woo;Han, Sang-Soo;Kim, Seong-Jo
    • Korean Journal of Soil Science and Fertilizer
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    • v.32 no.2
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    • pp.140-146
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    • 1999
  • This research was conducted to investigate the changes of $NH_4-N$ in soil, nitrogen uptake by rice plant, nitrogen-use efficiency and rice yield by the application of latex coated urea(LCU) on 10-day old seedling transplanted with machine on paddy field, Jeonbuk series at the Honam area, from 1997 to 1998. Almost all nitrogen in LCU application as basal dressing in whole layer was dissolved until maximum tiller stage, the maximum dissolution time was productive tiller stage and $NH_4-N$ content of conventional plot with surface application of fertilizer were lowered at full periods. Nitrogen deficiency symptom were appeared at heading stage of 31.6% SPAD value and nitrogen concentration was 1.29% shoot. From heading stage to ripening stage, the necessity of nitrogen-fertilizer was $2.9kg\;ha^{-1}$ for the conventional split application plot and $11.9kg\;ha^{-1}$ for the whole layer application plot of LCU basal dressing. Nitrogen-use efficiency was higher at the LCU application plot than the conventional application plot and was increased for 12.7% by fertilization at panicle forming stage. The additional fertilization at panicle forming stage to basal dressing of LCU causes 13% yield increase.

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An Implementation of Fuzzy Automatic Gauge Control for the Plate Steel Rolling Process (후판 압연공정에서 퍼지 두께제어 구현)

  • Hur, Yone-Gi;Choi, Young-Kiu
    • Journal of Institute of Control, Robotics and Systems
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    • v.15 no.6
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    • pp.634-640
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    • 2009
  • The plate manufacturing processes are composed of the reheating furnace, finishing mill, cooling process and hot leveling. The finishing rolling mill (FM) as a reversing mill has produced the plate steel through multiple pass rolling. The automatic gauge control (AGC) is employed to maintain the thickness tolerance. The high grade products are forming greater parts of the manufacturing and customers are requiring strict thickness margin. For this reason, the advanced AGC method is required instead of the conventional AGC based on the PI control. To overcome the slow response performance of the conventional AGC and the thickness measurement delay, a fuzzy AGC based on the thickness deviation and its trend is proposed in this paper. An embedded controller with the fuzzy AGC has been developed and implemented at the plate mill in POSCO. The fuzzy AGC has dynamically controlled the roll gap in real time with the programmable logic controller (PLC). On line tests have been performed for the general and TMCP products. As the results, the thickness deviation range (maximum - minimum of the inner plate) is averagely from 0.3 to 0.1 mm over the full length. The fuzzy AGC has improved thickness deviation and completely satisfied customer needs.

A Study on Development of Combined Drawing Process for Automotive Cowl Cross Bar with Variable Diameters (가변직경을 갖는 자동차용 카울크로스바의 복합인발공정 개발에 관한 연구)

  • Kim, H.S.;Youn, J.W.
    • Transactions of Materials Processing
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    • v.18 no.7
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    • pp.538-543
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    • 2009
  • The cowl cross bar of an automobile is a frame component that is installed inside the cockpit module to provide a guide surface, to which functional components for electricity and air condition are attached. In the recent years, the geometries of cowl cross bars are getting more complex in order to meet the demands of a wide variety of embedded functional components and the reduced weight of frame parts with enhanced mechanical and noise/vibration characteristics. There for, welding processes between tubes with different diameters are widely conducted while the welded parts are experiencing various problems such as undermined appearance, low production efficiency and poor mechanical characteristics. Therefore, this paper seeks to develop an one-piece forming process which eliminate welding process for the cowl cross bar by applying the tube drawing process. However, it was predicted that a conventional tube drawing can not be applied directly to the current part since the area reduction ratio of the drawing process reaches 51.7% which exceeds the general limiting value. Therefore, in this study, a combined drawing process which adds a compressive force to a tensile force of the conventional drawing process was proposed and 2-stage drawing process was designed by using CAE analyses. In addition, drawing tryouts were carried out by using the manufactured combined drawing machine in order to verify the designed process.

Calculating Array Patterns Using an Active Element Pattern Method with Ground Edge Effects

  • Lee, Sun-Gyu;Lee, Jeong-Hae
    • Journal of electromagnetic engineering and science
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    • v.18 no.3
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    • pp.175-181
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    • 2018
  • The array patterns of a patch array antenna were calculated using an active element pattern (AEP) method that considers ground edge effects. The classical equivalent radiation model of the patch antenna, which is characterized by two radiating slots, was adopted, and the AEPs that include mutual coupling were precisely calculated using full-wave simulated S-parameters. To improve the accuracy of the calculation, the edge diffraction of a ground plane was incorporated into AEP using the uniform geometrical theory of diffraction. The array patterns were then calculated on the basis of the computed AEPs. The array patterns obtained through the conventional AEP approach and the AEP method that takes ground edge effects into account were compared with the findings derived through full-wave simulations conducted using a High Frequency Structure Simulator (HFSS) and FEKO software. Results showed that the array patterns calculated using the proposed AEP method are more accurate than those derived using the conventional AEP technique, especially under a small number of array elements or under increased steering angles.

Process Modification and Numerical Simulation for an Outer Race of a CV Joint using Multi-Stage Cold Forging (등속조인트용 외륜의 다단 냉간 단조공정을 위한 공정개선 및 유한요소 해석)

  • Kang, B.S.;Ku, T.W.
    • Transactions of Materials Processing
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    • v.23 no.4
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    • pp.211-220
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    • 2014
  • The outer race of a constant velocity (CV) joint having six inner ball grooves has traditionally been manufactured by multi-stage warm forging, which includes forward extrusion, upsetting, backward extrusions, necking, ironing and sizing, and machining. In the current study, a multi-stage cold forging process is examined and an assessment for replacing and modifying the conventional multi-stage warm forging is made. The proposed procedure is simplified to the backward extrusion of the conventional process, and the sizing and necking are combined into a single sizing-necking step. Thus, the forging surface of the six ball grooves can be obtained without additional machining. To verify the suitability of the proposed process, a 3-dimensional numerical simulation on each operation was performed. The forging loads were also predicted. In addition, a structural integrity evaluation for the tools was carried out. Based on the results, it is shown that the dimensional requirements of the outer race can be well met.

Atomization Improvement of a Liquid Jet with Wall Impingement and its Application to a Jet Engine Atomizer

  • Shiga, Seiichi
    • Journal of ILASS-Korea
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    • v.11 no.3
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    • pp.176-189
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    • 2006
  • In the present study, capability of improving the liquid atomization of a high-speed liquid jet by using wall impingement is explored, and its application to a jet engine atomize. is demonstrated. Water is injected from a thin nozzle. The liquid jet impinges on a wall positioned close to the nozzle exit, forming a liquid film. The liquid film velocity and the SMD were measured with PDA and LDSA, respectively. It was shown that the SMD of the droplets was determined by the liquid film velocity and impingement angle, regardless of the injection pressure or impingement wall diameter. When the liquid film velocity was smaller than 300m/s, a smaller SMD was obtained, compared with a simple free jet. This wall impingement technique was applied to a conventional air-blasting nozzle for jet engines. A real-size air-blasting burner was installed in a test rig in which three thin holes were made to accommodate liquid injection toward the intermediate ring, as an impingement wall. The air velocity was varied from 41 to 92m/s, and the liquid injection pressure was varied from 0.5 to 7.5 MPa. Combining wall impinging pressure atomization with gas-blasting produces remarkable improvement in atomization, which is contributed by the droplets produced in the pressure atomization mode. Comparison with the previous formulation for conventional gas-blasting atomization is also made, and the effectiveness of utilizing pressure atomization with wall impingement is shown.

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Improvement of the Stamping Formability by BHF Control (블랭크 홀딩력 제어에 의한 스탬핑 가공성 향상 기술)

  • 김영석;임성언;손형성;한수식
    • Transactions of Materials Processing
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    • v.8 no.3
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    • pp.269-275
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    • 1999
  • A variable blank holding force method is proposed to improve deep drawing characteristics of sheet materials. In this method, the blank holding force (BHF) is controlled throughout a drawing process so that the punch load does not exceed a critical value, which is slightly less than the conventional process with the conforming process with the variable BHF is more flexible than the conventional process with the constant BHF and it could be used for improving the product's quality and drawability. In this paper we suggest a method controlling the BHF as a function of punch travel during the forming process. The optimization BHF curves are determined theoretically and experimentally. It is concluded that for the case of optimum BHF control methods the drawn cup height and the drawing formability achieved by this method are increased than those for constant BHF method. Also, as comparing the wall thickness distribution of the cup drawn by the constant BHF and the optimum BHF control, the BHF control reduce the wall thickness variation of the drawn cup at the cup wall and make the cup thickness distribution more uniformly than the constant BHF.

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Evaluation of Excess Sludge Reduction in the OSA Process using Kinetic Parameter and Mass Balance (동역학계수 및 물질수지를 이용한 OSA공정의 잉여슬러지 감량능 평가)

  • Nam, Duck-Hyun;Jang, Hyung-Suk;Ha, Kuem-Ryul;Kim, Joon-Kyu;Ju, Jae-Young;Jung, In-Ho;Park, Chul-Hwi
    • Journal of Korean Society on Water Environment
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    • v.25 no.4
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    • pp.530-538
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    • 2009
  • The Oxic-Settling-Anaerobic (OSA) treatment process, a modified Conventional Activated Sludge (CAS) process, was developed for the purpose of sludge reduction. The insertion of a sludge holding tank into a sludge return line, an anaerobic reactor, forming an OSA process, may provide a cost-effective way of reducing excess sludge production during a process. The OSA process was evaluated for its sludge reduction ability by kinetic parameter and mass balance, with an observed excess sludge reduction of 63.5%, as $P_{X.VSS}$, compared with the conventional activated sludge process.