• Title/Summary/Keyword: Engine development cost

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Development of an Intake E-CVVT Noise for the Medium-sized Sedan Vehicle (중형 세단 차량의 흡기 전동 CVVT 소음 개발)

  • Lee, Jong Kyu;Lee, Hyung Min;Lee, Hae Seung;Kwon, O Jun
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2014.10a
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    • pp.341-346
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    • 2014
  • Intake E-CVVT noise, generally caused by collision sound of roller and cage clearance at idle and driving condition, is considerable source of annoyance in passenger cars using the gasoline engine. Main source of this noise is the cam torque variation of an intake E-CVVT system, and can be controlled by clearance decrease such as backlash reduction, but which may increase the manufacturing cost. Thus in this paper, most effective solution for low noise intake E-CVVT was achieved through not only reduction of backlash and cam angular acceleration but also improvement of vehicle transfer system, which is optimal configuration through acoustic sensitivity optimization of engine mount support bracket.

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Development of Bending Process for Crank Throw of Large Marine Engine Using Unbending Concept (언벤딩 개념을 이용한 선박용 대형 크랭크 쓰로우 굽힘단조 공법 개발)

  • Lee, S.M.;Lee, W.J.;Kim, I.H.;Park, Y.G.;Park, H.J.
    • Proceedings of the Korean Society for Technology of Plasticity Conference
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    • 2007.10a
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    • pp.46-49
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    • 2007
  • The purpose of this study is to develop the optimum shape of blank for the crank throw of large marine engine in order to reduce manufacturing cost and forging defects. The effects of the curvature radius and the height of wing part of blank selected as design variables on the defects and machining margin of final products after forging process were investigated using FEA. Based on the results, the optimum shape for the blank of the crank throw was proposed and verified by experiment.

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A study on the technical consideration in initial game software planning of online game (온라인 게임 초기 기획단계에서 고려될 기술 요소에 대한 연구)

  • Lee, Myoun-Jae;Kim, Kyoung-Nam
    • Journal of Korea Game Society
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    • v.3 no.2
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    • pp.3-11
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    • 2003
  • Game software planning is divided into initial game software planning and detailed game software planning. Technique, design, marketing should be considered in initial game software planning. Especially, technical considerations, platform and game engine and sewer construction and sewer architecture should have effect on development cost and time. So, game software designer should choose technical consideration which is suitable for purpose of game software planning. In this paper, we researched technical considerations in initial game software planning, focusing on platform, game engine, game service, network infrastructure.

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1-D Model to Estimate Injection Rate for Diesel Injector using AMESim (디젤 인젝터 분사율 예측을 위한 AMESim 기반 1-D 모델 구축)

  • Lee, Jinwoo;Kim, Jaeheun;Kim, Kihyun;Moon, Seoksu;Kang, Jinsuk;Han, Sangwook
    • Journal of ILASS-Korea
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    • v.25 no.1
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    • pp.8-14
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    • 2020
  • Recently, 1-D model-based engine development using virtual engine system is getting more attention than experimental-based engine development due to the advantages in time and cost. Injection rate profile is the one of the main parameters that determine the start and end of combustion. Therefore, it is essential to set up a sophisticated model to accurately predict the injection rate as starting point of virtual engine system. In this research, procedure of 1-D model setup based on AMESim is introduced to predict the dynamic behavior and injection rate of diesel injector. As a first step, detailed 3D cross-sectional drawing of the injector was achieved, which can be done with help of precision measurement system. Then an approximate AMESim model was provided based on the 3D drawing, which is composed of three part such as solenoid part, control chamber part and needle and nozzle orifice part. However, validation results in terms of total injection quantity showed some errors over the acceptable level. Therefore, experimental work including needle movement visualization, solenoid part analysis and flow characteristics of injector part was performed together to provide more accuracy of 1-D model. Finally, 1-D model with the accuracy of less than 10% of error compared with experimental result in terms of injection quantity and injection rate shape under normal temperature and single injection condition was established. Further work considering fuel temperature and multiple injection will be performed.

Introduction to Construction of Propulsion Test Facilities for KSLV-II (한국형발사체 추진기관 시험설비 구축에 대한 소개)

  • Han, Yeoung-Min;Cho, Nam-Kyung;Chung, Young-Gahp;Kim, Seung-Han;Yu, Byung-Il;Lee, Kwang-Jin;Kim, Jin-Sun;Kim, Ji-Hoon;Kim, Young-Mog
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2010.11a
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    • pp.343-346
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    • 2010
  • The construction plan of a combustion chamber test facility(CTF), a turbopump real propellant test facility(TPTF), a rocket engine ground/high altitude test facility(ReTF, HAReTF) and a propulsion system test complex(PSTC) for KSLV-II is briefly described. The development/qualification tests of 75ton-class liquid rocket engine system and engine component will be performed in CTF, TPTF, ReTF and HAReTF and the development test of $1^{st}/2^{nd}/3^{rd}$ propulsion systems for KSLV-II will be performed in PSTC. These propulsion test facilities will be built in NARO space center considering construction schedule, cost, safety distance and utility factor of propulsion test facilities.

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Development of Air-Damping Mount (에어 댐핑 마운트 개발)

  • Kim, Jeong-Hoon;Lee, Dong-Wook;Kim, Jae-San
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2009.10a
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    • pp.328-329
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    • 2009
  • Air-Damping Mount is proposed to compromise between performance and weight & cost. The design of Air-Damping Mount was based on the specification from the engine mounting system analysis of a small car. To verify it's feasibility, R&H test was done on the small car and it is proven that Air-Damping Mount shows the performance between hydraulic mount and rubber mount.

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A Study on the Evaluation of Scavenging Efficiency in a Two-Stroke Diesel Engine. (2행정 디젤기관의 소기 효율 평가에 관한 연구)

  • Jo, Gyu-Baek;Gang, Geon-Yong;Lee, Jin-Uk;Jeong, Yong-Il
    • 연구논문집
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    • s.28
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    • pp.49-58
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    • 1998
  • In order to analyse the scavenging efficiency in a poppet valve type 2-stroke engine. visualization of scavenging flow and quantitative experiments for measuring scavenging efficiency were performed. The effect of shroud angle in RSSV which was developed by KIMM was evaluated under steady flow rig applying single-cycle method. Also dynamic simulator was used by using gas sampling with $CO_2$ and $O_2$gas. The $90^circ$ shroud RSSV was found to be the highest efficient system, and single-cycle and dynamic simulator test are very effective to save time and cost for the development of a 2-stroke engine.

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Heat Exchangers for Gas Turbine Cycles and Thermal Management (롤스로이스 기술개발 동향)

  • Stieger, Rory
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2011.04a
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    • pp.465-465
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    • 2011
  • Rolls-Royce is a global company producing advanced power systems for use on land, at sea and in the air. In order to develop competitive products and services, Rolls-Royce invests in technology, infrastructure and capability with much of the research carried out in a global network of University Technology Centres, such as the UTC in Thermal management at Pusan National University. Heat exchangers and thermal management play a critical role in today's gas turbine engines, maintaining the fuel and oil temperatures within the correct operational range. Future products are likely to place an increased duty on the thermal management system and thus require advances in heat exchanger design, installation and manufacturing. Heat exchangers further have the potential to play a vital role in Advanced Cycle Gas Turbine products. The Intercooled and recuperated WR21 marine gas turbine engine recently entered service with the Royal Navy and is delivering very attractive fuel burn in service. The development of an advanced cycle aero-engine is a significantly greater challenge, requiring better understanding of compact and light weight heat exchanger surfaces, novel installations and ducting systems and may required novel manufacturing techniques to achieve the volume, weight and cost necessary to realise a viable advanced cycle gas turbine aero-engine.

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Development of Low-Cost, Double-Speed, High-Precision Operation Control System for Range Extender Engine (레인지 익스텐더 전기자동차 엔진용 저가형 2단속도 고정밀 운전제어시스템 개발)

  • Ham, Yun-Young;Lee, Jeong-Jun
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.19 no.11
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    • pp.529-535
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    • 2018
  • The range extender vehicle runs on a mechanism that allows the small power generation engine to start in the most efficient specific operating range to charge the battery and extend the mileage. In this study, we developed a step motor type intake air supply system that replaces existing throttle body system to develop a simple low cost control logic system. The system was applied to the existing base engine, and in order to improve the performance by increasing the amount of intake air, the effect of changing the length of the intake and exhaust manifold was experimentally examined. As a result, the Type B intake air control actuator operated by one step motor showed higher performance than the Type A in all the operation region, but the performance was lower than that of the base engine due to the increase of flow resistance. To improve this, it was confirmed that the engine performance was improved at both speeds of 2200rpm and 4300rpm when the 140mm adapter was installed in the intake manifold and when the newly designed 70mm exhaust manifold was applied. Through this process, high - precision operation control was realized by connecting the generator load to the optimized engine for the range extender electric vehicle. Experimental results showed that the speed change rate was within ${\pm}2.5%$ at 2200rpm in 1st stage and 4300rpm in 2nd stage and the speed follow-up result of 610 rpm/s was obtained when the speed was increased from 2200rpm to 4300rpm.

The Study of Flow Rate Performance and Engine Application with LPG Composition Rate for LPi Fuel Supplying System Consisted of Turbine Type Pump (터빈방식 연료펌프로 구성된 LPi 연료공급 시스템의 LPG 조성비에 따른 토출성능 및 엔진적용성에 관한 연구)

  • Lim, Mu-Chang;Myung, Cha-Lee;Park, Sim-Soo;Park, Jeong-Nam;Kim, Sung-Kun
    • Transactions of the Korean Society of Automotive Engineers
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    • v.15 no.3
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    • pp.99-105
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    • 2007
  • Currently, BLDC fuel pump was applied on LPi vehicle using 3rd fuel supply system as liquified phase LPG injection method had already shown better performance than others. Its cost, however, is rather expensive because of drawbacks such as complicated structure, a fault of localization of system. In this work, demonstration system for a developed turbine type fuel pump to replace BLDC system was setup and investigated. This study results that fuel mass flow rate of turbine type pump and injection performance of injector were better compared to BLDC type. Comparing flow rate of summer LPG with that of winter LPG, the flow rate decreased about 25% using winter LPG. Performance applying turbine type LPi fuel pump to engine is confirmed.