• 제목/요약/키워드: Rotor performance

검색결과 1,504건 처리시간 0.027초

열회수 냉각 제습기의 이론적 해석 (Theoretical Analysis of a Recuperative Refrigeration Dehumidifier)

  • 김동선
    • 설비공학논문집
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    • 제26권1호
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    • pp.48-54
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    • 2014
  • A refrigeration dehumidifier with a recuperative heat exchanger is theoretically analyzed. The recuperative heat exchanger is located between the two air streams from and to the dehumidifying coil, and reduces the sensible heat load in dehumidification process. A simple model is developed to predict performance of the dehumidifier. The model predicts that the recuperative heat exchanger is effective especially in the low humidity condition, where the sensible heat load is relatively large. It is predicted that, by adopting a recuperative heat exchanger, a maximum 30~110% increase in COP is possible for indoor air at $27^{\circ}C$, and 40~60% relative humidity.

전산유체역학을 이용한 NREL Phase VI 풍력터빈의 축소효과 보정 (Scale Effect Corrections of NREL Phase VI Wind Turbine by Using Computational Fluid Dynamics)

  • 박영민;장병희
    • 신재생에너지
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    • 제3권3호
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    • pp.54-62
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    • 2007
  • The present paper describes the scale effect correction methods for scaled NREL Phase VI wind turbines by using CFD[computational fluid dynamics). For the corrections of wind turbine scale effect, various researches on the helicopter rotor scale effect were investigated and the feasibility study of the methods was performed to correct wind turbine scale effect. The present paper also introduces scale effect correction methods based on two dimensional lift slope. In order to test the present method, performance analyses of NREL Phase VI wind turbines under various scale conditions were carried out and new correction method was applied. Granting that the new correction method is valid only above Reynolds No. 100,000, it showed reasonable agreement between model and full scale wind turbines in the linear torque region.

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풍력발전 계통연계 변압기의 결선에 따른 배전계통의 고장전류에 관한 연구 (A Study on the Fault Current of Distribution System according to Connection of Wind Turbine Generation Grid-Connected Transformer)

  • 안해준;노경수;김현구
    • 한국신재생에너지학회:학술대회논문집
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    • 한국신재생에너지학회 2007년도 추계학술대회 논문집
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    • pp.369-371
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    • 2007
  • This study suggests a modeling of grid-connected wind turbine generation system that has induction generator, and aims to perform simulations for outputs by the variation of actual wind speed and for fault current of wind generation system by the transformer winding connection. This study is implemented by matlab&simulink. The simulation shall be performed by assuming single line to ground fault generated in the system. Generator power, generator rotor speed, generator terminal current and fault current shall be observed following the performance of simulation. The fault current change will be dealt through the simulation results for fault current of wind generation system following the grid-connected transformer winding connection and the simulation result by the transformer neutral ground method.

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MR유체를 이용한 다방향 제진형 마운트의 응답특성 (Response Property of Multi-directional Mount Using Magneto-Rheological Fluid)

  • 안영공;신동춘;양보석;이일영;김동조
    • 한국소음진동공학회논문집
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    • 제13권7호
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    • pp.517-523
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    • 2003
  • This paper presents response property of the squeeze mode type mount using Magneto-Rheological fluid (MR fluid) . The MR mount for the isolation of multi-directional vibrations was constructed in this study. Both the mechanism and shape of the mount are the same as squeeze film dampers for a rotor system. In the present work, the performance of the mount was experimentally Investigated according to the magnetic field strength. The experimental results present that the MR mount can effectively reduce the vibration in a wide range of frequency by controlling the applied electromagnetic filed strength. Viscous damping and stiffness coefficients of the MR mount tend to be changed according to the variation of the applied currents In this study.

저소음 고효율 로터깃 개발에 관한 연구 (Development of Rotor Blade with Low-Noise and High-Efficiency)

  • 신성룡;선효성;이수갑;남찬진;강인준
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2000년도 춘계학술대회논문집
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    • pp.84-90
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    • 2000
  • Integrated tools are developed for the analysis of the aerodynamic performance and aeroacoustics of helicopter rotors. Heli-NK(Helicopter Navier-Stokes & Kirchhoff) code is for hovering and heli-PA(Helicopter Panel & Acoustic analogy) for forward flight. The former showed its ability to predict the hovering efficiency and high-speed impulsive noise level. Thrust calculation, noise levels, and noise directivity patterns are investigated to confirm the availability of the latter. With some proper validation and improvements. these codes will be more useful and practical.

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수력터빈의 압력변동에 의한 로터 진동 (Vibration of the Rotor due to Pressure Fluctuation in a Hydraulic Turbine)

  • 김기섭;김호종;박영하;이욱;전재영
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2000년도 춘계학술대회논문집
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    • pp.1027-1033
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    • 2000
  • This paper describes the characteristics of vibration of a hydraulic turbine mainly due to cavitation occurrence. The analysis of vibration spectra of the turbine shaft shows that hub vortex cavitation occurs in the downstream of the turbine runner, which is verified from coherence analysis between shaft vibration displacement and dynamic pressure at the draft tube. Even though acceleration level measured at the guide vane lever, which is usually used for evaluation of cavitations performance, is decreased during forced aeration, it is found from the analysis of dynamic pressure spectra that cavitation around runner blades still remains unchanged. It is also found that lateral vibration of the turbine shaft is mainly due to the hub vortex cavitation of the turbine runner.

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퍼지 로직 시스템을 이용한 항공기 가스터빈 엔진 오류 검출에 대한 연구 (Fault Diagnosis in Gas Turbine Engine Using Fuzzy Inference Logic)

  • 모은종;지민석;김진수;이강웅
    • 제어로봇시스템학회논문지
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    • 제14권1호
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    • pp.49-53
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    • 2008
  • A fuzzy inference logic system is proposed for gas turbine engine fault isolation. The gas path measurements used for fault isolation are exhaust gas temperature, low and high rotor speed, and fuel flow. The fuzzy inference logic uses rules developed from a model of performance influence coefficients to isolate engine faults while accounting for uncertainty in gas path measurements. Inputs to the fuzzy inference logic system are measurement deviations of gas path parameters which are transferred directly from the ECM(Engine Control Monitoring) program and outputs are engine module faults. The proposed fuzzy inference logic system is tested using simulated data developed from the ECM trend plot reports and the results show that the proposed fuzzy inference logic system isolates module faults with high accuracy rate in the environment of high level of uncertainty.

Nonlinear Observer-based Control of Synchronous Machine Drive System

  • Sundrica, Marijo;Erceg, Igor;Maljkovic, Zlatko
    • Journal of Electrical Engineering and Technology
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    • 제10권3호
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    • pp.1035-1047
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    • 2015
  • Starting from a new dynamic system description novel synchronous machine deterministic observers are proposed. Reduced and full order adaptive observer variations are presented. Based on the feedback linearization control law and the use of deterministic observer a novel control system is built. It meets the requirements of high performance tracking system. Adaptivity to stator and rotor resistance and the torque sensorless application is included. The comparison of the proposed novel control with conventional linear and nonlinear control systems is discussed. The given simulational study includes complete drive system integration.

스큐를 고려한 다극 영구자석 발전기의 전자기 특성해석/제어정수 도출을 통한 발전특성 예측 및 실험적 검증 (Experimental Verification and Prediction of Generating Performance of PMG with Multi-Pole Rotor based on Electromagnetic Analysis and Parameter Estimation considering Skew Effects)

  • 장석명;최장영;고경진;박지훈;이성호;김일중
    • 대한전기학회:학술대회논문집
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    • 대한전기학회 2008년도 제39회 하계학술대회
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    • pp.752-753
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    • 2008
  • The analytical expressions for magnetic field distributions considering slotting effects, cogging torque and back-emf considering skew effects are established. On the basis of magnetic field solutions, electrical parameters such as back-emf constant and winding inductance are obtained. The predicted results are validated extensively by non-linear finite element (FE) analyses. In particular, test results such as back-emf, cogging torque, inductance and resistance measurements are given to confirm the analyses. Finally, generating performances are investigated by applying estimated parameters to equivalent circuit (EC) of the permanent magnet generator (PMG) and validated extensively by FE calculations and measurements.

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스마트무인기 축소형 비행체 개발 (Development of the Scaled Vehicle of Smart UAV)

  • 장성호;최성욱;구삼옥
    • 항공우주기술
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    • 제6권2호
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    • pp.236-244
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    • 2007
  • 스마트무인기의 기본 비행성능 파악과 비행제어 알고리즘의 검증을 위하여 40% 축소형 비행체를 개발하였다. 축소형 비행체는 실물기와 유사한 형태의 짐발 허브와 드라이브 장치를 채택하였으며 강제 공랭 방식의 왕복엔진을 장착하였다. 축소형 비행체 주요 부품에 대한 다양한 시험을 수행하였고 조립된 축소형 비행체의 지상시험 및 호버링 시험을 통하여 주요 성능과 기계적 내구성을 확인하였다.

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