• Title/Summary/Keyword: 검증장치

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A Development of on Electronic Starter for Single Phase Induction Motor (단상 유도전동기의 전자식 기동장치 개발)

  • Jeong, Hyeung-Woo;Kim, Dong-Hee;Baik, Won-Sik;Kim, Min-Huei;Song, Hyun-Jig
    • Journal of the Korean Institute of Illuminating and Electrical Installation Engineers
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    • v.22 no.5
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    • pp.73-79
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    • 2008
  • This paper presents a simple electronic starter for single phase induction motor (SPIM). It replaces the centrifugal switch in the auxiliary winding circuit of the capacitor start type SPIM. The electronic starter observes the auxiliary winding voltage, and disconnects the auxiliary winding when the motor gets close to its rated speed. Because of its possibly fluttering contacts of the centrifugal switch which mounted on the conventional SPIM, the reliability of SPIM can be reduced. Developed new electronic starter has no mechanical contacts. Therefore, the reliability and the performance of SPIM can be improved. The operational principle of the proposed electronic starter is explained, and illustrated with experimental results.

An Experimental Study on the Structural Vibration Control Using Semi-Active Orificed Fluid Dampers (반능동형 오리피스 유체댐퍼를 이용한 구조물 진동제어에 관한 실험적 연구)

  • 문석준;김병현;정종안
    • Journal of the Earthquake Engineering Society of Korea
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    • v.8 no.2
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    • pp.55-62
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    • 2004
  • In general, control performance of the active control system is superior to that of the passive control devices. However, the active system require a large amount of external energy to operate the actuators. Semi-active control systems maintain the reliability of the passive control systems while taking advantage of the adjustability of the active control system. In this research, a semi-active orificed fluid damper having the capacity of about 2 tons was designed and fabricated. It is a two-stage damper with normally open solenoid valve. A series of tests was performed to grasp its performance characteristics. It was also applied to a 6-story steel structure subjected to random and seismic excitations for the confirmation of its validity on structural vibration absorption.

An Analytical Study on Control Algorithm for the Precise Position Control of the Actuator System (구동장치의 정밀한 위치제어를 위한 구동제어기법에 대한 해석적 연구)

  • Ahn, Wongeun
    • Journal of the Korean Society of Propulsion Engineers
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    • v.20 no.4
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    • pp.19-25
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    • 2016
  • Using a actuator to which the motor and the gear is applied to the I-PD control method and a dual-loop system to carry out precise position control. I-PD control algorithm performs an operation to reduce the overshoot in the transient response. Accordingly, the actuator obtains a precise position tracking result. Also it utilizes two sensors and dual loops. It reduces the adverse effect on the precise position control that may occur by the end play of the gear train. In this paper, we uses the actuator model applying the BLDC motor and gear in order to determine the position tracking result by the dynamic characteristic change. It was verified by the simulation results.

Verification and Analysis of Characteristics of Mechanical Pulsation for Combustion Stability Study in a Model Chamber (모형 연소기의 연소 불안정성 연구용 섭동 장치의 기능 검증 및 분석)

  • Min, Yong-Ho;Sohn, Chae-Hoon
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2012.05a
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    • pp.28-30
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    • 2012
  • A mechanical pulsator is manufactured for study of combustion instabilities in a model chamber with impinging-jet injectors. Artificial disturbance is generated by the device and thereby, artificial instability can be examined experimentally. A sample F(fuel)-O(dxidizer)-O-F impinging-jet injector is adopted for the test. The model chamber was designed based on the methodologies proposed in the previous work regarding geometrical dimensions and operating conditions. Pressure fluctuation data, which is obtained from the dynamic pressure transducers installed in combustion chamber, is analyzed.

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Development of a Synchronization Test System for a Variable Nozzle (가변노즐의 동기화시험장치 개발)

  • Park, Dong-Chang;Lee, Sang-Youn;Lee, Ju-Young;Yun, Su-Jin;Cho, Sung-Won;Youn, Hyun-Gul
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2011.04a
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    • pp.130-131
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    • 2011
  • In the present work, a synchronization test system for variable nozzle is described. Variable nozzles are used to enhance the effectiveness of aircraft engines at various altitudes. The synchronization test system was developed to verify the dynamic characteristics and synchronization of variable nozzle mechanism including flaps. The system with a variable nozzle was analyzed, before its fabrication, by a multi-body dynamics analysis software RecurDyn. The newly developed test system is being used to show the synchronization capability of a variable nozzle system.

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Performance Analysis of a Pulse Separation Device for a F-type Multi-Pulse Rocket Motor (F형 다중펄스 로켓모타 적용 펄스분리장치 특성 분석)

  • Lee, Dong-Won;Lee, Won-Bok;Kim, In-Sik;Lee, Bang-Eop
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2012.05a
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    • pp.24-27
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    • 2012
  • In this study, the full scale flight type Dual-Pulse Rocket Motor(DPRM) with the bulkhead type Pulse Separation Device(PSD) was designed, manufactured, and fire-tested. The bursting time and pressure of PSD were analyzed by the pressure, thrust and vibration results of static fire tests and ablation of PSD was measured with 3-D coordinate measuring machine. As a result, PSD requirements, bursting conditions and thermal safety, were satisfied.

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Bursting Performance Analysis of a Pulse Separation Device for a Rocket Motor (추진기관 적용 펄스분리장치의 파열특성 분석)

  • Lee, Dong-Won;Lee, Won-Bok;Kim, In-Sik;Kim, Won-Hoon
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2011.04a
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    • pp.245-248
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    • 2011
  • A multi pulse rocket motor(MPRM) has several advantages compared to the single one. The range and the terminal velocity of the guided missile can be remarkably increased by the application of the pulse separation device(PSD) to the solid rocket motor which resulted in appropriate thrust distribution. In this study, the full scale heavy type dual pulse rocket motor with the bulkhead type PSD was designed, manufactured, and fire-tested. The bursting time and pressure of PSD were analyzed by the pressure, thrust and vibration results of static fire tests. As a result, the design requirement was verified that bursting pressure is lower than 30% of 2nd pulse operating pressure.

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Design and Analysis of Test Facility for the Experiment of Transpiration Cooling in Hot-flow Condition (고온유동 조건의 분출냉각 실험을 위한 시험장치의 설계 및 해석)

  • Lee, Jungmin;Na, Jaejeong;Kang, Kyoungtaik;Kwon, Minchan;Hwang, Kiyoung
    • Journal of the Korean Society of Propulsion Engineers
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    • v.17 no.2
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    • pp.46-56
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    • 2013
  • The test facility with hot-air supply system is required to develop transpiration cooling materials and experimentally evaluate its performance. In the study, the facility consists of an arc-plasma generator, plenum chamber suppling cold air, and test section was designed and an internal flow analysis was executed. From CFD results, it was confirmed that the designed plenum chamber thermally safeties and ideally mixes with plasma gas and cold air in the chamber. In addition, validity of design for supplying homogeneous flow to the test section was confirmed by this analysis.

Input Voltage Selection Methodology to Improve Power Transfer Efficiency of Half-Bridge Series Resonant Inverter Employing High Turn-numbered Coil for Induction Heating Application (높은 턴 수의 코일을 탑재한 유도 가열 장치용 하프 브릿지 인버터의 전력 변환 효율 향상을 위한 입력전압 선정 기법)

  • Jin, Juil;kim, Mina;Jung, Jee-Hoon
    • Proceedings of the KIPE Conference
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    • 2019.07a
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    • pp.156-158
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    • 2019
  • 낮은 저항 용기를 가열할 수 있는 유도 가열 장치는 유도가열 장치용 하프 브릿지 직렬 공진형 인버터의 높은 입력 전압과 높은 턴 수의 코일을 통해 낮은 저항의 용기를 가열한다. 그러나 자성체 용기는 높은 턴 수의 코일에서 높은 저항 값을 가지므로 적절한 전력을 내기 위해서는 높은 입력 전압이 필요하다. 이러한 경우 부스트 토폴로지의 역률 개선 회로를 사용할 수 있다. 하지만 입력 전압의 변동에 따라 직렬 공진형 인버터의 출력 전력 제어를 위한 동작 점 변동이 필요하므로 인버터의 손실이 변동한다. 본 논문에서는 낮은 저항 용기를 가열하기 위하여 높은 턴 수의 코일을 탑재한 유도 가열 장치용 하프 브릿지 직렬 공진형 인버터에서 자성체 용기의 가열 시 입력 전압 변동에 따른 인버터의 손실 분석을 통해 최적의 입력전압 조건을 선정하고자 한다. 제안하는 입력전압 선정 기법은 2-kW 급 유도 장치용 하프 브릿지 직렬 공진형 인버터 시 제품을 통해 타당성을 검증한다.

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Numerical Analysis of Foundation Reinforcing Method using Load Transfer Apparatus (하중전이 장치를 이용한 기초보강공법의 수치해석적 연구)

  • Jeon, Jun-Seo;Choi, Ki-Sun;You, Young-Chan;Ha, Soo-Kyoung
    • Journal of the Korea Institute of Building Construction
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    • v.21 no.6
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    • pp.617-627
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    • 2021
  • In this study, a numerical analysis using a three-dimensional numerical simulation was performed to assess the applicability of foundation reinforcing method using load transfer apparatus which can be used in the remodeling of deteriorated structures. The numerical model was validated through comparison with the real scale experimental results, and then a parametric study was performed to investigate the effect of friction coefficient of load transfer apparatus and axial stiffness of pile on the performance of foundation reinforcing method. It was confirmed that the foundation reinforcing method considered in this study can efficiently control the load applied to an existing foundation.