• 제목/요약/키워드: Engine performance simulation

검색결과 638건 처리시간 0.029초

중형 디젤 엔진의 연료분사노즐 형상에 따른 성능 해석 연구 (Performance Simulation for the Variation of Fuel Injection Nozzle Configurations in Medium Speed Diesel Engine)

  • 김기두;윤욱현;김병석;하지수;안광헌;김주태
    • Journal of Advanced Marine Engineering and Technology
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    • 제30권6호
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    • pp.662-668
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    • 2006
  • The effects of fuel injection nozzle hole on the NOx emission and fuel oil consumption of medium speed diesel engine HYUNDAI HiMSEN 6H21/32 engine are investigated by engine performance simulation. The results of performance simulation are verified by experimental results of NOx omission fuel oil consumption, cylinder pressure, and heat release rate according to the variation of the number of fuel injection nozzle hole and engine load. The performance simulations are also carried out to optimize the fuel injection nozzle of 6H21/32 engine in respect to the NOx emission and fuel oil consumption. The engine performance measurements are performed to verify the results of performance simulation and to investigate the effects of fuel injection nozzle on engine performance. The results of measurement indicate that significant NOx reduction can be achieved with minimum deterioration in fuel oil consumption by optimizing the geometry of fuel injection nozzle on 6H21/32 engine.

흡기가습 중형 디젤 엔진의 NOx 저감 평가를 위한 성능 해석 연구 (Engine Performance Simulation to Evaluate the NOx Reduction of Charge Air Moisturizer System in a Medium Speed Diesel Engine)

  • 김기두;박형근;김병석;하지수
    • 한국마린엔지니어링학회:학술대회논문집
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    • 한국마린엔지니어링학회 2005년도 후기학술대회논문집
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    • pp.15-16
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    • 2005
  • In this study, the characteristics of NOx reduction by using charge air moisturizer system were evaluated by engine performance simulation in medium speed diesel engines. The results of performance simulation were verified by experimental results of single cylinder medium speed diesel engine equipped with charge air moisturizer system. Performance simulation was carried out to evaluate charge air moisturizer system of turbocharged diesel engine, HYUNDAI HiMSEN 9H25/33 engine. Those results show 50% NOx reduction at dew point $80^{\circ}C$ and charge air pressure 4bar.

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엔진 부분 부하 성능 및 변속기 시프트맵을 이용한 차량주행성능 컴퓨터 시뮬레이션 (A Computer Simulation of a Driving Vehicle Performance using an Set of Engine Part Load Performance and a Transmission Shift Map)

  • 이충훈
    • 한국분무공학회지
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    • 제19권2호
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    • pp.64-68
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    • 2014
  • A driving vehicle performance which is driven by FTP-75 mode was simulated by computer. Throttle valve position, engine speed, air mass flow rate, fuel consumption et al. were computer simulated. A set of engine part load performance data, automatic transmission shift map and vehicle specifications were used for the computer simulation. Throttle valve position, engine speed, air mass flow rate et al. measured for evaluating the computer simulation results by driving the vehicle with FTP-75 mode on a chassis dynamometer. GT-Power$^{(R)}$ software was used for the computer simulation of the driving vehicle performance. Experimental fuel consumption rate was measured by using an ECU HILS fuel injection system. The experimental data and simulation results were compared. The computer simulation of the driving vehicle performance predicts the measured data well comparatively.

2스풀 분리 배기 방식 엔진의 정상상태 성능모사 및 작동 진단 (Steady-state Performance Simulation and Operation Diagnosis of a 2-spool Separate Flow Type Turbofan Engine)

  • 추교승;성홍계
    • 항공우주시스템공학회지
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    • 제13권1호
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    • pp.38-46
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    • 2019
  • 가스터빈 엔진에 대한 엔진 진단기술에 대한 관심이 높아지고 있으며, 엔진 건전성 진단기술에 적용 가능한 정확한 엔진 성능모사 프로그램의 중요성은 점점 더 커지고 있다. 이를 위한 엔진 성능모사는 설계점 해석으로부터 시작하여 탈설계점 성능모사, 부분부하 성능모사를 정확하게 수행해야 할 필요가 있다. 이에 따라 본 연구에서는 2-스풀 분리 배기 방식 터보팬 엔진에 대한 엔진 시뮬레이션 프로그램을 개발하고 PW(Pratt & Whitney)사의 JT9D-7R4G 엔진을 해석하였다. 각 비행영역에서의 설계점과 탈설계점에서의 정상상태 성능모사를 수행하고, 최대이륙조건 설계점과 순항상태 설계점의 해석결과의 차이를 비교하였다. 또한 구성품 성능선도 축척법 중 하나인 Reynold's Correction의 효과를 분석하였다. 개발된 프로그램의 결과와 NPSS의 결과를 비교하여 프로그램을 검증하였다.

Miller 사이클을 이용한 중형 디젤 기관 성능 개선 (Improving the performance of a Medium Speed Diesel Engine Using Miller Cycle)

  • 김동훈;김기두;하지수;김호익;김주태
    • Journal of Advanced Marine Engineering and Technology
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    • 제26권2호
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    • pp.248-255
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    • 2002
  • Miller cycle was studied and analyzed by engine performance simulation to achieve very low fuel consumption and to meet the IMO NOx regulation on a medium speed diesel engine. Based on the performance simulation results the intake valve closing time for HYUNDAI HiMSEN 6H21/32 engine was set at 0deg.ABDC(After Bottom Dead Center). Also, the simulation results indicated that significant NOx reduction could be achieved with low reduction of fuel consumption. The performance simulation investigated the effect of compression ratio and turbocharger on fuel consumption and NOx concentration in combination with Miller cycle. The results indicated a significant reduction of fuel consumption with keeping NOx concentration. The results of performance simulation were compared with measured data to verify simulation results. The comparison showed the maximum error was 2.34% in exhaust temperature. Also, the experimental result showed that improvement in BSFC(Brake Specific Fuel Consumption) was 5.8g/kwh with keeping NOx level similar to simulation result.

Performance Analysis, Real Time Simulation and Control of Medium-Scale Commercial Aircraft Turbofan Engine

  • Kong, Chang-Duk;Jayoung Ki;Chung, Suk-Chou
    • Journal of Mechanical Science and Technology
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    • 제15권6호
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    • pp.776-787
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    • 2001
  • The turbofan engine performance analysis for a medium scale commercial aircraft was carried out and the LQR control scheme for performance optimization was studied. By using scaled component maps from well-known CF6 engine characteristics, the steady-state performance analysis result was compared with BR715-56 engine performance data. The transient performance analysis was performed with four fuel schedules. The linear simulation was done at the maximum take-off condition. The real time linear simulation was performed by interpolation of the system matrices, which used the least square method as the function of LPC rotational speed. By using linear system matrices of design point, the LQR controller which used control variables for the fuel flow and the LPC bleed air was designed.

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특성곡선법과 다중길이 척도법을 이용한 가솔린 기관의 기관성능시뮬레이션 개선에 관한 연구 (A Study on the Improvment of Engine Performance Simulation Using Multi-Length-Scale Model and MOC)

  • 김철수
    • Journal of Advanced Marine Engineering and Technology
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    • 제25권3호
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    • pp.605-616
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    • 2001
  • Generally, there are two methods in researching internal combustion engines. One is by experimental research and the other is by computer simulation. The experimental research has many merits that researchers can get data for engine performance, but it has also some demerit of cost and time. If there is an engine simulation code with accuracy for the solution, it is very convenient to predict the performance and optimum design value of the engine. In this study, engine performance simulation program has been improved to predict the transient variation of properties of gas in cylinder, intake and exhaust manifolds, There total program code was developed to calculate the pressure, flame factor and turbulent intensity, As a result of present study, the authors could predicted the in-cylinder pressure, intake manifold pressure and the engine performance in various conditions. The authors also could easily prepare the tool if optimum design of manifold and in-cylinder geometry.

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A New Methodology for Advanced Gas Turbine Engine Simulation

  • M.S. Chae;Y.C. Shon;Lee, B.S.;J.S. Eom;Lee, J.H.;Kim, Y.R.;Lee, H.J.
    • 한국추진공학회:학술대회논문집
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    • 한국추진공학회 2004년도 제22회 춘계학술대회논문집
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    • pp.369-375
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    • 2004
  • Gas turbine engine simulation in terms of transient, steady state performance and operational characteristics is complex work at the various engineering functions of aero engine manufacturers. Especially, efficiency of control system design and development in terms of cost, development period and technical relevance implies controlling diverse simulation and identification activities. The previous engine simulation has been accomplished within a limited analysis area such as fan, compressor, combustor, turbine, controller, etc. and this has resulted in improper engine performance and control characteristics because of limited interaction between analysis areas. In this paper, we propose a new simulation methodology for gas turbine engine performance analysis as well as its digital controller to solve difficulties as mentioned above. The novel method has particularities of (ⅰ) resulting in the integrated control simulation using almost every component/module analysis, (ⅱ) providing automated math model generation process of engine itself, various engine subsystems and control compensators/regulators, (ⅲ) presenting total sophisticated output results and easy understandable graphic display for a final user. We call this simulation system GT3GS (Gas Turbine 3D Graphic Simulator). GT3GS was built on both software and hardware technology for total simulation capable of high calculation flexibility as well as interface with real engine controller. All components in the simulator were implemented using COTS (Commercial Off the Shelf) modules. In addition, described here includes GT3GS main features and future works for better gas turbine engine simulation.

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소형 장기체공 무인기용 왕복엔진 성능 예측 시뮬레이션 연구 (A Study on Performance Simulation of an Reciprocating Engine for Small Long Endurance Unmanned Aerial Vehicles)

  • 장성호;구삼옥;신영기
    • 대한기계학회논문집B
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    • 제29권7호
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    • pp.820-827
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    • 2005
  • Development of an engine with good fuel economy is very important for successful implementation of long endurance miniature UAVs (unmanned aerial vehicles). In the study, a 4-stroke glow-plug engine was modified to a gasoline-fueled spark-ignition engine. Engine tests measuring performance and friction losses were conducted to tune a simulation program for performance prediction. It has been found that excessive friction losses are caused by insufficient lubrication at high speeds. The simulation program predicts that engine power and fuel economy get worse with high altitude due to increasing portion of friction losses. The simulation results suggest quantitative guidelines for further development of a practical engine.

EFFECT OF DI-TERTIARY-BUTYL PEROXIDE ON IGNITION PERFORMANCE IN A COMPRESSION IGNITION NATURAL GAS ENGINE

  • Li, F.C.;Zheng, Q.P.;Zhang, H.M.
    • International Journal of Automotive Technology
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    • 제8권4호
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    • pp.413-419
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    • 2007
  • Experimental study of additives on the ignition performance of a compression ignition natural gas engine is introduced, followed by results of a simulation of its working mechanism. From the experimental results, it is understood that engine ignition performance can be improved when a certain amount of Di-tertiary-butyl peroxide additive is added. If the mass fraction of Di-tertiary-butyl peroxide additive reaches as high as 14.2%, engine ignition can be realized at ambient temperatures with a glow plug temperature of about $750^{\circ}C$. From the simulation results, we verify that the Di-tertiary-butyl peroxide additive, by cracking its radicals at lower temperature, can accelerate reaction rate. Therefore, the additive is able to improve the ignition performance of natural gas significantly.