• Title/Summary/Keyword: Turbocharger noise

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차량용 터보차져의 소음도표 작성 및 응용 (Noise Diagram of an Automotive Turbo Charger and Its Applications)

  • 이형일
    • 한국소음진동공학회논문집
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    • 제20권5호
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    • pp.502-509
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    • 2010
  • A test facility which can simultaneously measure turbocharger operating condition variables and vibro-acoustic emission in the situations that are quite similar to real internal combustion engine operating conditions has been introduced. Using this facility, a new method sweeping from full open throttle to deep surge region along constant speed curves can be utilized instead of the stationary method that has been traditionally used to obtain turbocharger compressor maps. Data covering an extensive range of the compressor performance map have been collected and analyzed. An experimental study is performed to define a noise diagram that correlates vibro-acoustic measurements to aerothermodynamic operating conditions. An instrumentation set in the facility allows the automatic definition of the operating point on the turbine and compressor map of the turbocharger. Also, radiated sound pressure and casing vibration data corresponding to the point are obtained by a microphone in the vicinity of the compressor casing and an accelerometer on the casing. The major source(s) of noise at specific operating point on the map can be easily identified with these maps. Also, acoustic characteristics of a given turbocharger at the vicinity of the surge as well as in the surge are also defined. Finally, the possibility to define mild surge region of a turbocharger using vibro-acoustic measurements is studied.

터보 차져 디젤 엔진에서의 기류음 감소를 위한 연구 (A study on the reduction of the flow-induced noise in turbo-charger diesel engines)

  • 강웅;김형진;성형진
    • 대한기계학회:학술대회논문집
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    • 대한기계학회 2007년도 춘계학술대회B
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    • pp.2913-2917
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    • 2007
  • Turbocharger has been widely used in many passenger cars in application with diesel engines because of high power and fuel efficiency. However, flow-induced noise (whoosh or hissing noise) which is generated within the compressor during its operation at marginal surge line can deteriorate noise characteristics. Hissing noise excitation was associated with the generation of turbulence within the turbocharger compressor and radiated through the transmission path in turbocharger system. In this study, a sharp-edged reactive-type muffler was devised and installed in the transmission path to reduce the hissing noise. Acoustic and fluid dynamic characteristics for the muffler were investigated which is related to the unsteadiness of turbulence and pressure in turbocharger system. A transfer matrix method was used to analyze the transmission loss of the muffler. Simple expansion muffler with extended tube of the reactive type is proposed for the reduction of high frequency component noise. Turbulence computation was carried out by a standard ${\kappa}-{\varepsilon}$ model. An optimal design condition of the muffler was obtained by extensive acoustic and fluid dynamic analysis on the engine dynamometer with anechoic chamber. A significant reduction of the hissing noise was achieved at the optimal design of the muffler as compared with the conventional turbocharger system.

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대형 디젤 엔진 터보차져 고주파 소음에 관한 연구 (Investigation on Turbocharger Whine Noise in a Heavy-duty Diesel Engine)

  • 최성배;정용진;여승동
    • 한국음향학회:학술대회논문집
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    • 한국음향학회 2000년도 학술발표대회 논문집 제19권 2호
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    • pp.235-238
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    • 2000
  • Current diesel engines are usually equipped with turbochargers for improving fuel economy as well as meeting more stringent emission regulations. These turbochargers usually cause noise problems because they spins vey high such as 100,000 to 200,000 rpm, These noises are largely divided into whistle and whine noises. The frequency of whistle noise corresponds to their rotation speed, and the frequency of whine noise does to the multiplication of their rotation speed and the number of compressor blades. Turbocharger manufacturers developed a special type of compressor, effectively compressing air sucked from a duct; Recirculation Compressor Cover (RCC) or Map Width Enhancement (MWE). This special structure improves turbocharger's capability by expanding compressor's working area, but it seriously causes a noise problem, whine noise. There were many trials to surpress the noise occurred inside a compressor such as modification of a compressor, noise baffles or secondary measurements. However, it was currently concluded that the whine noise caused by the special compressor can not be reduced to that done by a standard compressor, and the strength difference of whine noises between the two compressors is not negligible. Thus, the standard compressor is decided to be applied to a newly developing heavy-duty diesel engine in order to resolve the turbocharger noise problem with a stiffened suction duct directly connected to a compressor.

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삽입관이 있는 확장형 소음기에서의 기류음 감소 (Reduction of Flow-Induced Noise in an Expansion Muffler with Lids)

  • 강웅;김형진;성형진
    • 대한기계학회논문집B
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    • 제33권2호
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    • pp.79-84
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    • 2009
  • Turbocharger has been widely used in many passenger cars in application with diesel engines because of high power and fuel efficiency. However, flow-induced noise (whoosh or hissing noise) which is generated within a compressor during its operation at marginal surge line can deteriorate noise characteristics. Hissing noise excitation is associated with the generation of turbulence within the turbocharger compressor and radiated through the transmission path in a turbocharger system. In this study, a expansion muffler with lids is devised and installed in the transmission path to reduce the hissing noise. Acoustic and fluid dynamic characteristics for the muffler are investigated which are related to the unsteadiness of turbulence and pressure in the turbocharger system. A transfer matrix method is used to analyze the transmission loss of the muffler. A simple expansion muffler with lids is proposed for the reduction of high frequency component noise. Turbulence simulation is carried out by a standard k - ${\varepsilon}$ model. An optimal design condition of the muffler is obtained by extensive acoustic and fluid dynamic analysis on the engine dynamometer with anechoic chamber. A significant reduction of the hissing noise is achieved at the optimal design of the muffler as compared with the conventional muffler.

디젤 엔진에서의 터보 차저 Blow 소음 저감 위한 시뮬레이션 기반 공명기 위치 최적화 (Simulation-based Optimum Allocation of a Resonator for Reducing the Blow Noise of a Turbocharger in a Diesel Engine)

  • 강용헌;최동훈
    • 한국자동차공학회논문집
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    • 제18권2호
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    • pp.129-134
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    • 2010
  • A diesel engine is equipped with a turbocharger for providing more power at a low engine speed region by supplying charge air to combustion chambers. The turbocharger makes it possible to satisfy stringent emission regulations and customers' demand of enjoying the fun to drive by increasing engine performance. However, the turbocharger has the disadvantage of making BPF(Blade Passing Frequency), hissing, surge, whistle, and blow noises. Among them, reducing the blow noise, a narrow-band noise(a general range : 1800~2000Hz), is possible by using a resonator that controls the narrow frequency band governing the resonance in the intake system. In this study, the optimum location of the resonator is found by employing Boost as a CAE(Computer Aided Engineering) tool and is confirmed by experiments of an engine dynamo test and a real vehicle test.

과급기 축계의 진동 해석 (Vibration Analysis of Turbocharger Rotor-Bearing System)

  • Suk, Ho-Il;Yang, Bo-Suk;Song, Jin-Dea
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2002년도 추계학술대회논문초록집
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    • pp.400.2-400
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    • 2002
  • Recently rotating machines have became high speed and high Power and light weight. Bearings are one of the main components which influence power loss and stability of rotating machines. Appropriate bearing should be selected with considering characteristics of rotating machine. Floating ring journal bearing(FIB) consists of an inner film and outer film, and possess high damping and stability. FJB has been for adopted into turbocharger for the high stability at high operating speed. (omitted)

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차량용 터보차져의 컴프레서 BPF 소음 저감 (Compressor BPF noise reduction for an automotive turbocharger)

  • 박호일;엄상봉;서주봉;이승현
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2012년도 춘계학술대회 논문집
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    • pp.851-856
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    • 2012
  • Automotive turbochargers have become common in gasoline engines as well as diesel engines. They are excellent devices to effectively increase fuel efficiency and power of the engines, but they unfortunately cause several noise problems. The noises are classified into mechanical noises induced from movement of a rotating shaft and aerodynamic noises by air flow in turbochargers. The mechanical noises are whine and howling noises, and the aerodynamic noises are BPF (blade-passing frequency), pulsation, surge, some special frequency noises. These noises are bothering passengers because their levels are higher or their frequencies are clearly separated from engine or vehicle noises. The noise investigated in this paper is a BPF noise induced by compressor wheels, whose frequency is the multiplication of the number of compressor wheel blades and its rotational speed. The noise is strongly dependent upon the geometry of wheels and the number of blades. This study tried to apply a groove close to the inlet side of compressor wheels in order to reduce the BPF noise. The groove has successfully reduced the noise of narrow band frequency of a turbocharger. It shows that the groove could reduce the wide band frequency noise, the compressor BPF noise with a best shape of the groove.

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차량용 터보차져 흡기 유동음 최적 개선 (Optimization of an Intake Flow Noise Induced from an Automotive Turbocharger)

  • 박호일;최성배;장성식;황준영
    • 한국소음진동공학회논문집
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    • 제25권8호
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    • pp.546-552
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    • 2015
  • In the previous study, the air flow noise around 1.6 k~1.8 kHz was analyzed, and could be reduced by machining a groove in the bore of compressor inlet in front of the main blades of a compressor wheel. It was proven that this groove was very effective for removing the noise without critical sacrifice of compressor performance, and in addition, it did not noticeably deteriorate vehicle performance, drivability and acceleration. It is interesting that the type of groove tried for 1.6~1.8 kHz noise reduction could be effective for another air flow noise, 4 k~6 kHz which is the 3rd order frequency range of turbocharger speed. This study tried various shapes of grooves for minimizing engine performance difference as well as reducing the 3rd order noise. Finally, it was shown that the groove should be round for the engine performance, and an optimal size exist for the noise and the engine performance.

터보차져 NVH 시험장치 (The Turbocharger Cold Test Bench for NVH test)

  • 김형진;최상보;김재헌;강구태
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2007년도 추계학술대회논문집
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    • pp.913-917
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    • 2007
  • The turbocharger for a vehicle is consisting of a centrifugal compressor and turbine. These compressor and turbine are vibrating and emitting noises through the T/C body, exhaust system (Catalyst, Bellows, Pipe, etc) and Intake system (Hoses, Intercooler pipes, Intercooler) as rotating. A turbocharger cold test bench is constructed to reduce these noises, especially for the purpose of realizing transient operating environment and oil temperature control to simulate the vehicle operating characteristics with intake system and exhaust system. This research laid the groundwork to develop a lower noise level T/C through understanding the mechanism of the noise source of T/C.

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3 기통 엔진의 터보 차저 맥동 저감에 대한 연구 (A study about reducing Turbocharger Pulsation of 3 cylinder engine)

  • 서광현;조성용
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2014년도 추계학술대회 논문집
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    • pp.667-669
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    • 2014
  • Development of 3 cylinder turbo charger engine is increasing due to engine down-sizing, cost reduction and emission regulations. However, 3 cylinder engine makes higher Exhaust manifold gas pressure(P3) pulsation than 4 cylinder engine and it generate boosting air with high pulsation. The mechanical waste-gate turbocharger just controlled by the boosting air has higher movement because of this high pulsation boosting air. This causes high vibrations to wasted gate and accelerate wear of the linkage system. So we need to understand out of the exhaust gas pressure pulsation changed by turbocharger compressor pressure(P2) Pulsation. In this study, we discuss how to prevent to abnormal movement of the turbo actuator by stabilized P2 Pulsation.

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