• 제목/요약/키워드: Heating pipe

검색결과 344건 처리시간 0.034초

보일러 운전조건 및 마감층 두께 변화에 따른 온돌난방공간의 열특성에 관한 실험연구 (An experimental study on the heat transfer characteristics of a Ondol-heated space by varying pipe embedding depths and hot water supply conditions)

  • 박병윤
    • 한국주거학회:학술대회논문집
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    • 한국주거학회 1991년도 학술발표대회논문집
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    • pp.41-47
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    • 1991
  • This study reports the results of the transient temperature response of a floor heating panel according to variation of the hot water supply temperature and the pipe embedding depth. Also, this experiment compares the temperature responses of floor heating panels under the continuous and intermittent heating system. Furtthermore, this study presents some details of the thermal response of Ondol-heated buildings to varying loads and patterns of heat input. The analysis of the thermal performance fo Ondol heating system have been presented.

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난류발생기를 가지는 원형 파이프내에서의 마찰저감 및 열전달율에 관한 실험적 연구 (Experimental Study on the Drag Reduction & Heat Transfer Ratio in the Circular Pipe with Swirl Generater)

  • 김성수;조성환;윤석만
    • 대한설비공학회:학술대회논문집
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    • 대한설비공학회 2008년도 하계학술발표대회 논문집
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    • pp.430-435
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    • 2008
  • Total lengths of domestic pipe network for district heating system are above about 2,500Km. A lots of pumping power for heat transportation through long pipe are required by the flow friction of pipe surface. Until now there have been considered about various methods to reduce the flow friction for district heating system such as using surfactants and turbulence promoters by swirl flow and baffles etc. At this study, swirl flow generator was tested about the possibility to increase the heat transfer ratio at the heat exchanger in the case which the suppling water temperature increased from $50^{\circ}C$ until $120^{\circ}C$. Experimental results showed that the heat transfer ratio increased and also pressure increase ratio increased simultaneously in the case which swirl flow generator installed. The amount of the increasing ratio for heat transfer and pressure were reached until 4.33% and 11% at the case of $120^{\circ}C$ suppling temperature which domestic district heating system were using.

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전열밀폐식 X-L 파이프 보일러 난방장치의 특성 및 경제성 평가 (Evaluation on Characteristics and Economical Efficiency of X-L Pipe Boiler with Electric Heat Closed Type)

  • 김수만;전태규;양영준
    • 에너지공학
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    • 제20권4호
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    • pp.330-337
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    • 2011
  • 난방장치로서 통상 가스 및 기름보일러가 많이 사용되어진다. 본 연구는 기존의 가스 및 기름 보일러에 의한 난방방식과 달리 밀폐된 X-L 파이프 내에 특수 제작된 전열선을 삽입하여 그 전열선에 전압을 인가함으로써 X-L 파이프 내 열매체의 온도를 상승시켜 난방하는 방법에 관한 것이다. 특수 제작된 전열선의 가닥수와 인가전압을 변화시켜 X-L 파이프 보일러의 특성과 발열 메카니즘을 파악하였다. 또한 X-L 파이프 보일러와 가스 및 기름보일러와의 난방비용을 객관적인 자료에 근거하여 서로 비교를 함으로써 그 경제성을 평가하였다. 그 결과 X-L 파이프 보일러는 기름(보일러등유)보일러의 28%, 가스(천연가스)보일러의 58%의 비용으로 난방이 가능함을 확인하였다.

냉난방용 배관 용접부의 전기화학적 부식특성에 관한 연구 (A Study on Characteristics of the Electrochemical Corrosion of Weld Zone for Refrigerating and Heating Systems Pipe)

  • 임우조;윤병두;김환식
    • 수산해양교육연구
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    • 제19권1호
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    • pp.84-90
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    • 2007
  • This paper was studied on the electrochemical corrosion characteristics of weld zone for refrigerating and heating systems pipe. Austenitic stainless steel is widely applied to various fields of industry, because it is good to corrosion resistance and mechanical properties. But STS 304 is reliable to sensitization by heat cycle on welding. Therefore, in this study, electrochemical polarization test of STS 304 steel pipe manufactured by arc welding in tap water was carried out. And then polarization resistance behavior, uniform and local corrosion behaviors of base metal(BM), weld metal(WM) and heat affected zone(HAZ) for STS 304 pipe were investigated. The corrosion current density of STS 304 steel pipe is high in order of BM(153nA/cm2) < WM(614nA/cm2) < HAZ ($1.675{\mu}A/cm2$). The pitting potential of HAZ(238mV/SCE) for STS 304 is lower than BM(1206mV/SCE) and WM(369mV/SCE). Therefore, the local corrosion like pitting corrosion, galvanic corrosion and crevice corrosion of HAZ for STS 304 is more sensitive than BM and WM.

공동주택 바닥용 시멘트 모르타르의 복합강화법 변화에 따른 열전도 특성 (Properties of Thermal Conductivity of Cement Mortar for Apartment Housing Floor Using Combined Strengthening Method)

  • 윤길봉;전충근;정성철;윤기원;한천구
    • 한국콘크리트학회:학술대회논문집
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    • 한국콘크리트학회 2001년도 봄 학술발표회 논문집
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    • pp.243-248
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    • 2001
  • The objective of this study is to investigate the thermal conductivity of cement mortar for apartment housing floor using expansive admixture, copper fiber, cower lathe, hollowed aluminum plate. According to test results, temperature at point (a) located above heating pipe does not show significant variation with age, and temperature at (b), which is located at the finishing surface above heating pipe, and temperature at (c), which is located at center surface between heating pipe has remarkable change. Temperature distribution sat (b) are in order for, structure containing copper fiber>plain structure>structure containing hollowed aluminum plate>structure containing expansive admixture. Temperature distribution, shows high tendency in order for, structure containing copper fiber>structure containing copper lathe>structure containing hollowed aluminum plate>plain structure>structure containing expansive admixture. (a) estimation of temperature distribution is determined with the variation of temperature between (b) point and (c) point during 60 minutes heating.

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온수 가열 바닥 난방 시스템용 고성능 버블젯 루프 히트파이프 개발 (Development of High Performance Bubble Jet Loop Heat Pipe for Hot Water Floor Heating System)

  • 김종수;권용하;김정웅
    • 동력기계공학회지
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    • 제18권4호
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    • pp.23-28
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    • 2014
  • In order to increase the performance of conventional hot water floor heating system, the bubble jet loop heat pipe for the system was developed. This experiment was conducted under next conditions : Working fluid was R-134a, charging ratio was 50%. A temperature of hot water, room temperature and flow rate were $60^{\circ}C$, $15^{\circ}C$ and 0.5~1.5 kg/min, respectively. The experimental results, show that bubble jet loop heat pipe had a high effective thermal conductivity of $4714kW/m^{\circ}C$ and a sufficient heat flux of $73W/m^2$ to heat the floor to $35^{\circ}C$ in case of the 1.5 kg/min of flow rate. So the bubble jet loop heat pipe has a possibility for appling of the floor heating system. Additionally, the visualization of bubble jet loop heat pipe was performed to understand the operating principle. Bubbles made by the narrow gap between inner tube and outer tube of evaporating part generate pulsation at liquid surface of working fluid. The pulsation had slug flow and wavy flow. So working fluid circulates in the bubble jet loop heat pipe as two phase flow pattern. And large amount of heat is transferred by the latent heat from evaporating part to condensing part.

유한요소 시뮬레이션을 통한 지역난방열배관 특성 평가 및 강화이형관의 제안 (Design Validation and Improvement of District Heating Pipe Using FE Simulation)

  • 김주용;김호범;고현일;안영모;조종두
    • 대한기계학회논문집A
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    • 제33권4호
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    • pp.337-345
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    • 2009
  • This paper investigates the reliability of district heating pipes at thermo-elastic fatigue loading. District heating pipes, subjected to $120^{\circ}C$ and $16kg_f/cm^2$ due to water distributing service through inside the pipes, should endure long term cyclic thermal-mechanical loadings. The heating pipes are the co-centric tubes of steel pipe, poly urethane(PUR) insulator, and high density poly ethylene(HDPE) case. On installation, foam pad is externally wrapped for accommodating stress reduction near the bend sections of pipes. However, there have been frequent reports on the failures of bend sections in the middle of long term service. This study scrutinizes the observed failures near the bend sections through applying the finite element methods. Specially in this study, heating pipes are studied on the influence of foam padding on failures and proposed new designs for reinforced bend without foam pad.

긴 관을 이용한 롱넥플랜지 성형공정 개발에 관한 연구 (A Study on the Forming Process Development off Long-neck Flange Using a Long Pipe)

  • 최간대;강우진;배원병;조종래
    • 한국정밀공학회:학술대회논문집
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    • 한국정밀공학회 2002년도 춘계학술대회 논문집
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    • pp.699-704
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    • 2002
  • The pipe with a long-neck flange is widely used in power plants, chemical plants, and shipbuilding companies. New the pipe with a long-neck flange is manufactured by welding a thick flange to a pipe. But this long-neck flange pipe has some deflects in the welding region such as unfitting and local thermal fatigue, which weaken the strength around the neck of the flange. Moreover, after welding the flange, the contacting surfaces of the flange have to be machined flat. So, that is uneconomical. Therefore, to solve the above problems of the long-neck flange pipe, a new process, which has no defects around the flange neck, is required. In this study, three forming processes are suggested to get an enhanced long-neck flange. First suggested process consists of conical terming and flange forming. Second and third suggested processes consist of the bulging of a long pipe locally heated by induction coils and the flange forming. The differences between second and third suggestions are the thickness and local heating area of the pipe. That is, the thickness of the initial pipe of third suggestion is larger than that of the final product, and the local heating area is smaller than that of second suggestion. These three suggestions fur forming a long-neck flange are simulated by FE analyses with a commercial cede DEFORM 2D. Especially, the theoretical result of FE analysis on the first suggestion fur forming a long-neck flange is verified by the experiment with aluminum 6063 pipes. From the theoretical and experimental results, it is concluded that three suggested processes are very useful in order to manufacture the pipe with a long-neck flange without any deflects.

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긴 관을 이용한 롱넥플랜지 성형공정 개발에 관한 연구 (A Study on the Forming Process Development of a Long-neck Flange Using a Long Pipe)

  • 최간대;강우진;배원병;조종래
    • 한국정밀공학회지
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    • 제19권8호
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    • pp.212-219
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    • 2002
  • The pipe with a long-neck flange is widely used in power plants, chemical plants, and shipbuilding companies. Now the pipe with a long-neck flange is manufactured by welding a thick flange to a pipe. But this long-neck flange pipe has some defects in the welding region such as unfitting and local thermal fatigue, which weaken the strength around the neck of the flange. Moreover, after welding the flange, the contacting surfaces of the flange have to be machined flat. So, that is uneconomical. Therefore, to solve the above problems of the long-neck flange pipe, a new process, which has no defects around the flange neck, is required. In this study, three forming processes are suggested to get an enhanced long-neck flange. First suggested process consists of conical forming and flange forming. Second and third suggested processes consist of the bulging of a long pipe locally heated by induction coils and the flange forming. The differences between second and third suggestions are the thickness and local heating area of the pipe. That is, the thickness of the initial pipe of third suggestion is larger than that of the final product, and the local heating area is smaller than that of second suggestion. These three suggestions for forming a long-neck flange are simulated by FE analyses with a commercial code DEFORM 2D. Especially, the theoretical result of FE analysis on the first suggestion for forming a long-neck flange is verified by the experiment with aluminum 6063 pipes. From the theoretical and experimental results, it is concluded that three suggested processes are very useful in order to manufacture the pipe with a long-neck flange without any defects.