• Title/Summary/Keyword: Assembly Test

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Hydrodynamic Performance Test of a Turbopump Assembly (터보펌프 조립체의 수력 성능 시험)

  • Hong, Soon-Sam;Kim, Dae-Jin;Kim, Jin-Sun;Kim, Jin-Han
    • Transactions of the Korean Society of Mechanical Engineers B
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    • v.32 no.4
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    • pp.249-254
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    • 2008
  • Hydrodynamic performance test of a turbopump for a liquid rocket engine is carried out. The turbopump is composed of an oxidizer pump, a fuel pump and a turbine, and the two pumps are driven by the turbine. In the test, water is used for the pumps as working media and air is used for the turbine. Performance parameters of pumps and a turbine are drawn, and a power balance between the pumps and the turbine are calculated. The calculation shows a good power balance, which implies that the pump component tests, the turbine component test and the assembly test are reliably performed. At the starting period of the test, pressure rise-flow rate curve of a pump gradually approaches the ideal curve which could be obtained by very slow starting.

KOMPSAT-2 RF COMPATIBILITY TEST FOR S-BAND

  • Cho Seung-Won;Youn Young-Su;Choi Jong-Yeon;Choi Seok-Weon
    • Bulletin of the Korean Space Science Society
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    • 2004.10b
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    • pp.344-346
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    • 2004
  • KOMPSAT-2 (Korea Multi Purpose Satellite 2) which is scheduled to launch in 2005 year will communicate with KARI TTC (Tracking, Telemetry, and Command) station flying along sun synchronous orbits (685 km). The command from KARI TTC passes S-band omni-antenna, RF assembly, and transponder and finally reachs OBC (On Board Computer). The telemetry from KOMPSAT-2 arrives at KARI TTC through inverse procedure. In this paper, RF compatibility test between KOMPSAT-2 and KARI TTC station is demonstrated. RF interface for this test was established through real space and uplink signal test and downlink signal test and uplink & downlink signal test were performed.

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Development of Hydraulic Device Performance Test Equipment Automation Process (유압 디바이스 성능 검사 장비 자동화 공정 개발)

  • Kim, Hong-Rok;Chung, Won-Jee;Seol, Sang-Seok;Park, Sang-Hyeok;Lee, Kyeong-Tae
    • Journal of the Korean Society of Manufacturing Process Engineers
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    • v.19 no.10
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    • pp.74-80
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    • 2020
  • Crawler-type hydraulic devices facilitate forward and backward driving of construction equipment by converting power into mechanical energy. The existing hydraulic device performance test process is time- and labor-intensive. This study aims to improve efficiency and productivity by automating the hydraulic device production performance test processes, which have been separately conducted so far. We also used SolidWorksⓇ, a 3D modeling program, and ANSYSⓇ, a structural analysis tool, for structural analysis and to verify the suitability of fixing pins required for connecting a hydraulic device to performance test equipment. Our results that employing an automated hydraulic device performance test process improves efficiency.

3D Packaging : Where All Technologies Come Together

  • Kim YC
    • Proceedings of the International Microelectronics And Packaging Society Conference
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    • 2006.02a
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    • pp.139-151
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    • 2006
  • [ $\bullet$ ] 3D is proliferating in all package types $\bullet$ Thin packages challenge all assembly technologies $\bullet$ Package assembly and test are closely coupled and design for testability is imperative to success

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The Vibration Study on Car Compact Disk Player (자동차탑재용 컴펙트 디스크 플레이어의 진동특성 연구)

  • Lee, Tae-Keun;Kim, Byong-Sam
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2006.05a
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    • pp.283-288
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    • 2006
  • This study developes the vibration model to estimate the vibration energy of damper/spring assembly(mainbase assembly) for car CD player, and this model is verified by experiment. From frequency response, response, we investigate the natural frequency and mode shape in the up/down direction. In order to determine the analysis frequency band, we investigate the excitation frequency from the vehicle test. As the characteristics of damper and spring is changed, we carry out the vibration test(transmissibility) and investigate the change of transmissibility.

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A Study on the Quality Test of Grinding Disk Assembly for Crushing Material in Secondary Battery (이차전지 원료 해쇄용 Grinding Disc Assembly 품질 시험에 관한 연구)

  • Sang-Pil Han;Dong-Hyuk Lee
    • Design & Manufacturing
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    • v.17 no.2
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    • pp.42-46
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    • 2023
  • Currently, fossil resources are depleting rapidly. We are looking for energy to replace fossil fuels. They are trying to use electricity to replace internal combustion locomotives. Secondary battery raw materials and chemical additives are pulverized by the high-speed rotation of the grinding disc of the Classifier Separator Mill. Grinding Disc Assembly requires characteristics to withstand abrasion, corrosion, high-speed rotational force and impact. Domestic and foreign grinding discs were analyzed through abrasion resistance, hardness, bending strength, and tensile adhesion strength tests.

Development of Torsion Bar for Antiroll-Bar Assembly for Express Train (고속철도용 안티롤바 어셈블리의 토션바 개발)

  • Tominaga, Yasutoshi;Pyun, Young-Sik;Kim, Dong-Il;Choe, Do-Hyun
    • Transactions of the Korean Society of Mechanical Engineers A
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    • v.36 no.9
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    • pp.979-984
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    • 2012
  • An antiroll-bar assembly is a precision component that is designed to control the rolling of railway cars. It is important for ensuring a safe and comfortable ride. A torsion bar is the main part of the antiroll-bar assembly. Now, this part is classified as a consumable, and it is imported into Korea from France. Therefore, there is a strong need to domestically develop a torsion bar suitable for Korean conditions and to reduce cost and improve quality. In this study, an antiroll bar is developed, and it is analyzed and tested by using a road histogram measured on Korean railroads. This bar shows satisfactory results in a comparison with the imported bar. It has a novel design featuring a ring cover made of SUS steels to prevent the corrosion of the torsion bar. Its safety is examined through CAE analysis and wear tests. It is found that its design does not result in a significant difference in static and fatigue safety. Two different SUS steels were investigated in terms of their wear resistance, and the best one was adopted.

Erection Capability of Heavy Precast Frames with Metal Plates using Wet Concrete for Tolerance (톨러런스기반 플레이트 접합 장치를 사용한 고중량 RC보의 설치 성능)

  • Hong, Won-Kee;Nguyen, Van Tien;Nguyen, Manh Cuong;Nkundimana, Eric
    • Proceedings of the Korean Institute of Building Construction Conference
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    • 2021.05a
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    • pp.12-13
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    • 2021
  • Methods for the manufacture, erection, and assembly of heavy frame modules were proposed. Interferences among precast members were prevented by using bolted metal plates for dry precast beam-to-column joints during assembly with a clearance for tolerance implementing grouted concrete filler plates instead of metal filler plates. Clearances for tolerances were provided to avoid conflictions among components during erection phases. These gaps were, then, grouted by high-strength mortar. The constructability of new connections of a beam-to-column joint using bolted metal plates for precast structures was examined using a full-scale assembly test in which practical observations indicated that members could be aligned and placed accurately in both horizontal and vertical directions, leading to a fast and convenient assembling. Bolt holes of the endplate were properly aligned using couplers with 30 mm fastened length embedded in the columns. The assembly test demonstrated the erection safety and structural stability of the proposed joints that were without filler plates when they were subjected to heavy loads at the time of their erection. The facile and rapid assembly of precast beam-to-column connections with a 30 mm tolerance was observed. The proposed assembly method is rapid, sustainable, and resilient, replacing the conventional methods of concrete frame construction, offering a connection that can be used in constructing infrastructure, such as buildings and pipe-rack frames.

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Interpretation of AE Signals from Rocket Motor Case Assembly (로켓 연소관 조립체의 음향방출 신호해석)

  • Rhee, Sang-Ho;Hwang, Tae-Kyong;Mun, Sun-Il
    • Journal of the Korean Society for Nondestructive Testing
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    • v.23 no.5
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    • pp.488-496
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    • 2003
  • To establish nondestructive test method for rocket motor assembly with rubber and aerospace composite materials, practicable quality control acoustic emission test method is presented. Structural analysis for motor assembly is performed by ABAQUS code and analysis output result is confirmed by strain gage and AE data. Various specimens were tested and analyzed using strain gage and acoustic emission data. The hit rate of acoustic emission was closely related with case/rubber debonding. This report also describes practicable acoustic emission nondestructive method for evaluating motor case assembly quality assurance in the industrial field.

Effects of Underfills on the Dynamic Bending Reliability of Ball Grid Array Board Assembly (Ball Grid Array 보드 어셈블리의 동적굽힘 신뢰성에 미치는 언더필의 영향)

  • Jang, Jae-Won;Bang, Jung-Hwan;Yoo, Se-Hoon;Kim, Mok-Soon;Kim, Jun-Ki
    • Korean Journal of Materials Research
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    • v.21 no.12
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    • pp.650-654
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    • 2011
  • In this paper, the effects of conventional and newly developed elastomer modified underfill materials on the mechanical shock reliability of BGA board assembly were studied for application in mobile electronics. The mechanical shock reliability was evaluated through a three point dynamic bending test proposed by Motorola. The thermal properties of the underfills were measured by a DSC machine. Through the DSC results, the curing condition of the underfills was selected. Two types of underfills showed similar curing behavior. During the dynamic bending reliability test, the strain of the PCB was step increased from 0.2% to 1.5% until the failure circuit was detected at a 50 kHz sampling rate. The dynamic bending reliability of BGA board assembly using elastomer modified underfill was found to be superior to that of conventional underfill. From mechanical and microstructure analyses, the disturbance of crack propagation by the presence of submicron elastomer particles was considered to be mainly responsible for that result rather than the shear strength or elastic modulus of underfill joint.