• Title/Summary/Keyword: Nozzle Pressure

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Design and Development of High Altitude Test Facility for Kick Motor (고공환경모사 시험설비 설계/개발)

  • Ryu, Jung-Hun;Lee, Jun-Ho;Suh, Hyuk;Jang, Ki-Won;Kim, Yong-Wook;Oh, Seung-Hyub
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2008.11a
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    • pp.403-404
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    • 2008
  • The 2nd stage Kick Motor under the national aerospace middle and long term plan operates over the height of 300Km. Rocket Motors, designed for operation in high altitude, need nozzles with large expansion ratio to improve thrust efficiency. Hence, to evaluate the performance of such rocket motors on the ground, similar low pressure with the operating condition has to be made for the ground test to prevent flow separation in the nozzle. This study is for the installation of the high altitude test facility and test result for Kick Motor.

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Mass flow rate of Knudsen pump According to Membrane Type for Micro Propulsion Applications (초소형 추진장치에 적용을 위한 누센펌프의 멤브레인 종류에 따른 질유량 특성)

  • Kim, Hye-Hwan;Huh, Hwan-Il
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2008.11a
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    • pp.36-40
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    • 2008
  • Minimization of nozzle induces many flow losses in micro-propulsion system. In this study, we studied about thermal transpiration based new conceptual micro propulsion system to overcome these losses. Thermal transpiration device(Knudsen pump) having no moving parts can self-pump the gaseous propellant by temperature gradient only (cold to hot). We designed, fabricated the knudsen pump and analyzed pressure gradient efficiency of membrane according to Knudsen number under vacuum condition. In this paper, we compared mass flow rate of Knudsen pump by using different membrane type ; Polyimide and Hangi, Korean traditional paper.

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Design and Fabrication of Technology Demonstration Model of 75 tonf Regenerative Cooling Thrust Chamber (75톤급 재생냉각 연소기 기술검증용 시제 설계 및 제작)

  • Kim, Jong-Gyu;Ahn, Kyu-Bok;Lim, Byoung-Jik;Kim, Mun-Ki;Kang, Dong-Hyuk;Choi, Hwan-Seok
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2011.04a
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    • pp.31-34
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    • 2011
  • Design and fabrication of Technology Demonstration Model(TDM) of 75 tonf regenerative cooling thrust chamber were described. It has design chamber pressure of 60 bar, propellant mass flow rate of 243.6 kg/s, and nozzle expansion ratio of 12. It has a single welded structure of the mixing head and the chamber. Design and fabrication technologies established through this TDM can be used to development of flight model.

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Conceptual Design of Thrust Chamber for 7 tonf-class Liquid Rocket Engine (7톤급 액체로켓엔진 연소기 개념설계)

  • Kim, Jong-Gyu;Ahn, Kyu-Bok;Joh, Mi-Ok;Choi, Hwan-Seok
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2012.05a
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    • pp.454-456
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    • 2012
  • Conceptual design results of a thrust chamber for a 7 tonf-class liquid rocket engine of KSLV-II 3rd stage were described. The engine system for KSLV-II 3rd stage is pump-fed system, the thrust chamber has vacuum thrust of 6.9 tonf, vacuum specific impulse of 336.9 sec, chamber pressure of 70 bar, nozzle expansion ratio of 94.5, total propellant mass flow rate of 20.5 kg/s, mixture ratio(O/F) of 2.45. The thrust chamber consists of mixing head with 90 coaxial swirl injectors and regeneratively combustion chamber cooled by kerosene.

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A Numerical Study on the Control of the Gap Flow Using a Fluid Supply Device (유체 공급장치를 활용한 간극유동 제어에 관한 수치적 연구)

  • Seo, Dae-Won;Oh, Jung-Keun;Lee, Seung-Hee
    • Journal of the Society of Naval Architects of Korea
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    • v.46 no.6
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    • pp.578-586
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    • 2009
  • Recently, horn-type rudders are generally being used at high speed container ships and are frequently suffering from the cavitation occurs on the rudder surface in the vicinity of the gap between the horn and rudder plate. In the present study, a fluid supplying device is employed as to decrease the gap cavitation of the horn-type rudder. The device is devised to inject the water against the pressure side through the nozzle installed inside of the gap to control the gap flow. Numerical calculations are performed to investigate the effectiveness of the device and the results show that the device can noticeably reduce the gap cavitation. The rates of water injection for achievement of the maximum retardations of gap flow are also sought.

An Experimental Study on Wafer Demounting by Water Jet in a Waxless Silicon Wafer Mounting System

  • Kim, Kyoung-Jin;Kwak, Ho-Sang;Park, Kyoung-Seok
    • Journal of the Semiconductor & Display Technology
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    • v.8 no.2
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    • pp.31-35
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    • 2009
  • In the silicon wafer polishing process, the mounting stage of silicon wafer on the ceramic carrier block has been using the polishing template which utilizes the porous surface instead of traditional wax mounting method. Here in this article, the experimental study is carried out in order to study the wafer demounting by water jet and the effects of operating conditions such as the water jet flowrate and the number of water jet nozzles on the wafer demounting time. It is found that the measured wafer demounting time is inversely proportional to the water flowrate per nozzle, regardless of number of nozzles used; implying that the stagnation pressure by the water jet impingement is the dominant key factor. Additionally, by using the transparent disk instead of wafer, the air bubble formation and growth is observed under the disk, making the passage of water flow, and subsequently demounting the wafer from the porous pad.

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Development of a Lightweight Prediction Model of Fuel Injection Rates from High Pressure Fuel Injectors (고압 인젝터의 분사율 예측을 위한 경량 모델 개발)

  • Lee, Sanggwon;Bae, Gyuhan;Atac, Omer Faruk;Moon, Seoksu;Kang, Jinsuk
    • Journal of ILASS-Korea
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    • v.25 no.4
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    • pp.188-195
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    • 2020
  • To meet stringent emission regulations of automotive engines, fuel injection control techniques have advanced based on reliable and fast computing prediction models. This study aims to develop a reliable lightweight prediction model of fuel injection rates using a small number of input parameters and based on simple fluid dynamic theories. The prediction model uses the geometry of the injector nozzle, needle motion data, injection conditions and the fuel properties. A commercial diesel injector and US No. 2 diesel were used as the test injector and fuel, respectively. The needle motion data were measured using X-ray phase-contrast imaging technique under various fuel injection pressures and injection pulse durations. The actual injector rate profiles were measured using an injection rate meter for the validation of the model prediction results. In the case of long injection durations with the steady-state operation, the model prediction results showed over 99 % consistency with the measurement results. However, in the case of short injection cases with the transient operation, the prediction model overestimated the injection rate that needs to be further improved.

Effects of Ultrasonic Standing Wave on the Ultrasonically-atomized Aerosol Flame Injected through a Slit-jet Nozzle (Slit-jet 노즐을 통과한 초음파 무화 에어로졸 화염에 정상초음파가 미치는 영향)

  • Ahn, Hyun Jong;Kang, Yun Hyeong;Kim, Jeong Soo
    • Journal of the Korean Society of Propulsion Engineers
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    • v.24 no.6
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    • pp.53-60
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    • 2020
  • In liquid-fuel spray combustion, an experimental study was conducted to observe the effect of ultrasonic excitation on the ultrasonically-atomized liquid fuel flame by controlling pressure field through an ultrasonic standing wave. Flame of the ultrasonically-atomized kerosene aerosol was visualized by using a high speed camera, DSLR, and Schlieren photography. The amount of fuel consumed was obtained by a precise flow-rate measurement technique during combustion, through which the ratio of carrier gas (air) to fuel mass was able to be obtained, too. As a result, it could be found that the combustion reaction-rate of the liquid-fuel aerosol was increased by applying an ultrasonic standing wave to the secondary flame zone of the flame.

Simplified elastic-plastic analysis procedure for strain-based fatigue assessment of nuclear safety class 1 components under severe seismic loads

  • Kim, Jong-Sung;Kim, Jun-Young
    • Nuclear Engineering and Technology
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    • v.52 no.12
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    • pp.2918-2927
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    • 2020
  • This paper proposes a simplified elastic-plastic analysis procedure using the penalty factors presented in the Code Case N-779 for strain-based fatigue assessment of nuclear safety class 1 components under severe seismic loads such as safety shutdown earthquake and beyond design-basis earthquake. First, a simplified elastic-plastic analysis procedure for strain-based fatigue assessment of nuclear safety class 1 components under the severe seismic loads was proposed based on the analysis result for the simplified elastic-plastic analysis procedure in the Code Case N-779 and the stress categories corresponding to normal operation and seismic loads. Second, total strain amplitude was calculated directly by performing finite element cyclic elastic-plastic seismic analysis for a hot leg nozzle in pressurizer surge line subject to combined loading including deadweight, pressure, seismic inertia load, and seismic anchor motion, as well as was derived indirectly by applying the proposed analysis procedure to the finite element elastic stress analysis result for each load. Third, strain-based fatigue assessment was implemented by applying the strain-based fatigue acceptance criteria in the ASME B&PV Code, Sec. III, Subsec. NB, Article NB-3200 and by using the total strain amplitude values calculated. Last, the total strain amplitude and the fatigue assessment result corresponding to the simplified elastic-plastic analysis were compared with those using the finite element elastic-plastic seismic analysis results. As a result of the comparison, it was identified that the proposed analysis procedure can derive reasonable and conservative results.

A Study on the Development and Application of an Automatic Injection Type Lubrication System for the Cleaning of the Line Switching Part (선로전환부 청결을 위한 자동 분사형 윤활시스템 개발에 관한 연구)

  • In-Chul Lee;You-Shin Lee
    • Journal of the Korean Society of Industry Convergence
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    • v.26 no.3
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    • pp.455-462
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    • 2023
  • In this study, an automatic spraying lubrication system was developed to maintain the cleanliness of the switchgear when detecting the movement of the track through the switchgear. To develop this system, an air tank, valve block, and spray nozzle were designed, and the safety was secured through the pressure test of the prototype after designing the air tank. Furthermore, the environmental aspect was considered by minimizing the use of lubricant by enabling the mixing of air and lubricant through the production of a valve using the Venturi principle. The performance evaluation was conducted by implementing (producing) the injection system, and the product developed in this study was deemed installable in actual switchgear. It is expected that the proposed system will enable the maintenance of the cleanliness of the track during switching and reduce faults and malfunctions caused by switchgear defects.