• Title/Summary/Keyword: Turbo engine

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A Study on Power loading Experiment & Performance Analysis for Dynamic Transient Effect of a Turbo-shaft Engine with Free Power Turbine (분리 축 가스 터빈 엔진의 동역학적 천이 효과를 고려한 성능 해석 및 부하 인가 시험에 관한 연구)

  • Kim Gyoung-du;Yang Soo-seok
    • Journal of the Korean Society of Propulsion Engineers
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    • v.8 no.3
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    • pp.17-26
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    • 2004
  • In this paper, power transmission systems converts the shaft power of a Turbo-shaft Engine with Free Power Turbine into the generator power and be composed of a method being supplied in the thrust motor driving a propellers. Being used this, Gas turbine engine works to flat rating about 110 kw (147 shp) that the thrust motor be extremely supplied from the engine of 317shp. In this test equipment, the engine is installed with the flywheel being able to the damping function when happen to the varying load between gas turbine engine output-shaft and generator. Then if the flywheel of inertial moment be not considered, the generator and motor not get the required power from the engine for raising the load. Also it is certified that the engine works the abnormal operation. Hence the flywheel of inertial moment is determined the required range to do the performance analysis with the dynamic transient from the given and tested engine data. This system is able to get the required power after a mounting test with the redesigned flywheel.

Development of T700/701K Engine for KUH (한국형 기동 헬기 엔진 (T700/701K) 개발)

  • Kim, Jae-Hwan;Ahn, Iee-Ki;Lee, Dae-Sung;Sung, Ok-Suck;Sung, In-Kyung
    • Journal of the Korean Society of Propulsion Engineers
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    • v.15 no.4
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    • pp.79-84
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    • 2011
  • This paper presents development activities of the T700/701K turbo-shaft engine for Korean Utility Helicopter(KUH). The T700/701K is the first rear-drive variant of the GE's T700 engine which is proven for military applications in the world. The main workscope of the development includes a modification from a front-drive engine to a rear-drive one, an performance enhancement of the power turbine and an incorporation of two channel FADEC(Full Authority Digital Engine Control) system for more reliable operation. The first engine run for development and qualification test was successfully completed in 2008. Since the PFRT(Preliminary Flight Rating Test) has been completed, the first flight of the engine installed in the first prototype of KUH has been successfully demonstrated in March, 2010 and the engine installation compatibility tests are being carried out during KUH flight test. The test and evaluation for qualification has been done except for the low cycle fatigue test up to date.

A Study on the Rotordynamic Stability of Turbo Pump Unit

  • Kwak, Hyun-Duck;Lee, Yong-Bok;Kim, Chang-Ho;Ha, Tae-Woong;Yoo, Woo-Chul
    • KSTLE International Journal
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    • v.4 no.1
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    • pp.1-7
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    • 2003
  • A turbo pump unit provides high pressure oxygen and fuel in a space shuttle main engine (SSME). This paper focused on rotordynamics, investigating its characteristics based on a numerical simulation of turbo pump finite element model. Speeds up to 50,000 rpm are considered, as well as the special problems related to elastic-ring, seal hydrodynamic force, shroud force and clearance-excitation farce. The rotordynamic prediction shows that the elastic-ring which is inserted between the casing and the outer race of ball bearing allows far an acceptable separate margin of first critical speed. Additionally, the results show that the floating ring seal, which have a peculiar ring, adds substantial stiffness and damping to the system as well as exhibits superior performance in terms of rotordynamic stability of system compared to the plain seal.

Qualification Process of T700/701K Engine for KUH (한국형 기동헬기 엔진 (T700/701K) 인증 과정)

  • Jung, Yong-Wun;Kim, Jae-Hwan;Ahn, Iee-Ki
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2011.11a
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    • pp.344-347
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    • 2011
  • This paper presents qualification process of the T700/701K turbo-shaft engine for Korean Utility Helicopter(KUH). The T700/701K is the rear-drive variant of the GE's T700-701C/D engine which was qualified for military applications in the world. The main scope of the development is the modification from a front-drive engine to a rear-drive one, the performance enhancement of the power turbine and the incorporation of two channel FADEC(Full Authority Digital Engine Control) system for more reliable operation. Therefore, T700/701K engine must be qualified by Korean government in order to perform a flight in the country. Reflecting the influence of developing scope, the main requirements including performance and control are verified by test and analysis, while the requirement for module or component that is same to that of T700-701C/D are verified by similarity.

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A Study of the Noise Reflection Effect of an Alternator in a 13-liter Turbo-intercooler Diesel Engine (13 리터급 터보.인터쿨러 디젤 엔진의 얼터네이터 소음 반사 효과에 관한 연구)

  • 최성배
    • Journal of Advanced Marine Engineering and Technology
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    • v.27 no.3
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    • pp.381-387
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    • 2003
  • Engine noise consists of the noise radiated from an engine structure and noises from engine ancillaries such as a turbocharger fuel injection system, and alternator. The noise of these ancillaries might be incorrectly evaluated in the aspect of the noise contribution to engine noise because the noise reflection effect of their neighbor engine structure is easily ignored. Consequently, noise source identification should be misled. This study investigates the fact that the engine structure located around an alternator reflects alternator noise, and the reflected noise acts as another alternator noise source in a heavy-duty diesel engine. The result shows that the alternator noise can be correctly estimated in engine noise by properly including the noise reflection effect.

A Numerical Simulation of Flows in an Engine Cooling Passage (엔진 냉각유로 내의 유동에 관한 수치해석)

  • 허남건;윤성영;조원국;김광호
    • Transactions of the Korean Society of Automotive Engineers
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    • v.1 no.1
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    • pp.32-40
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    • 1993
  • Flow fields in model engine cooling passages are studied numerically by using TURBO-3D program, a finite volume based 3-D turbulent flow program adopting a general body fitted coordinate system. The effects of exit position on mass flow rate at each gasket hole are examined for a model cooling passage in order to understand the flow distribution inside the water jacket. The results of the present study can be applied to the design of high performance, high reliability engine.

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Numerical Simulation on Flows inside an Engine Room with Radiator and Cooling Fan Models (방열기 및 냉각팬을 고려한 엔진룸 내부유동 해석)

  • Kim S. L.;Lee S. C.;Lee K. H.;Hur N.
    • 한국전산유체공학회:학술대회논문집
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    • 1995.10a
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    • pp.70-75
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    • 1995
  • Recently, for the thermal system design in an engine room, the importance of the numerical analysis on the heat and fluid flow has been recognized. In the present study, the flow inside an engine room with complex geometry was analysed by use of TURBO-3D program being developed in KIST. Radiator and Cooling fan were simulated by porous media and momentum sources, and the result shows a good agreement with our expectation.

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Professional Engineer Yard: Understanding of Engine Variable Valve Train Technology and Trend (기술사마당: 엔진 가변 밸브 기구 이해 및 개발동향)

  • Kim, Do-Wan
    • Journal of the Korean Professional Engineers Association
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    • v.44 no.4
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    • pp.39-43
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    • 2011
  • To cope with recent high gas prices and global warming phenomenon, the latest gasoline engine technologies are focusing on direction injection, downsizing by turbo charging, variable compression ratio, controlled auto Ignition to enhance fuel efficiency and satisfy emission regulations. The variable valve train technology will be a basement for these innovative technologies in internal combustion engines and is supposed to play a key role to improve low thermal efficiency and pumping loss in gasoline engine caused by low compression ratio and throttled operation respectively.

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An Experimental Analysis for System Optimization to Reduce Smoke at WOT with Low Volatile Fuel on Turbo GDI Engine (저 기화성 연료를 사용한 직접분사식 과급 가솔린엔진에서 전 부하 스모크 저감을 위한 시스템 최적화에 관한 연구)

  • Kim, Dowan;Lee, Sunghwan;Lim, Jongsuk;Lee, Seangwock
    • Transactions of the Korean Society of Automotive Engineers
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    • v.23 no.1
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    • pp.97-104
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    • 2015
  • This study is a part of the high pressure injection system development on the Turbo GDI engine in order to reduce smoke emission in case of using the low volatile(high DI) fuel which is used as normal gasoline fuel in the US market. Firstly, theoretical approach was done regarding gasoline fuel property, performance, definition of particle matters and its creation as well as problems of the high DI fuel. In this experimental study, 2L Turbo GDI engine was selected and optimized system parameter was inspected by changing fuel, fuel injection mode (single/multiple), fuel pressure, distance between injector tip and combustion chamber, start of injection, intake valve timing in engine dyno at all engine speed range with full load. In case of normal gasoline fuel, opacity was contained within 2% in all conditions. On the other hands, in case of low volatile fuel (high DI fuel), it was confirmed that the opacity was rapidly increased above 5,000 rpm at 14.5 ~ 20 MPa of fuel pressure and there were almost no differences on the opacity(smoke) between 17 MPa and 20 MPa fuel pressure. According to the SOI retard, smoke decrease tendency was observed but intake valve close timing change has almost no impact on the smoke level in this area. Consequently, smoke decrease was observed and 16% at 6000rpm respectively with injector washer ring installed. By removing injector washer to make injector tip closer to the combustion chamber, smoke decrease was observed by 46% at 5,500 rpm, 42% at 6,000 rpm. It is assumed that the fuel injection interaction with cylinder head, piston head, intake and exhaust valve is reduced so that impingement is reduced in local area.

Study on the Prediction of Performance and Emission in a 4-Cylinder 4-Stroke Cycle Turbocharged Gasoline Engine (First Paper) (4기통 4사이클 터보과급 가솔린 기관의 성능 및 배기조성 예측에 관한 연구 (제1보))

  • 유병철;이병해;윤건식
    • Journal of the korean Society of Automotive Engineers
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    • v.10 no.6
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    • pp.25-38
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    • 1988
  • As a mean of increasing engine power, great attention has been concentrated on the turbo-charging owing to better fuel economy, smaller engine size and lower emission. The performance in turbocharged engine depends not only on the efficiency of the engine and the turbocharger used, but also on the total characteristics of the system by the matching turbocharger to the engine. The matching of the turbocharger to the engine has been usually accomplished by the empirical techniques with a great deal of laborious work. It would be better to predict the performance and emission in the turbocharged engine using the effective simulation model. In this study, computer simulation program has been developed to predict the transient variation of properties of gas in the cylinder, intake and exhaust pipes, the engine performances and emissions.

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