• 제목/요약/키워드: Centrifugal turbo blower

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FCEV 블로워의 소음특성과 개선방향에 관한 연구 (A Study on the Noise Property and its Reduction of the FCEV Blower)

  • 오기석;이상권;서상훈
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2007년도 추계학술대회논문집
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    • pp.1419-1424
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    • 2007
  • Centrifugal turbo blower is requested highly efficiency and low noise in FCEV, but the noise generated by this machine causes of the most serious problems in the NVH performance. In general, centrifugal turbo blower is dominated by mechanical noise and aerodynamic noise. Mechanical noise is generated by rotation of the bearing, misalignment and unbalance. And aerodynamic noise is generated by the strong intersection between the flow discharged from the impeller and the cut-off in the casing. The first object of this study is to comprehend a noise property of the blower through the noise test. And, second object is to bring up the method that can reduce blower noise.

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FCEV 블로워의 소음특성과 개선방향에 관한 연구 (A Study on the Noise Property and Its Reduction of the FCEV Blower)

  • 오기석;이상권;서상훈
    • 한국소음진동공학회논문집
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    • 제18권5호
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    • pp.516-523
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    • 2008
  • Centrifugal turbo blower is requested highly efficiency and low noise in FCEV, but the noise generated by this machine causes of the most serious problems in the NVH performance. In general, centrifugal turbo blower is dominated by mechanical noise and aerodynamic noise. Mechanical noise is generated by rotation of the bearing, misalignment and unbalance. And aerodynamic noise is generated by the strong intersection between the flow discharged from the impeller and the cut-off in the casing. The first object of this study is to comprehend a noise property of the blower through the noise test. And, second object is to bring up the method that can reduce blower noise.

진동 동력 흐름 기법을 이용한 FCEV용 원심형 터보 블로워의 진동 저감 (Reducing Vibration of a Centrifugal Turbo Blower for FCEV Using Vibrational Power Flow)

  • 김윤석;이상권
    • 한국자동차공학회논문집
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    • 제17권2호
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    • pp.150-158
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    • 2009
  • A centrifugal turbo blower is one of the part to generate electric power of fuel cell electric vehicle(FCEV). In order to generate the electric power of FCEV, the centrifugal turbo blower operates at very high speed above 30,000rpm in order to increase the pressure of the air, which supplied to a stack of FCEV, using rotation of its impeller blades. Vibration which originated from the blower is generated by unbalance of mechanical components, rotation of bearings and rotating asymmetry that rotate at high speed. The vibration is transmitted to receiving structure through vibration isolators and it can causes serious problems in the noise, vibration and harshness(NVH) performance. Thus, the study about reducing this kind of vibration is an important task. Quantifying the effectiveness of vibration isolation can be effectively accomplished by using vibrational power flow because relative contributions of each isolator to the total vibration transmission can be easily represented. In this paper, vibrational power flow is applied to the centrifugal turbo blower mounted on FCEV in order to analyze the most dominant vibration transmitting path. As a result, the main contributor among four isolators is a mount #3 of the blower. Also, a 30 percent lowering of the mount #3 stiffness shows 34 percent decrement of vibrational power flow by the simulation.

FCEV용 원심형 터보 블로워의 마운트 진동 저감에 관한 연구 (A Study on Mount Vibration Reduction of a Centrifugal Turbo Blower for FCEV)

  • 김윤석;이상권
    • 한국소음진동공학회논문집
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    • 제18권10호
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    • pp.1073-1081
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    • 2008
  • A centrifugal turbo blower of the fuel cell electric vehicle (FCEV) operates at very high speed above 30000 rpm in order to increase the pressure of the air, which supplied to a stack of FCEV, using rotation of its impeller blades. Vibration which originated from the blower is generated by unbalance of mechanical components, rotation of bearings and rotating asymmetry that rotate at high speed. The vibration is transmitted to receiving structure through vibration isolators and it can causes serious problems in the noise, vibration and harshness(NVH) performance. Thus, the study about reducing this kind of vibration is an important task. In this paper, dynamic analysis of the blower executed by numerical simulation and experimental analysis of the blower is also performed. Then, measured and simulated results are compared in order to validate of the simulation. Finally, reducing vibration through modifying mount stiffness is the main purpose of this paper.

FCEV Turbo Blower 의 동특성 해석 (Dynamic Analysis of FCEV Turbo Blower)

  • 육지용;양현섭;이창하;조경석;박용선;권혁률
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2010년도 추계학술대회 논문집
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    • pp.599-606
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    • 2010
  • This paper presents dynamic analysis of FCEV (Fuel Cell Electric Vehicle) Turbo Blower. To analyze the dynamic characteristics of Turbo Blower, finite element model which consists of solid elements is constructed. Evaluation of stress for safety of rotor sleeve due to centrifugal force, Shrink fit analysis in maximum rotation speed is performed. Rotor dynamic analysis of Turbo blower is conducted using Campbell diagram and FEA (Finite element analysis) results are compared with experimental results to evaluate of validity of finite element model. To evaluate of Structure vibration characteristics, Modal analysis and forced vibration analysis are performed through FEA and experiment.

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유동 저항에 따른 원심홴의 선정 (Selection of Centrifugal Fan for Flows with Down-Stream Resistance)

  • 김재원;장동희;안은영
    • 한국유체기계학회 논문집
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    • 제9권3호
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    • pp.44-48
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    • 2006
  • Comprehensive experimental works are carried out for the optimal design of a centrifugal blower adopted in an indoor unit of an air-conditioner. The models for consideration are typical multi-blade turbo blower and limit loaded one, respectively. The main interest lies on the fluid dynamics performance when the blower Is installed in the practical system. The methodologies are an experimental estimations with a wind tunnel for blower performance and PIV measurement for the detail flow information. A centrifugal blower with limit loaded fan shows pronounced performances in terms of the flow rate and static pressure rise and the reason is explained by the precise measurement of the flows between blades using PIV. Consequently, it is found that the blower is proper for the flows with a resistance in down stream such as a heat exchanger.

고압 터보 Blower "Greenpressor" 개발 (Commercial Development of a High Pressure Turbo Blower "Greenpressor")

  • 최문창;바르탄 뻬뜨로샹;나탈리아 자칼로바
    • 유체기계공업학회:학술대회논문집
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    • 유체기계공업학회 2003년도 유체기계 연구개발 발표회 논문집
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    • pp.323-323
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    • 2003
  • Many recent development activities suggest the possibility of a high-speed turbo(centrifugal) compressor or blower for the industrial application of compressed air supplying system when used with the most advanced high-speed motor, inverter technology, and advanced bearing for high rotational speed. The problems to be overcome are of reliability, the application of mass production methods, cost effective manufacture and competitive running costs. This presentation is not focused on a specific technology advances but on an overall review of our recent experiences while we have developed the high pressure turbo blower for the commercial purpose.

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Design and Experimental Investigation of High-Speed Three-Phase Induction Motor for Turbo Blower

  • Kim, Young-Kwan;Lee, Ju
    • 조명전기설비학회논문지
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    • 제22권3호
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    • pp.59-65
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    • 2008
  • High-speed electrical motor has been studied for several applications, i.e. for direct-drive systems of centrifugal compressors and turbo blowers. This paper deals with a design consideration of electromagnetic, mechanical and thermal limits of high-speed induction motor for turbo blower. Basic design concept of high-speed motor was proposed. As the motor is to be operated at high speed, the losses are quite different from conventional low-speed machines. Especially, the increases of rotor eddy current and friction losses could lead to an overheated motor. So, we suggested a special cooling system to reduce temperature rise. And, based upon this design concept, the prototype induction motor(37[kW], 45,000[rpm]) for high-speed turbo blower was designed and 2-D electromagnetic field analysis was implemented. Finally, criteria to evaluate the characteristics of high-speed induction motor have been proposed and tested.

PEM 연료전지용 터보 블로워의 내구성에 관한 실험적 연구 (An Experimental Study on the Durability Test for PEM Fuel Cell Turbo-blower)

  • 이용복;이희섭;정진택
    • 한국자동차공학회논문집
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    • 제16권5호
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    • pp.37-43
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    • 2008
  • The durability test of turbo-blower for PEM fuel cell is very important process of BOP development. It is a major barrier to the commercialization of these systems for stationary and transportation power applications. Commercial viability depends on improving the durability of the air supply system to increase the reliability and to reduce the lifetime cost. In this study, turbo-blower supported by oil-free bearing is introduced as the air supply system used by 80kW proton exchange membrane fuel systems. The turbo-blower is a turbo machine which operates at high speed, so air foil bearings suit their purpose as bearing elements. The impeller of blower was adopted mixed type of centrifugal and axial. So, it has several advantages for variable operating condition. The turbo-blower test results show maximum parasitic power levels below 1.67kW with the 30,000 rpm rotating speed, the flow rate of air has maximum 163SCFM(@PR1.1). For proper application of FCV, these have to durability test. This paper describes the experiment for confirming endurance and stability of the turbo-blower for 500 hours.

흡입저항이 높은 원심홴 소음특성에 관한 연구 (Study on the Noise Characteristic of Centrifugal Fan operating at High Pressure Region)

  • 정윤영;박진원;전완호
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2006년도 춘계학술대회논문집
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    • pp.1011-1014
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    • 2006
  • Turbo blower generates high peaks when it operates at high pressure region. The fan of the air-cleaner system, operates especially high pressure region due to several filters, generates high noise level. In this case, the tonal sound of BPF makes people annoyance. The blower of air-cleaner has several high resistance filters in its inlet area and rotates above 900rpm Moreover, for the compact design, the size of the blower should be reduced 10%. The reduced diameter of blower makes low flow rate and high noise level. In order to reduce the noise, new blade shape was suggested and optimized

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