• Title/Summary/Keyword: Motor rpm

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A study on the Development of Micro Hole Drilling Machine and its Mechanism (미소경 드릴링 머신의 개발과 절삭현상의 연구)

  • Paik, In-Hwan;Chung, Woo-Seop
    • Journal of the Korean Society for Precision Engineering
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    • v.12 no.1
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    • pp.22-28
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    • 1995
  • Micro Drills have found ever wider application. However micro drilling is a machining to integrate the difficult machinablities such as tool stiffness, position control and revolution accuracy, and is known to cost and time consuming. So, this study aimed to practice ultraminiature drilling(0.05 .phi. ) wiht simple component, if possible. System is developed as the three modules : feed drives, spindle and monitoring part. The dynamics of measured current signals from the spindle of Micro Hole Drilling machine are investigated to establish the criteria of stepfeed mechanism. Cutting experiments identify the relationship of spindle rpm, feed rate and tool life. The smaller drill diameter is, the more suitable cutting condition have to be selected because of chip packing.

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The Study of the Design and Control for the Hydrogen Recirculation Blower Noise and Vibration Reduction (수소 재순환 블로어 소음 진동 저감을 위한 설계 및 제어에 관한 연구)

  • Bae, Ho June;Ban, Hyeon Seok;Noh, Yong Gyu;Jang, Seok Yeong;Lee, Hyun Joon;Kim, Chi Myung;Park, Yong Sun
    • Journal of Hydrogen and New Energy
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    • v.25 no.5
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    • pp.509-515
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    • 2014
  • At the fuel processing system (FPS) of fuel cell vehicle, hydrogen recirculation blower (HRB) is used for the recirculation of remained hydrogen after reaction. In this paper, noise and vibration improvement of HRB is studied by changing design and control. It is checked the campbell diagram and critical speed for stability of rotor, and housing stiffness is improved using simulation of frequency response function (FRF). A method is suggested that can decrease the unbalance amount of the rotor and impeller which main source of noise and vibration. In order to reduce the noise during deceleration of blower, electrical braking is applied and tested the risk impact of durability. Founded the optimum switching frequency of the motor control, and reduced the idle rpm by increasing of aerodynamic performance. The superiority of paper is proved by measurement of the improved product's noise and vibration.

Study on the Electromagnetic Excitation System for the Measurement of Dynamic Coefficients of Air Foil Bearing for High Speed Rotor (초고속 회전체용 공기 포일 베어링의 동특성 계수 측정을 위한 전자석 가진장치에 관한 연구)

  • Park, Cheol-Hoon;Choi, Sang-Kyu;Ham, Sang-Yong
    • The KSFM Journal of Fluid Machinery
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    • v.16 no.3
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    • pp.18-25
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    • 2013
  • Recently the requirement of long-term mobile energy source for mobile robot or small-sized unmanned vehicle is highly increased, and the micro turbine generator(MTG) which is known to have high energy and power density is under development. MTG is designed to have air foil bearing and high speed rotor of which operating speed is 400,000rpm. In the development stage of high speed rotor and bearing, stability analysis for the full operational speed range is essential and the dynamic coefficients such as stiffness and damping coefficients of bearing depending on the rotational speed are required for that. Although perturbation method is usually used to identify the dynamic coefficients, it's not easy to give the perturbation to the high speed rotating rotor. In this study, we present the dynamic coefficients measurement system for air foil bearing which consists of electromagnets, gap sensors, high speed motor and controller. This measurement system can exert the sine sweep force to the rotor-bearing, measure the displacement of rotor and get FRF(Frequency response function) of rotor-bearing. The least square estimation method is applied to identify the dynamic coefficients of bearing from the measured frequency response at the different rpm and the identified dynamic coefficients for the wide rotational speed range are presented.

A Basic Experimental Study on Performance of Proton Exchange Membrane Fuel Cell System for Vehicle (PEM 연료전지 자동차 적용을 위한 성능실험에 관한 기초연구)

  • Lee, Hyun-kun;Oh, Byeong-soo;Jeong, Kwiseong
    • Journal of Hydrogen and New Energy
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    • v.11 no.3
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    • pp.137-147
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    • 2000
  • Not only study of fuel cell performance but study of fuel cell application is very important, therefore these studies were paralleled together for the commercialization of exciting power generation. The objective of this study is to determine the characteristics of shaft power and efficiency as a function of rpm and to compare natural convection air method to forced air method. From these results, performance of forced air was better than that of natural convection air because it enables to improve mass transportation by increasing air flow rate. With decreasing shaft power, efficiency of fuel cell decreases remarkably because dc motor drives at the low range of efficiency. Fuel cell powered vehicle has to be driven considering efficiency and shaft power. It should be driven at 35-45% of efficiency and 0.55-0.75v/cell.

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Design and experiment with a plastic mulch wrapper using a hydraulic system

  • Park, Hyo Je;Lee, Sang Yoon;Park, Yong Hyun;Kim, Young Keun;Choi, Il Su;Nam, Young Jo;Kweon, Gi Young
    • Korean Journal of Agricultural Science
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    • v.47 no.1
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    • pp.43-58
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    • 2020
  • Mulching plastic is used for the purpose of maintaining soil temperature, moisture, and weed and pest prevention in agriculture. Any remaining plastic after use may contaminate the soil and damage crop growth. To solve this problem, mulching plastic wrappers have been studied and developed, but the actual use rate is quite low due to their poor performance and frequent tearing of the plastic on the field. In this study, we developed a tractor attachable mulching plastic wrapper to minimize the tearing of the mulched plastic. The developed mulching plastic wrapper consists of hydraulic motors and pumps, valves, a microcontroller, and sensors. The collecting speed of the plastic mulch was calculated considering the tractor's travel speed and the radius of the collecting drum. A proportional controller was designed to control the rotating speed of the hydraulic motor as the plastic was wound around the collection drum and the radius increased. The performance of an indoor experiment was quite promising because the difference between the collecting speed predicted by the calculation and the actual collecting speed was 2.71 rpm. Based on a field verification test, the speed difference was max. 14.28 rpm; thus, the, proportional integral derivative (PID) controller needs to be considered to control the drum speed precisely. Another issue was found when the soil covered at the edge of the plastic was hardened or the road surface was uneven, the speed control was unstable, and the plastic was torn. In future research, vibrational plows will be equipped to break-up the harden soil for collecting the plastic smoothly.

Development and Performance Test of a Spherical Reaction Wheel Actuator with Magnetic Levitation (자기부상을 적용한 구체 반작용휠 구동기 개발 및 성능 시험)

  • Kim, Dae-Kwan;Yoon, Hyung-Joo;Kim, Yong-Bok;Kang, Woo-Yong;Choi, Hong-Taek
    • Journal of Advanced Navigation Technology
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    • v.16 no.5
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    • pp.731-737
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    • 2012
  • In the present study, a feasibility study on an innovative satellite attitude control actuator is performed. The actuator is specially designed to generate the reaction torque in an arbitrary axis, so that a satellite attitude can be controlled by using itself. It consists of a spherical flywheel and electromagnets for levitation and rotation control of the ball. As the earlier study, a rotating performance test on the spherical actuator is conducted in a single rotating axis and vertical levitation condition. From the test results, it can be confirmed that the maximum speed and torque of the innovative device are 7,200rpm and 0.7Nm, respectively. Using a velocity-voltage characteristic curve of the spherical motor, an open-loop control (V/f constant control) is performed, and the test results show excellent control performance in acceleration and deceleration phases.

Design of Stiffeners for Reducing Resonant Vibration of Large Vertical Pumps and Its Performance Verification (대형 입형펌프 운전 중 공진현상의 진동 저감을 위한 스티프너 설계 및 성능 검증)

  • Ryu, Kil-Su;Bong, Suk-Keun;Han, Seung-Woo;Roh, Cheol-Woo;Lee, Dong-Min;Lee, Jung-Woo;Park, Junhong
    • Transactions of the Korean Society for Noise and Vibration Engineering
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    • v.23 no.1
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    • pp.65-72
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    • 2013
  • This case study presents a practical method to reduce resonant vibration of large vertical pumps. The pumps are driven at 400 rpm rated speed by induction motor. The vibration was not significantly large when operated at this rated speed. Large vibration was occurred when the pump was operated below the rated speed for flow control. Due to the large vibration resonance, variable speed operation of the pump was not possible for several months at worst cases. To find an efficient vibration control method, the flexural responses of pumps for both normal and transient operations were measured. The measured modal characteristics were compared with those of finite element analysis. When the pump was operated at a specific rpm, the natural mode whose resonance frequency is twice the rotating angular speed induced the large vibration. The retrofit utilizing stiffeners to reduce this resonant vibration were performed. Effects of designed stiffeners on reducing vibration were validated through tests after actual installation.

Experimental Study on the Load Carrying Performance and Driving Torque of Gas Foil Thrust Bearings (가스 포일 스러스트 베어링의 하중지지 성능 및 구동 토크에 관한 실험적 연구)

  • Kim, Tae Ho;Lee, Tae Won;Park, Moon Sung;Park, Jungmin;Kim, Jinsung;Jeong, Jinhee
    • Tribology and Lubricants
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    • v.31 no.4
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    • pp.141-147
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    • 2015
  • Gas foil thrust bearings (GFTBs) have attractive advantages over rolling element bearings and oil film thrust bearings, such as oil-free operation, high speed stability, and high-temperature operation. However, GFTBs have lower load carrying capacity than the other two types of bearings owing to the inherent low gas viscosity. The load carrying capacity of GFTBs depends mainly on the compliance of the foil structure and the formed hydrodynamic wedge, where the gas pressure field is generated between the top foil and the thrust runner. The load carrying capacity of the GFTBs is very important for the suitable design of oil-free turbomachinery with high performance. The aim of the present study is to identify the characteristics of the load carrying performance of GFTBs. A new test rig for the experimental measurements is designed to provide static loads up to 800 N using a pneumatic cylinder. The maximum operating speed of the driving motor is 30,000 rpm. A series of experimental tests—lift-off test, static load performance test, and maximum load capacity test—estimate the performance of a six-pad GFTB, in terms of the static load, driving torque, and temperature. The maximum load capacity is determined by increasing the static load until the driving torque rises suddenly with a sharp peak. The test results show that the torque and temperature increase linearly with the static load. The estimated maximum load capacity per unit area is approximately 80.5 kPa at a rotor speed of 25,000 rpm. The test results can be used as a design guideline for GFTBs for realizing oil-free turbomachinery.

Developed a test rig for studying the hover performance of a coaxial propeller (동축반전 프로펠러의 제자리 비행 성능연구를 위한 시험장치 개발)

  • Song, Youn-Ha;Song, Jae-Rim;Kim, Deog-Kowan
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2017.05a
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    • pp.560-562
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    • 2017
  • This paper presents the development and test results of a test rig for confirming the hover performance of the coaxial propeller which is applied to the drone in order to carry out the mission that requires high payload such as the development of the courier drones. the performance of each propeller was measured by varying the thrust and torque according to the H/D ratio. the Thrust sensor and torque sensor were used to measure the thrust and torque generated when the propeller rotated, and a photo sensor was used to measure the rpm. it used the data acquisition system to acquire data from each sensor, and used the Labview softwaer to control data storage, monitoring and BLDC motor control. In the test, each propeller meansured the figure of mefit according to the chansge of the interval at the same rpm.

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Evaluation of Structural Safety of Linear Actuator for Flap Control of Aircraft (항공기 플랩 제어를 위한 선형 구동기의 구조 안전성 평가)

  • Kim, Dong-Hyeop;Kim, Sang-Woo
    • Journal of Aerospace System Engineering
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    • v.13 no.4
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    • pp.66-73
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    • 2019
  • The objective of this study was to evaluate the structural safety of the basic design for the linear actuator for the flap control of aircrafts. The kinetic behavior of the linear actuator was determined using the multi-body dynamics (MBD) analysis, and the contact force was calculated to be used as input data for the structural analysis based on the finite element analysis. In the structural analysis, the thermal and static behaviors of the linear actuator satisfying the designed velocity were examined, and the structural safety of the linear actuator evaluated. Moreover, the dynamic behaviors of the key components of the linear actuator were investigated by the modal analysis. The actuation rod linearly moved with about 5 mm/s when the motor operated at 225 rpm and the maximum contact force of 32.83 N occurred between two driving gears. Meanwhile, the structural analysis revealed that the maximum thermal and static stresses were 1.57% and 78% of the yield strength of steel, respectively, and they were in a safe range of the structure. In addition, the linear actuator for the basic design is stable to the resonance by avoiding the natural frequencies of the components.