• Title/Summary/Keyword: Pipe roughness improvement

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The improvement of surface roughness of cast-iron pipe (주철관의 표면조도 개선)

  • Park, Seong-Yoo;Park, Myung-Ho;Kim, Sung-Joon
    • Transactions of the Korean Society of Mechanical Engineers A
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    • v.21 no.9
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    • pp.1491-1497
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    • 1997
  • The purpose of this research is to improve the surface roughness of cast-iron pipe porduced by the centrifugal casting. A twin-fluid atomizer of mold-wash slurry is designed for this project. New atomizer is equipped with the existing manufacturing facility to produce pipes. Cast-iron pipes (.cent.125*L3000mm) are produced and the surface roughnesses of those are analysed by UBM. The average surface roughness of new products is 6.7.mu.m while the old products of sand-resin coating method have 17.0.mu.m of average surface roughness. The surface roughness of cast-iron pipe is improved very much than before.

Analysis of Rainfall-Runoff Characteristics by Improvements to the Roughness Coefficient in a Storm Sewer System (우수관거 조도계수 개선에 따른 강우-유출 특성 분석)

  • Kim, Eung-Seok;Jo, Deok-Jun;Yoon, Ki-Yong
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.18 no.1
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    • pp.282-286
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    • 2017
  • Rapid industrialization and urbanization have resulted in an increase in impervious areas and an increase in runoff, therefore, this causes more flooding and damage in urban areas. This study has analyzed the effects of improvements to the roughness coefficient in storm sewer pipes on flood runoff and outflow through rainfall-runoff simulations. The simulations are implemented by three scenarios to evaluate effects of improvements to the roughness coefficient for the improved length ratio to the total length, diameters and mainlines of sewer pipes. The size and length of the sewer mains are large and long to effectively increase the flow rate to the outlet, secure the passage discharge capacity of the pipe and reduce the overflow. It is effective for flood reduction that the improvement to roughness coefficient is first conducted in mainlines with longer lengths and larger diameters. The results from this study can provide a guideline for prioritizing of the sewer pipe replacement.

Improvement of Manufacturing Process for Fuel Oil Supply Pipe using Large Vessel (대형선박용 연료공급관 가공공정 개선)

  • Jeon, Eon-Chan;Han, Min-Sik;Kim, Nam-Hun;Min, Jung-Oh
    • Journal of the Korean Society of Manufacturing Process Engineers
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    • v.9 no.5
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    • pp.64-69
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    • 2010
  • This study is the machining of fuel supply pipe used in large vessels. The fuel supply pipe of large vessels have effects to reduce engine exhaust because of common rail system and show excellent fuel efficiency so it is in the limelight as a vessel engine of next generation. At present, the shape of fuel supply pipe of common rail used for huge two-stroke & low-speed vessels is like a peanut hole so the second machining is necessary after the first machining. There is high error rate for machining and the materials waste caused by machining error is serious. Also, in this time the request for increasing the length of fuel supply pipe is suggested in the world market, it's judged that current methods will show higher error rate for machining. Therefore, the purpose of this study is to improve the machining process used originally. For that, the system controlling the process was developed as well as surface roughness and straightness which are evaluation items of fuel supply pipe were measured so that improved process can be observed in real time.

Analysis of Bearing Capacity Improvement Effect of Inner Cone Penetration Equiped Open-Ended Steel Pipe Pile (개단 강관말뚝 내부 콘항타에 의한 지지력 증대효과 분석)

  • Lee, Junho;Ji, Su-Bin;Lee, Kicheol;Kim, Dongwook
    • Journal of the Korean Geosynthetics Society
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    • v.16 no.2
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    • pp.67-77
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    • 2017
  • This study analyzes behavior of bearing capacity of open-ended pipe pile from laboratory experiment results. Unlike the conventional pipe piles, cone penetration is implemented into the inside of the pipe pile. During the cone penetration, cone driving energy helps densification of plugged soils and soils below the pile end. Sand pluviator was used to obtain homogeneous soil layers. Two kinds of piles with different pile outer surface roughness were prepared, and two different drop heights of pile driving were applied. Eight experimental cases varying pile outer surface roughness, pile driving energy for conventional and cone penetration implemented piles were conducted. From the experiments, ultimate load of the pile increased approximately by 70% for increased pile driving height, and it increased by 21% for rougher surface pile. When cone penetration is implemented, the ultimate load increased by 40% in average.

A Study on the Characteristics of Internal-Face Magnetic Abrasive Finishing for Titanium Pipe (타이타늄 파이프의 내면 자기연마 가공에 관한 연구)

  • Li, Li-Hai;Mun, Sang-Don;Kim, Young-Whan;Park, Won-Ki;Yang, Gyun-Eui
    • Journal of the Korean Society for Precision Engineering
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    • v.28 no.6
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    • pp.701-708
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    • 2011
  • Although Titanium material has superior properties, it belongs to difficult-to-machine materials. The present research applies magnetic abrasive finishing to precision machining of internal-face of titanium pipes, and analyzed & assessed the influence of grinding conditions on magnetic abrasive effects through the removed amount and surface roughness of materials. There was the influence on grinding properties according to change of rotational speed, a total input of mixed powder and an input of grinding liquid, and when the total input, rotational speed and ratio of electrolytic iron versus magnetic abrasives are 8g and 1000rpm, it was most advantageous in aspects of surface roughness and material removal amount, and the grinding liquid remarkably improved the surface roughness and material removal amount only with addition of trace amounts of light oil rather than dry machining conditions. And a result of considering the influence on grinding properties by using an inert gas (Argon gas) for improving grinding properties of the internal-face of titanium pipe, the present research has obtained improvement effects in the removal amount and surface roughness through utilization of an inert gas.

A study on the effects of Friction loss of CPVC pipe according to Roughness coefficient in a sprinkler system (스프링클러 시스템에서 조도계수에 따른 CPVC 배관 마찰손실 영향의 연구)

  • Kang, Ung Il
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.17 no.11
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    • pp.355-362
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    • 2016
  • The pipe material is selected according to the physical and chemical properties of the fluid flowing within it. Because the fluid used in fire extinguish systems is water, the various foreign substances dissolved in it cause scale to form on the pipe wall and accelerate the corrosion and aging of the pipe itself. This results in an increase in the friction loss and eventually degrades the efficiency of the pump. The use of CPVC (Chlorinated Poly-Vinyl Chloride) pipes was confirmed to reduce the friction loss compared to conventional steel pipes in the design and construction stages. The friction loss was found to be 76.64MPa with a C-value of 120 for the steel pipe and 50.72 MPa with a C-value of 150 for the CPVC pipe in an actual apartment construction environment. It was confirmed that the friction loss was improved by about 34% when using the CPVC pipe. When the steel and CPVC pipes were employed in the construction, the construction costs were 1,585,158 and 931,842 won, respectively. Therefore, it was shown that the construction cost was reduced by about 41%. We investigated the safety of the fire extinguishing system and the improvement in the economic performance due to the reduction in the total installed capacity by studying practical applications in the field.