• Title/Summary/Keyword: Cavitation number

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Experimental Study on the Cavitation Noise of a Hydrofoil (3차원 날개의 캐비테이션 소음 계측시험)

  • Lee, Seung-Jae;Seo, Jong-Soo;Han, Jae-Moon
    • Journal of the Society of Naval Architects of Korea
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    • v.44 no.2 s.152
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    • pp.111-118
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    • 2007
  • In order to investigate the noise characteristics of the different caviation, noise measurements were carried out in a large cavitation tunnel of the Samsuug Ship Model Basin(SSMB). The noise measurements for a 3-dimensional hydrofoil were carried out at the angle of attack of $12^{\circ}$ and $16^{\circ}$ according to the decrease in cavitation number. It is exhibited that sound pressure level(SPL) increased sharply with cavitation inception. The frequency of the noise induced by sheet cavitation was higher than that of tip vortex cavitation in the phase of cavitation inception. Within the range of the high frequency, in the case of fully developed cavitation, sheet cavitation noise was significantly increased in sound pressure level compared with tip vortex cavitation noise. In this study, the noise characteristics of the different cavitation types were considered experimentally and would be utilized as a basis for the analysis of propeller cavitation noise.

Study on Tip-Vortex Cavitation and Its Noise Characteristics - Effects of Surface Roughness - (타원형날개끝 캐비테이션과 유기소음 특성연구 - 표면거칠기의 영향 -)

  • B.S. Hyun;C.M. Lee;H.S. Choi
    • Journal of the Society of Naval Architects of Korea
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    • v.31 no.1
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    • pp.84-93
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    • 1994
  • The purpose of present study is to investigate the surface roughness on tip-vortex cavitation and its induced noise, emanating from an elliptic wing of NACA 0012 section. Roughness elements of $200{\mu}m$ are applied to the 10% portion of wing tip, and then, the wing tip as well as the leading edge. It is shown from cavitation observation that the cavitation inception is first visible at about half chord downstream of wing tip for most experimental conditions, and developed into the tip-vortex cavitation and finally the fully developed cavitation as cavitation number is decreased. Acoustic noise generated by a tip-vortex cavitation has its frequency range of 3 kHz to 50 kHz, while the fully-developed cavitation at lower cavitation number induces a broad band spectrum. It is also shown that, when the roughness elements are applied to the wing tip and the leading edge, the cavitation characteristics and its induced noise are improved. Moreover, it is appeared that the condition at which the rough surface is at pressure side gives a better result. although its lift-drag ratio is reduced.

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Effect of Reynolds Number, Leading Edge Roughness and Air Content on the Cavitation Performance of Model Propellers (Reynolds수, 표면거칠기 및 공기함유량이 모형프로펠러 캐비테이션 성능에 미치는 영향)

  • Ki-Sup Kim;Kyung-Yeul Kim;Jong-Woo Ahn;Jin-Tae Lee
    • Journal of the Society of Naval Architects of Korea
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    • v.37 no.1
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    • pp.10-25
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    • 2000
  • The effects of Reynolds number of model propeller leading edge roughness and air content resolved in tunnel water on cavitation inception, cavitation extent and pressure fluctuation were investigated experimentally by using two model propellers in a cavitation tunnel. Cavitation observation and propeller induced fluctuating pressure measured in the present model test were compared with the model test results of other research institutes and the full-scale data of a German container ship(Sydney Express). The comparison shows a reasonable agreement.

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The Characteristics of a Pump at Nearly Saturated State

  • Kim, S. N.;Kim, J. C.
    • Nuclear Engineering and Technology
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    • v.30 no.1
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    • pp.40-46
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    • 1998
  • A set of experiments using a 1/10 scale model pump which was manufactured to simulate performance of reactor coolant pump(RCP) of Y.G.N # 3 and 4, was executed in single phase(at atmospheric pressure and room temperature) and near-saturation(300 ~ 600kPa). The pump characteristics in single phase flow was similar to the characteristics of the RCP. The pump characteristic curves at nearly saturated state were correlated in terms of flow coefficient and head coefficient for subcooled temperature using the cavitation number defined as (equation omitted), which can be predicted the cavitation possibility. The pump behavior around the saturated temperature almost consists with single phase behavior until the cavitation occurs(When cavitation occurs. When the flow coefficient is about 0.12), the pump head rapidly degrades. In this situation, subcooled temperature is about 1.8~8$^{\circ}C$ and cavitation number of model pump is 1.0 ~ 1.7.

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Control of cavitation in Venturi using hemispherical bump (반구형 융기부를 이용한 벤투리에서의 캐비테이션 제어)

  • Jongbin Hwang;Yisu Shin;Jooha Kim
    • Journal of the Korean Society of Visualization
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    • v.21 no.2
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    • pp.91-101
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    • 2023
  • In this study, we investigated how the performance of a Venturi changes when a hemispherical bump is applied to the divergent part of the Venturi tube and what causes the performance difference. The Venturi-tunnel experiment was conducted in the Reynolds number range of 0.2 × 105 - 1.2 × 105 and cavitation number range of 0.9 - 10. The bump was found to reduce the pressure loss coefficient and increase the discharge coefficient by shortening the cavitation length. The decrease in the cavitation length by the bump was explained by the strengthening of the re-entrant jet. The wake generated from the hemispherical bump seems to increase the adverse pressure gradient on the Venturi surface, thereby strengthening the re-entrant jet.

Cavitation studies on axi-symmetric underwater body with pumpjet propulsor in cavitation tunnel

  • Suryanarayana, Ch.;Satyanarayana, B.;Ramji, K.;Rao, M. Nageswara
    • International Journal of Naval Architecture and Ocean Engineering
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    • v.2 no.4
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    • pp.185-194
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    • 2010
  • A pumpjet propulsor (PJP) was designed for an underwater body (UWB) with axi-symmetric configuration. Its performance was predicted through CFD study and models were manufactured. The propulsor design was evaluated for its propulsion characteristics through model tests conducted in a Wind Tunnel (WT). In the concluding part of the study, evaluation of the cavitation performance of the pumpjet was undertaken in a cavitation tunnel (CT). In order to assess the cavitation free operation speeds and depths of the body, cavitation tests of the PJP were carried out in behind condition to determine the inception cavitation numbers for rotor, stator and cowl. The model test results obtained were corrected for full scale Reynolds number and subsequently analyzed for cavitation inception speeds at different operating depths. From model tests it was also found that the cavitation inception of the rotor takes place on the tip face side at higher advance ratios and cavitation shifts towards the suction side as the RPS increases whereas the stator and cowl are free from cavitation.

Numerical investigation of the gravity effect on the shape of natural supercavity

  • Pouraria, Hassan;Park, Warn-Gyu
    • 한국전산유체공학회:학술대회논문집
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    • 2011.05a
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    • pp.58-64
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    • 2011
  • The objective of this paper is to investigate the gravity effect on the shape characters of natural supercavity. A finite difference solver along with an implicit, dual time, preconditioned, three-dimensional algorithm has been used to solve the two-phase Navier Stokes equations. Numerical solutions were performed for natural supercavitating flow past a disk for different cavitation and Froud numbers. The numerical results were compared with corresponding analytical results in quantitative manner and it was found that the shape of supercavity was reasonably predicted Numerical results indicated that the gravity effect can induce the asymmetry of supercavity. The asymmetry was apparent when the froud number was smaller so that for constant cavitation number when we reduced the froud number the opt of the axis of supercavity increased. Moreover, for specific froud number a decrease in cavitation number resulted in an increase in the offset of the supercavity Numerical results revealed that for froud number greater than 25 the gravity effect is negligible.

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Experimental Study on the Unsteady Cavitation of Turbopump Inducer (터보펌프 인듀서의 비정상 캐비테이션에 관한 실험적 연구)

  • Hong, Soon-Sam;Kim, Jin-Sun;Choi, Chang-Ho;Kim, Jin-Han
    • The KSFM Journal of Fluid Machinery
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    • v.8 no.1 s.28
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    • pp.23-29
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    • 2005
  • Steady and unsteady cavitation characteristics of turbopump inducer were investigated in this paper. To investigate the effect of blade angle on the inducer performance, three inducers with inlet tip blade angle of $7.8^{\circ},\;7.0^{\circ},\;6.1^{\circ}$, respectively, were tested. For $7.8^{\circ},\;7.0^{\circ}$ inducers in the non-cavitating condition, head decreased linearly with flow rate, but head-flow rate curve had a dip at the flow coefficient ${\psi}=0.065$ for $6.1^{\circ}$ inducer. Attached cavitation and cavitation surge were found in the $7.8^{\circ},\;7.0^{\circ}$ inducers in the cavitation tests. During the attached cavitation one cell rotated at the same rotational speed as that of the inducer. The cavitation surge did not rotate and the oscillating frequency was $7{\sim}20\;Hz$. From the curve of the critical cavitation number versus flow rate, it was found that the steady cavitation performance of $6.1^{\circ}$ inducer was much lower than that of $7.8^{\circ},\;7.0^{\circ}$ inducers.

Experimental Study on the Unsteady Cavitation of Turbopump Inducer (터보펌프 인듀서의 비정상 캐비테이션에 관한 실험적 연구)

  • Hong, Soon-Sam;Kim, Jin-Sun;Choi, Chang-Ho;Kim, Jin-Han
    • 유체기계공업학회:학술대회논문집
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    • 2003.12a
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    • pp.333-339
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    • 2003
  • Steady and unsteady cavitation characteristics of turbopump inducer were investigated in this paper. To see the effect of blade angle on the inducer performance, three inducers with inlet tip blade angle of $7.8^{\circ},\;7.0^{\circ},\;6.1^{\circ}$, respectively, were tested. For $7.8^{\circ},\;7.0^{\circ}$ inducers in the non-cavitating condition, head decreased linearly with flow rate, but head-flow rate curve had a dip at the flow coefficient ${\Phi}=0.065\;for\;6.1^{\circ}$ inducer. Rotating cavitation and cavitation surge were found in the $7.8^{\circ},\;7.0^{\circ}$ inducers in the cavitation tests. During the rotating cavitation one cell rotated at the same rotational speed as that of the inducer. The cavitation surge did not rotate and the oscillating frequency was $7{\sim}20\;Hz$. From the curve of the critical cavitation number versus flow rate, it was found that the steady cavitation performance of $6.1^{\circ}$ inducer was much lower than that of $7.8^{\circ},\;7.0^{\circ}$ inducers.

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Experimental Investigations on Upper Part Load Vortex Rope Pressure Fluctuations in Francis Turbine Draft Tube

  • Nicolet, Christophe;Zobeiri, Amirreza;Maruzewski, Pierre;Avellan, Francois
    • International Journal of Fluid Machinery and Systems
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    • v.4 no.1
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    • pp.179-190
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    • 2011
  • The swirling flow developing in Francis turbine draft tube under part load operation leads to pressure fluctuations usually in the range of 0.2 to 0.4 times the runner rotational frequency resulting from the so-called vortex breakdown. For low cavitation number, the flow features a cavitation vortex rope animated with precession motion. Under given conditions, these pressure fluctuations may lead to undesirable pressure fluctuations in the entire hydraulic system and also produce active power oscillations. For the upper part load range, between 0.7 and 0.85 times the best efficiency discharge, pressure fluctuations may appear in a higher frequency range of 2 to 4 times the runner rotational speed and feature modulations with vortex rope precession. It has been pointed out that for this particular operating point, the vortex rope features elliptical cross section and is animated of a self-rotation. This paper presents an experimental investigation focusing on this peculiar phenomenon, defined as the upper part load vortex rope. The experimental investigation is carried out on a high specific speed Francis turbine scale model installed on a test rig of the EPFL Laboratory for Hydraulic Machines. The selected operating point corresponds to a discharge of 0.83 times the best efficiency discharge. Observations of the cavitation vortex carried out with high speed camera have been recorded and synchronized with pressure fluctuations measurements at the draft tube cone. First, the vortex rope self rotation frequency is evidenced and the related frequency is deduced. Then, the influence of the sigma cavitation number on vortex rope shape and pressure fluctuations is presented. The waterfall diagram of the pressure fluctuations evidences resonance effects with the hydraulic circuit. The influence of outlet bubble cavitation and air injection is also investigated for low cavitation number. The time evolution of the vortex rope volume is compared with pressure fluctuations time evolution using image processing. Finally, the influence of the Froude number on the vortex rope shape and the associated pressure fluctuations is analyzed by varying the rotational speed.