• Title/Summary/Keyword: CO tube

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OPTIMAL PROCESSING AND SYSTEM MANUFACTURING OF A LASER WELDED TUBE FOR AN AUTOMOBILE BUMPER BEAM

  • Suh, J.;Lee, J.H.;Kang, H.S.;Park, K.T.;Kim, J.S.;Lee, M.Y.;Jung, B.H.
    • International Journal of Automotive Technology
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    • v.7 no.2
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    • pp.209-216
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    • 2006
  • A study has been conducted for an optimal processing and an apparatus for manufacturing a laser welded tube for one-body formed bumper beam. The tube dimensions used in calculation were the thickness of 1.4 mm, the diameter of 105.4 mm and the length of 2000 mm. The tube was formed of a cold rolled high strength steel plate(tensile strength of 600 MPa). The two-roll bending method was the optimal tube forming process in comparison with the UO-bending method, the bending method on the press brake, the multi-step continuous roll-forming method and the 3-roll bending method. Monitoring of the welding quality was conducted and the seam tracking along the butt-joint lengthwise to the tube axis was also examined. The longitudinal butt-joint was welded by using a $CO_2$ laser welding machine equipped with a seam tracker and a plasma sensor. The $CO_2$ laser tube welding machine could be used for precise seam tracking and real-time monitoring of the welding quality. As a result, the developed laser welded tube could be used for a one-body formed automobile bumper beam.

Production of Laser Welded Tube for Automobile Bumper Beam from 60kgf/$\textrm{mm}^2$Grade Steel Sheet (60kgf/$\textrm{mm}^2$급 자동차 범퍼빔용 레이저 용접 튜브 제조기술 및 장치연구)

  • Seo, Jung;Lee, Je-Hoon;Kim, Jong-Soo;Kim, Jung-O;Kang, Hee-Sin;Lee, Moon-Yong;Jung, Byung-Hoon
    • Journal of the Korean Society for Precision Engineering
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    • v.21 no.7
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    • pp.136-144
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    • 2004
  • Optimal process and system to produce the laser welded tube for one body formed bumper beam are studied. The calculated size of tube is a thickness of 1.4mm, diameter of 105.4mm and length of 2000mm. The tube is shaped from a cold rolled high strength steel sheet(tensile strength: 60kgf/$\textrm{mm}^2$ grade). Two roll bending method is the optimal tube shaping process compared to UO-bending, bending on press brake, multi-step continuous roll forming and 3 roll bending methods. Weld quality monitoring and seam tracking along the butt-joint lengthwise to the tube axis are also studied. The longitudinal butt-joint is welded by the $CO_2$ laser welding system equipped with a seam tracker and plasma sensor. The constructed $CO_2$laser tube welding system can be used for the precision seam tracking and the real-time monitoring of weld quality. Finally, the obtained laser welded tube can be used for one-body formed automobile bumper beam.

A Study on Roll Reduction Devices for FPSOs (FPSO의 횡요 감쇠 장치에 대한 고찰)

  • PARK IN-KYU;YANG JIN-HO;SHIN HYUN-SOO
    • Proceedings of the Korea Committee for Ocean Resources and Engineering Conference
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    • 2004.05a
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    • pp.30-35
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    • 2004
  • Several roll motion reduction devices are reviewed and suggested for the application in FPSO. The firstly suggested solution is the shape of the bilge. The next is a bilge keel. The last suggestion is the ART (anti-rolling tank). Typical U-tube type ART is designed for a FPSO and examined extensively by model experiment. The model section was made of transparent acryl. Free decay test, forced oscillation test and wave test were carried out at a two-dimensional wave flume. U-tube type ART is effective only when the natural periods of ART and ship are same. Therefore, the divided U-tube type ART with split plate is suggested for the reduction of the roll motion of a FPSO over the wide range of the roll period.

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Development of Ceramic Arc-tube by the PIM Process

  • Rhee, Byung-Ohk;Choi, Seung-Chul;Park, Jeong-Shik;Kim, Byoung-Kyu;Kim, Hyung-Soo;Kim, Sang-Woo
    • Proceedings of the Korean Powder Metallurgy Institute Conference
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    • 2006.09a
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    • pp.205-206
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    • 2006
  • A ball-shape alumina arc-tube for low-wattage lamp was developed by the PIM process. An ultra high purity translucentgrade alumina powder was used. In injection molding process, a hot-runner type mold was developed. The translucent-grade alumina powder was extremely sensitive to contamination so that the injection molding condition and atmosphere control in the furnace should be taken care of with extreme caution. Contamination sources were pinpointed with EPMA. The arc-tube was molded in half and two halves were bonded in the middle by a new bonding technique at room temperature developed in this study.

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Cooling Heat Transfer Characteristics of $CO_2$ on Tube Geometry of Inclined Helical Coil Type Gas Coolers (경사진 헬리컬 코일형 가스냉각기의 관형상에 따른 $CO_2$ 냉각 열전달 특성)

  • Son, Chang-Hyo;Oh, Hoo-Kyu
    • Korean Journal of Air-Conditioning and Refrigeration Engineering
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    • v.19 no.9
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    • pp.640-646
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    • 2007
  • The cooling heat transfer coefficient of $CO_2$ (R-744) for tube and coil diameter (CD), inclined angle of tube and coil pitch of inclined helical coil type copper tubes were investigated experimentally. The main components of the refrigerant loop are a receiver, a variable-speed pump, a mass flow meter, a pre-heater and a inclined helical coil type gas cooler (test section). The test section consists of a smooth copper tube of 2.45 and 4.55 mm inner diameter (ID). The refrigerant mass flukes were varied from 200 to 800 [$kg/m^2s$] and the inlet pressures of gas cooler were 7.5 to 10.0 [MPa]. The heat transfer coefficients of $CO_2$ in inclined helical coil tube with 2.45 mm ID are $5{\sim}10.3%$ higher than those of 4.55 mm. The heat transfer coefficients of 41.35 mm CD are $8{\sim}32.4%$ higher than those of 26.75 mm CD. Comparison between $45^{\circ}\;and\;90^{\circ}$ of coil angle, the heat transfer coefficients of $45^{\circ}$ are higher than those of $90^{\circ}$. For coil pitch of gas cooler, the heat transfer coefficients of inclined helical coil gas cooler with coil pitch of 5 mm are similar to those of 10 and 15 mm.

A study on manufacturing of laser welded tube from 60kgf/$mm^2$Grade Steel Sheet for one-body forming (60kgf/$mm^2$급 일체화 성형용 레이저 용접 튜브 제조에 관한 연구)

  • Seo, Jung;Lee, Je-Hoon;Kim, Jung-Oh;Kang, Hee-Sin;Lee, Mun-Yong;Jung, Byung-Hoon
    • Proceedings of the KWS Conference
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    • 2003.11a
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    • pp.18-20
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    • 2003
  • Optimal processing and system to produce the laser welded tube for one body formed bumper beam are studied. The calculated size of tube is a thickness of 1.4mm, diameter of 105.4mm and length of 2000mm. The tube is shaped from cool rolled high strength steel sheet(tensile strength: 60kgf/$\textrm{mm}^2$ grade). Two roll bending method is the optimal tube shaping process compared to UO-bending, bending on press brake, multi-step continuous roll forming and 3 roll bending methods. Weld quality monitoring and seam tracking along the butt-joint lengthwise to the tube axis are also studied. The longitudinal butt-joint is welded by the $CO_2$ laser welding system equipped with a seam tracker and plasma sensor. The constructed $CO_2$ laser tube welding system can be used for the precision seam tracking and the real-time monitoring of weld quality. Finally, the obtained laser welded tube can be used for one-body formed automobile bumper beam.

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Bi2212 Tube Characteristics for SCFCL (한류기용 Bi2212 튜브의 특성)

  • Lee, N.I.;Jang, G.E.;Oh, I.S.;Park, G.B.
    • Progress in Superconductivity
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    • v.7 no.2
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    • pp.174-178
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    • 2006
  • For the practical application on SCFCL, Bi2212 tubes were fabricated by Centrifugal Forming Process (CFP) in terms of many different processing parameters. Typical sizes of tubes were 60, 150 mm in length and 2.5, 3.5, 4.8 mm in thickness. Initially powder was melted by induction heating. The optimum range of melting temperatures and preheating temperature were $1100^{\circ}C$ and $500^{\circ}C$ for 30min respectively. The nominal mold rotating speed was around 1000 RPM. A tube was annealed at $840^{\circ}C$ for 80 hours in oxygen atmosphere. The tube of 50mm x 70mm x 2.5mm, rotated with 1000 RPM showed $I_c=890\;A\;and\;T_c=80$. It was found that the tube processed with faster rate of mold rotation speed, thinner tube thickness and shorter tube length shows better electric characteristics as compared with the tube normally processed. In order to study the uniformity heat and fluid flow analysis tool was adopted along tube.

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Analysis of Mechanism for Diffusion of Incomplete Combustion Gas Released from Domestic Gas Boiler (가정용 보일러의 불완전연소가스 누출확산 메커니즘 해석)

  • Kang, Seung-Kyu;Choi, Kyung-Suhk;Yoon, Joon-Yong
    • Proceedings of the KSME Conference
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    • 2008.11b
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    • pp.2868-2873
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    • 2008
  • Carbon Monoxide(CO) poisoning accident is higher than any other gas accident in the rate of deaths/incidents. In the last five years, 36 people died and 104 were wounded because of carbon monoxide poisoning accident. Most of these CO poisoning accidents were caused by defective exhaust tube in the old gas boiler and multi-use facility. In this study, the spread of incomplete combustion gas(CO) released from leakage hole of exhaust tube was analyzed by computational flow modeling and concentration measuring test. CO gas leaked form exhaust tube in a building was highest concentrated near the ceiling and formed the circular currents along the walls. Through these experiments and simulation, the reasonable installation location of carbon monoxide alarm was made certain and suggested.

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Pressure Drop Characteristics of Supercritical $CO_2$ in a Helically Coiled Tube (헬리컬 코일관 내 초임계 $CO_2$의 압력강하 특성)

  • Yu, Tae-Geun;Kim, Dae-Hui;Roh, Geon-Sang;Ku, Hak-Geun;Oh, Hoo-Kyu
    • Proceedings of the Korean Society of Marine Engineers Conference
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    • 2005.06a
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    • pp.216-221
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    • 2005
  • The heat transfer coefficient and pressure drop during gas cooling process of carbon dioxide in a helically coiled tube were investigated experimentally. The experiments were conducted without oil in the refrigerant loop. The main components of the refrigerant loop are a receiver, a variable speed pump, a mass flowmeter, a pre-heater, a gas cooler(test section) and an isothermal tank. The test section is a double pipe type heat exchanger with refrigerant flowing in the inner tube and water flowing in the annulus. It was made of a copper tube with the inner diameter of 4.85 [mm], the outer diameter of 6.35 [mm] and length of 10000 [mm]. The refrigerant mass fluxes were 200${\sim}$600 [kg/$m^2$s] and the average pressure varied from 7.5 [MPa] to 10.0 [MPa]. The main results were summarized as follows: The heat transfer coefficient of supercritical $CO_2$ increases, as the cooling pressure of gas cooler decreases. And the heat transfer coefficient increases with the increase of the refrigerant mass flux. The pressure drop decreases in increase of the gas cooler pressure and increases with increase the refrigerant mass flux.

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Verification experiment of a ground source multi-heat pump at heating season (지열원 멀티 히트펌프의 동절기 난방성능에 관한 실증 연구)

  • Choi, Jong-Min;Lim, Hyo-Jae;Kang, Shin-Hyung;Choi, Jae-Ho;Moon, Je-Myung;Kwon, Young-Seok;Kwon, Hyung-Jin;Kim, Rock-Hee
    • Proceedings of the SAREK Conference
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    • 2009.06a
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    • pp.52-57
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    • 2009
  • This paper describes the multi-heat pumps applied in an ground source heat pump system for an actual building. The performance of a ground source multi-heat pump installed in the field was investigated at heating season. The average COP of the systems with single U-tube and double tube type GLHXs were 4.8 and 5.0, respectively. It is needed to investigate the long term performance of double tube type GLHX, because the reduction of inlet temperature of OD HX for this GLHX was larger than it for U-tube GLHX.

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