• 제목/요약/키워드: Water/wastewater treatment

검색결과 2,067건 처리시간 0.023초

화학적 처리에 의한 1차 하수처리장의 처리효과 개선 -현장시험을 중심으로- (Chemically Enhanced Primary Treatment at D Wastewater Treatment Plant)

  • 곽종운;김승현;이찬원
    • 상하수도학회지
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    • 제11권1호
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    • pp.99-108
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    • 1997
  • This study examined the feasbility of upgrading D waste water treatment plant which treats incoming wastewater by primary sedimentation only. By adding 20-40 ppm of Hi-PAX into the outlet of the aerated grit chamber, BOD and SS removal efficiences were improved from 29% and 36% to 53 % and 73%,respectively. However, chemically enhanced primary treatment failed to meet the upcoming wastewater quality standard(BOD and SS <20 mg/l) consistently. This was suspected to result from the deteriorated plant return stream. The wastewater treatment by chemical treatment should have increased the amount of the sludge to be removed as the sludge production was increased. Chemically enhanced primary treatment is anticipated to consistently produce effluent of the 1996 standards quality by adjusting the amount of the sludge to be removed. Besides BOD and SS removal, chemically enhanced primary treatment resulted in the improved T-P removal from 30% to 64-74%. However, such benefit was not observed in T-N removal. Improved T-P removal will be expected to help control water pollution in Masan bay.

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환경·생태학적 기법을 이용한 혼합폐수 처리장의 생물학적 처리공정 내의 미생물 군집 특성 분석 (Analysis of Microbial Community Structure in Biological Wastewater Treatment Process of Mixed Wastewater Treatment Facility using Environmental·Ecological Technique)

  • 손형식;이상준;손희종
    • KSBB Journal
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    • 제28권2호
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    • pp.80-85
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    • 2013
  • The bacterial community structure in a biological reactor fed influent from a wastewater treatment system was investigated by denaturing gradient gel electrophoresis (DGGE) and in situ hybridization. Sludges were collected from three biological reactors (aerobic, oxic, and anoxic tanks) at the M wastewater treatment facility (WTF). The influent of the MWTF consisted of mixed tannery wastewater (40~65%) and seafood wastewater (35~60%). The treatment processes resulted in a removal efficiency for BOD (biochemical oxygen demand) and COD (chemical oxygen demand) of 83.6~98.2% and 72.8~84.6%, respectively for tannery wastewater than for seafood wastewater resulted in greater survival of biomass in the biological reactors and a higher removal of BOD, COD, and T-N of about 8~18%. In contrast, addition of greater amounts of seafood wastewater decreased the amount of biomass in the bioreactors due to the increasing concentration of chromium from that wastewater and it also. The dominant bacterial species during the high seafood wastewater input period were Burkholderia cepacia (JX901049) and an uncultured bacterium (JF247555), while Pseudomonas geniculata (HQ256559) was dominant during the high tannery wastewater input period. Flavobacteriumsp. BF.107 (FM173271) and Hyphomicrobium zavarzinii (Y14306) were dominant under anoxic conditions.

하수종말처리장 방류수를 밭작물 관개용수로 처리시 시금치와 배추의 생육, 대장균 분포 및 토양의 질 평가 (Growth Response and Total Coliform Distribution of Spinach and Chinese Cabbage and Soil Quality by Irrigation of Domestic Wastewater)

  • 조재영;박승우;손재권;박봉주;이용근
    • 농촌계획
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    • 제12권2호
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    • pp.57-64
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    • 2006
  • The experiment was carried out to determine the distribution of total coliform the translocation of heavy metals and the salt accumulation in soils following the supply of ground water, the domestic wastewater and the ultraviolet treatment of domestic wastewater during the spinach and the chinese cabbage cultivation. There were not much changes in the Total-N, Total-P and cations in soils following the ultraviolet treatment of the domestic wastewater. However, the density of total coliform was dramatically reduced from 894MPN/100mL to 5MPN/100mL. The diagnosis of composition of soil after the harvest of chinese cabbages and spinach has shown that the concentration of Na$^+$ was 3-4 times higher in plot using domestic wastewater than in plot using ground water. When domestic wastewater and ground water were used in growing spinach md chinese cabbage at 50% each, the application of chemical fertilizers reduced about 25% to 50% compared to the criteria set down by the Rural Development Administration and there was not significant difference in terms of harvest. Using non-ultraviolet treatment of domestic wastewater directly on spinach and chinese cabbage has resulted in excessive density of total coliform at 25,000MPN/100mL. Even when ultraviolet treatment, the density was still high at 2,000MPN/100mL. The high density of total coliform even following ultraviolet treatment of domestic wastewater is considered to be caused by photo-reactivation of micro-organism. When reusing domestic wastewater, the application of sterilization such as ultraviolet, ultrasonic and electron-beam for public health and hygiene reasons may provide safe supply of agricultural water.

화학 응집제 투입에 따른 수질항목별 하수처리 반응곡선 (Saturation curves for chemical coagulation of wastewater treatment)

  • 류재나;오재일;이경종
    • 상하수도학회지
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    • 제24권5호
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    • pp.537-548
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    • 2010
  • Recently the Government has announced updated water quality standards for wastewater treatment effluent (become effective in 2012). That includes highly enforced regulations for T-P, BOD and COD, and a large budget, in particular for phosphorus removal, was set by the Ministry of environment. Chemical coagulation destabilizes colloidal particles so that particles grow to larger flocs, and solid particles are removed by solid-liquid separation. The efficiency of chemical coagulation depends on a various factors, including coagulant types and costs, construction and operation costs for the treatment facilities and so on. The proper selection should be based on the treatment efficiency of coagulants and underlying costs. The current research was to evaluate the treatment efficiencies of coagulants on a variety of wastewater influents and to develop saturation curves for several water quality parameters. Typical $Al_2(SO_4)_3$ and $FeCl_3$ were tested under a range of coagulant concentrations. The pollutant removal efficiencies of chemical treatment both for the $Al_2(SO_4)_3$ and $FeCl_3$ were especially high for T-P, followed by SS, BOD and COD. Correlation test also proved the highest relationship between SS and T-P.

Performance evaluation of nitrate removal in high TDS wet scrubber wastewater by ion exchange resin with dissolved air flotation (DAF) process

  • Kim, Bongchul;Yeo, Inseol;Park, Chan-gyu
    • Membrane and Water Treatment
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    • 제13권1호
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    • pp.1-6
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    • 2022
  • The regulations of the International Maritime Organization (IMO) have been steadily strengthened in ship emissions. Accordingly, there is a growing need for development of related technologies for the removal of contaminants that may occur during the treatment of SOx and NOx using a wet scrubber. However, this system also leads to wastewater production when the exhaust gas is scrubbed. In this research, we evaluated the performance of an ion selective resin process in accordance with scrubber wastewater discharge regulations, specifically nitrate discharge, by the IMO. Accelerated real and synthetic wastewater of wet scrubbers, contained high amounts of TDS with high nitrate, is used as feed water in lab scale systems. Furthermore, a pilot scale dissolved air flotation (DAF) using microbubble generator with ion exchange resin process was combined and developed in order to apply for the treatment of wet scrubber wastewater. The results of the present study revealed that operating conditions, such as resin property, bed volume (BV), and inlet wastewater flow rate, significantly affect the removal performance. Finally, through a pilot test, DAF with ion exchange resin process showed a noticeable improvement of the nitrate removal rate compared to the single DAF process.

MHD 수처리방식에 의한 에멀젼오일폐수의 처리 (Emulsified Oily Wastewater Treatment by MHD Water Treatment Device)

  • 김인수;박승조
    • Journal of Advanced Marine Engineering and Technology
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    • 제17권4호
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    • pp.20-27
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    • 1993
  • Emulsified oily wastewater is generally hard to treat in separating oil and water by conventional separators. In this paper the magnetohydrodynamic water treatment device was used to separate oil from emulsified oily wastewater which contained high conductivity. The emulsified oil removal rates and economic ranges of oil separation at various factors were investigated to confirm the influence of the magnetic field in MHD water treatment device according to the characteristics of emulsion brake. Experimental results proved that the oil removal rates were proportional to Lorentz force which depends on the intensity of magnetic field, conductivity and velocity of wastewater.

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염색폐수의 생물학적 색도제거 연구 (Biological Decolorization Characteristics of Dyeing Wastewater)

  • 김미경;서상준;신응배
    • 한국물환경학회지
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    • 제22권2호
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    • pp.333-341
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    • 2006
  • The concept for the decolorization in biological dye wastewater treatment systems is based on anaerobic treatment, for the reductive cleavage of the dyes' azo linkages, in combination with aerobic treatment, for the degradation of the products from azo dye cleavage, aromatic amines. Batch tests were conducted to examine the conditions and the factors affecting biological treatment of dye wastewater. From the tests, the removal efficiencies of organics and colors of dyeing wastewater were improved to $COD_{Cr}$ 27% and color 9% by injecting 10% of the domestic wastewater as a cosubstrate, and $COD_{Cr}$ 30%, color 22% with 30% injection of domestic wastewater. Therefore it was proved that decolorization efficiency is demonstrated with domestic wastewater as a cosubstrate. The analysis of aromatic amines in wastewater showed that decolorization was achieved by cometabolism while aromatic amines were produced by cleavage of azo bonds under anaerobic conditions and these products were removed in an aerobic tank subsequently.

교량 바닥판 보수공사에서 발생하는 콘크리트 폐수처리 방안 (Treatment of Concrete Wastewater in Repair of Bridge Deck)

  • 이봉학;최판길;김정기
    • 산업기술연구
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    • 제28권A호
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    • pp.125-132
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    • 2008
  • As of 2003, construction waste has been produced at the level of 130,614.8 tons/day, in which the amount of waste concrete was 92,639.1 tons/day and accounted for about 66.4% of the amount of construction waste. Waste concrete is mainly produced in construction work and civil engineering work. Especially, road surface crushing method using a large amount of water requires thorough management of concrete wastewater. The aim of this study was to analyze water pollution due to concrete wastewater generated in repair of bridge deck using road surface crushing equipment and to suggest reasonable countermeasures for solve the problem. In this study, it was surveyed current conditions of produced concrete wastewater in bridge deck repair, analyzed physical features of concrete wastewater, expected effects of water pollution on inflow rivers if it is not treated, established treatment plan of water pollution by categories, and calculated capacity of each treatment process and required amount of necessary chemicals. As a result of sampling wastewater generated in field sites and testing it at a lab scale, it was revealed that the original wastewater was produced in removing concrete from bridge deck slabs using surface crushing equipment whose pH was 12.53, CODMn was 12.910mg/L, SS was 547.0mg/L, and other heavy metals were included in extremely small quantities.

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국내 하수처리시설 에너지 등급 평가를 위한 ENERWATER의 적용 가능성에 관한 연구 (A Study on the Applicability of ENERWATER for Evaluation of the Energy Consumption Label of WWTPs in Korea)

  • 박민오;이호식
    • 한국물환경학회지
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    • 제38권5호
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    • pp.231-239
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    • 2022
  • In this study, we applied ENERWATER to evaluate the energy consumption labeling of wastewater treatment plants in Korea using the Korea sewerage statistics data. The results showed that the energy label status was excellent in the SBR process for small and medium-scale wastewater treatment plants and the A2O process for large-scale wastewater treatment plants. The energy labeling of wastewater treatment plants of 50,000 tons capacity was excellent. The statuses of metropolitan cities and Jeollanam-do province were excellent. We analyzed the effects of renewable energy on wastewater treatment plants' energy consumption and found out that digestion gas for large-scale plants and photovoltaic energy for small-scale plants were effective in improving energy labeling. In addition, we compared the energy labels of four wastewater treatment plants in "Z" city and wastewater treatment plant "X" had the best energy label, and the wastewater treatment plants "V" and "Y" had to be selected as priorities for the energy diagnosis and improvement project. In a comprehensive conclusion, the applicability of ENERWATER was confirmed based on sewage statistics data and labeling can be used to set priorities for the energy diagnosis and improvement project.