• 제목/요약/키워드: Boiler tube

검색결과 198건 처리시간 0.104초

300 MW 급 유동층보일러에서 적정 층 물질량 산정 (Allowable Amount of Bed Inventory in a 300 MW Class Circulating Fluidized Bed Boiler)

  • 김우용;유호선
    • 플랜트 저널
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    • 제14권2호
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    • pp.33-38
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    • 2018
  • 본 연구에서는 순환유동층보일러의 베드가 과열되어 층 물질의 소결이 발생하고 노 내 유동물질에 의해 보일러튜브가 마모 되는 것을 최소화하기 위하여, 노 하부 베드의 층 물질량 조정을 통한 베드 온도 변화를 실험적으로 연구하였다. 실험은 300MW급 순환유동층보일러인 여수화력 2호기를 대상으로 하였으며 터빈출력, 석탄소비량, 공기량 등을 고정한 상태에서 층 물질 양을 감소시켜 베드 압력을 설계값 4.5KPa에서 2.5KPa까지 감소시켰다. 결론적으로 층 물질 양을 적정하게 줄이면 베드 온도가 저하 되나, 지속적으로 저하되지 않는 것을 확인 하였으며, 베드 압력 3.0KPa, 즉 베드 물질량 110 톤을 변곡점으로 하여 베드 온도는 상승하기 시작하였다. 층 물질량이 충분히 많은 상태에서, 층 물질량이 감소되면 베드 온도는 저하되며, 층 물질량이 적정량 보다 적으면 노 내 유동물질의 순환량 감소로 베드 온도는 상승함을 알 수 있었다. 또한 유동층보일러에서 베드 온도 변화는 단순히 층 물질의 양 뿐만 아니라, 보일러 용량 및 연료의 성상 등에 따라 변화 추이가 매우 다양하게 나타난다는 것을 알 수 있었다.

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음향방출을 이용한 보일러튜브 누설평가 (Leak Detection and Evaluation for Power Plant Boiler Tubes Using Acoustic Emission)

  • 이상국
    • 비파괴검사학회지
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    • 제24권1호
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    • pp.45-51
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    • 2004
  • 발전소 보일러튜브는 장시간 동안 고온고압하의 기혹한 조건으로 운전됨에 따라 크리프, 열피로와 같은 각종 열화에 의해 누설손상이 발생하고 있다. 이러한 누설손상을 실시간 감시하고 진단하기 위하여 음향방출기술을 이용한 현장적용 연구를 수행하였다. 또한 고장예측 진단기술, 튜브의 수명관리 및 설비 감시에 활용할 수 있도록 음향방출 진단시스템을 개발하여 현장에 설치하고, 보일러 운전상태에 따른 신호측정 및 평가, 누설위치 판별 등에 대해 고찰하였다. 누설감지는 저주파 및 고주파대역의 누설로 구분하여 음향방출신호를 각각 측정 및 평가하였다. 현장적용 연구결과로부터 실시간으로 보일러튜브 상태감시와 누설위치 추적이 가능하였으며, 향후 본 기술을 이용하면 발전설비 안전운전과 발전소 정지에 따른 경제적 손실 예방에 크게 기여할 것으로 기대된다.

LPG 증기보일러의 배기 배출물에 미치는 요소-SCR 후처리 시스템의 영향에 관한 연구 (A Study on Effect of Urea-SCR Aftertreatment System upon Exhaust Emissions in a LPG Steam Boiler)

  • 배명환;송병호
    • 한국자동차공학회논문집
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    • 제22권3호
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    • pp.1-11
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    • 2014
  • The aim of this study is to investigate the effect of SCR reactor on the exhaust emissions characteristics in order to develop a urea-SCR aftertreatment system for reducing $NO_x$ emissions. The experiments are conducted by using a flue tube LPG steam boiler with the urea-SCR aftertreatment system. The urea-SCR aftertreatment system utilizes the ammonia converted from 17% aqueous urea solution injected in front of SCR catalyst as a reducing agent for reducing $NO_x$ emissions. The equivalence ratio, urea injection amount, ammonia slip and $NO_x$ conversion efficiency relative to boiler load are applied to discuss the experimental results. In this experiment, the average equivalence ratio is calculated by changing only the fuel consumption rate while the intake air amount is constantly fixed at $25,957.11cm^3/sec$. The average equivalence ratios are 1.38, 1.11, 0.81 and 0.57 when boiler loads are 100, 80, 60 and 40%. The $NO_x$ conversion efficiency is raised with increasing urea injection amount, and $NH_3$ slip is also boosted at the same time. Consequently, the $NO_x$ conversion efficiency relative to boiler load should be examined in combination with urea injection amount and $NH_3$ slip. The results are calculated by 89, 85, 77 and 79% for the boiler loads of 100, 80, 60 and 40%. The appropriate amount of urea injection for the respective boiler load can be not discussed by only $NO_x$ emissions, and should be determined by considering the $NO_x$ conversion efficiency, $NH_3$ slip and reactive activation temperature simultaneously. In this study, the urea amounts of 230, 235, 233 and 231 mg/min are injected at the boiler loads of 100, 80, 60 and 40%, and the final $NH_3$ slips are measured by 8.48, 5.58, 11.97 and 11.34 ppm at the same conditions. THC emission is affected by the SCR reactor under other experimental conditions except 100% engine load, and CO emission at only 40% engine load. The rest of exhaust emissions are not affected by the SCR reactor under all experimental conditions.

Flyash에 의한 STS304 재료의 내침식성 평가 (Evaluation on erosion resistance of STS304 by flyash)

  • 박해웅;이의열
    • 한국표면공학회지
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    • 제34권6호
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    • pp.575-584
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    • 2001
  • Erosion due to abrasive particles contained in gas streams from boilers has been emerged as a significant problem in the coal fired power plants. Particle erosion accounted for approximately 50% of boiler failures and especially flyash erosion was responsible for 20~30% of emergency boiler shutdowns. Particularly, because of the high ash loading and high velocity, most erosion occurs in the boiler tubes and economiser tube bank where the direction of the gas stream changes to $180^{\circ}$ .In this study, a high temperature particle erosion tester was used to evaluate erosion rate in a simulated environment. The erosion parameters such as erosion temperature, particle impact angle, particle velocity and various particle size were changed. Flyash is the combustion product of the pulverized coal, where size is ranging from 1 to $200\mu\textrm{m}$. Flyash composed of mainly SiO$_2$, $A1_2$$_O3$, and $Fe_2$$O_3$has dense spherical particles and irregular particles containing numerous pores and cavities. From the erosion tests at various conditions, the maximum erosion was experienced at impact angles of $30^{\circ}$ to $60^{\circ}$ In addition, erosion rate increased in proportional to velocity and temperature. And from the observation of the eroded surfaces, it was also concluded that 304 stainless steel was mainly eroded by extrusion-forging at high impact angle ($90^{\circ}$) and by microcutting mechanism at low impact angles ($30^{\circ}$ and $45^{\circ}$).

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분리형 히트파이프의 저발열량 연료가스 예열시스템에 대한 적용연구 (Application of a Large Scale Heat Pipe System to Preheating the Fuel Gas of Low Heating Value)

  • 박흥수;유갑종;이진호;이용국
    • 대한기계학회논문집B
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    • 제23권9호
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    • pp.1085-1097
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    • 1999
  • A separate heat pipe system capacity of 3,700kW has been developed and applied to preheating the blast furnace gas for recovery of the waste heat from boiler. The system is designed to preheat the blast furnace gas up to $126^{\circ}C$ by using tho boiler exhaust gas of which temperature is $180^{\circ}C{\sim}220^{\circ}C$. The arrangement of the fin tubes as well as the shape of the fin has been carefully determined to minimize the fouling problems. The heat pipe system was found to be stable in circulation of the working fluid and the range of the temperature variation of the preheated blast furnace gas was within $10^{\circ}C$. It was proved through a long-term test that the selected tube arrangement and the shape of the fins are proper to prevent the fouling problems and that the pay-back period of the system Is within one year.

가스보일러 코일형 열교환기의 열전달 특성에 관한 실험적 연구 (The Experimental Study on the Heat Transfer Characteristics)

  • 홍성혁;김영기;김일겸;김동춘;이창언;임장순
    • 태양에너지
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    • 제17권4호
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    • pp.57-66
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    • 1997
  • The performance of gas-fired boilers were experimentally investigated. The heat exchanger used for the experiments consisted of circular tube with longitudinal fins for the gas side and a spiral coil for the water side. The burner was located at the top of the heat exchanger, and the burned gas flowed down to the exit. The experiments carried out for different water flow rates, the heat capacities of the boiler and the number of baffle. The thermal efficiency of the upward flow was higher than that of the downward flow of the water in the heat exchanger. As the boiler capacity increased, the thermal efficiency decreased. As the number of the baffles increase, the thermal efficiency increased and the increasing rate of the efficiency decreased. The gas-side overall heat transfer coefficient was independent of the flow rate of the water. The effect of the number of the baffles on the heat transfer coefficient was greater than that of the boiler capacity.

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터보 냉동기용 핀 튜브에 관한 연구 (III) -압력 손실에 관하여- (A Study on Finned Tube Used in Turbo Refrigerator(III) -for Pressure Drop-)

  • 한규일;김시영;조동현
    • 수산해양교육연구
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    • 제6권1호
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    • pp.58-76
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    • 1994
  • Heat transfer and pressure drop measurements are made on low integral-fin tubes in turbulent water flow condition. The integral-fin tubes investigated in this paper are nominally 19mm in diameter. Eight tubes have been used with trapezoidally shaped integral-fins having fin density from 748 to 1654 fpm and 10, 30 grooves. Plain tube having same diameter as finned tube is also tested for comparison. Experiments are carried out using R-11 as working fluid. The refrigerant condensates at a saturation state of $30^{\circ}C$ on the outside tube surface cooled by coolant. The amount of noncondensable gases present in the test loop is reduced to a negligible value by repeated purging. For a given heat input to the boiler and given cooling water flow rate, all test data are taken on steady state. The heat transfer loop is used for testing single long tubes and cooling water is pumped from a storage tank through filters and flowmeters to the horizontal test section where it is heated by steam condensing on the outside of the tube. The pressure drop across the test section is measured by means of pressure gauge and manometer. Each tube tested is cleaned with sodium dichromate pickling solution and well rinsed with water prior to installation in the test section. The results obtained in this study is as follows : 1. Based on inside diameter and nominal inside area, heat transfer of finned tube is enhanced up to 4 times as that of a plain tube at constant Reynolds number and up to 2 times at constant pumping power. 2. Friction factors are up to 1.6~2.1 times those of plain tube. 3. At a given Reynolds number, Nusselt number decrease with increasing pitch to diameter. 4. The constant pumping power ratio for low integral-fin tubes increase directly with the effective area to the nominal area ratio, and with the effective area diameter ratio.

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석탄연소중 발생되는 보일러 튜브의 화염측 부식특성 (Fireside Corrosion Characteristics in Coal-Fired Boiler Tube)

  • 김태형;서상일;박호영;김영주
    • 한국연소학회:학술대회논문집
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    • 한국연소학회 2006년도 제33회 KOSCO SYMPOSIUM 논문집
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    • pp.276-281
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    • 2006
  • Although fireside corrosion of heat transfer surfaces in coal fired steam generators has been a problem to some extent for a number of tears, with the advent of low NOx firing systems these surfaces can be exposed to conditions that will exacerbate wastage rates. Numerous reports of waterwall wastage in coal fired boilers have appeared in the literature. It is believed that wastage results both from gaseous phase attack of metal surfaces and from deposition of ash and unburned fuel. Gaseous phase attack is known to occur in the presence of reducing sulfur species such as $H_2S$ and in the presence of fuel chlorine. The highest wastage rates are thought to be due to deposition of unoxidized material and the presence of fuel chlorine. Localized wall and near wall conditions that may exacerbate wastage include reducing conditions, high temperatures, high heat fluxes, and a high fraction of unoxidized material deposited. So, this study is directed at developing an advanced corrosion model in coal-fired utility boilers.

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바이패스 시스템 체용 유무에 따른 증기 터빈제어 비교 (A comparison of steam turbine control systems according to adoption of turbine bypass system)

  • 최인규;김종안
    • 대한전기학회:학술대회논문집
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    • 대한전기학회 2000년도 하계학술대회 논문집 D
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    • pp.2342-2344
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    • 2000
  • Many years ago, most of thermal power plants built in this country were of subcritical pressure, of medium or small size, of constant pressure operation, of drum type steam generator. But, nowadays, almost all of them were of high efficiency, of supercritical pressure, of great capacity(about 500MW), of sliding pressure operation, of once through type steam generator. Presently built once through boiler introduces turbine bypass systems to variable pressure operation which eliminates unexpected materials in boiler tube during startup, minimizes fuel loss by short startup period, eventually improves total efficiency and power system stability

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저온온수 모세유관 바닥복사 난방시스템의 성능에 관한 실험적 연구 (Experimental Study on a Low-Temperature Hot Water Capillary Radiant Floor Heating System)

  • 조진균;박병용;이용준;정원호
    • 설비공학논문집
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    • 제30권2호
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    • pp.68-82
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    • 2018
  • Radiant floor heating systems with capillary tubes are energy saving systems in which hot water is circulated into capillary tube with a small diameter. In this study, the heating performance of capillary tube system is investigated in an experimental study and a simulation model. The results of the study showed that, the capillary tube radiant floor heating system maintains a more stable floor surface temperature in comparison a PB pipe system. In terms of energy consumption, the capillary tube radiant floor heating system proved to be more efficient than the PB pipe heating system at $40^{\circ}C$ of low temperature hot water supply. The difference between water temperature and room temperature can be held low for heating which saves energy. Low temperature radiant floor heating system with capillary tubes have significant advantages such as health improvement, low energy cost, optimum use of heat source(boiler) and higher operational efficiency.