• Title/Summary/Keyword: $2{\alpha}$ angle

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THE EFFECT OF AUTOCLAVE STERILIZATION AND REUSE OF $SMARTPEG^{TM}$ ON THE IMPLANT STABILITY QUOTIENT (ISQ) MEASUREMENT ($Smartpeg^{TM}$의 고압멸균소독 및 재사용이 임플랜트 안정성 지수(ISQ) 측정에 미치는 영향)

  • Kang, In-Ho;Kim, Myung-Joo;Lim, Young-Jun;Kim, Chang-Whe
    • The Journal of Korean Academy of Prosthodontics
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    • v.45 no.5
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    • pp.644-652
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    • 2007
  • Statement of problem: Resonance frequency analysis is evaluated as the non-invasive and objective method for the evaluation of implant stability and has been increasingly used. It is necessary to evaluate the factors affect the ISQ measurement stability. Purpose: This study was performed to evaluate the effect of the autoclave sterilization and reuse of $Smartpeg^{TM}$ on ISQ measurement. Material and methods: $SmartPeg^{TM}$ (Integration Diagnostics Ltd., $G\ddot{o}teborg$, Sweden) of autoclave group (A) was autoclave sterilized 9 times and $Smartpeg^{TM}$ of reuse group (R) was reused 9 times. Ten $SmartPeg^{TM}s$ were allocated to each group and after each autoclave sterilization and reuse, implant stability quotient (ISQ) values were measured 3 times from the two directions a and b at a right angle. $Osstell^{TM}$ mentor (Integration Diagnostics Ltd. $G\ddot{o}teborg$, Sweden) was used and type 1 (article no. 100353) $Smartpeg^{TM}$ was selected according to $Smartpeg^{TM}$ reference list. Osstem Implant US II future (Osstem Co., Seoul, Korea) in $4.0mm{\times}11.5mm$ was embedded in the self-curing acrylic resin ($Orthojet^{(R)}$, Lang Dental, U.S.A.). Data was statistically analyzed by one-way ANOVA $({\alpha}=.05)$ and scheffe test was done where a significant difference exist. Correlation test was also done between ISQ value and the number of autoclave sterilization or reuse. Results: 1. In autoclave group, the means and sd. of ISQ value before autoclave sterilization were $84.97{\pm}0.41,\;84.93{\pm}0.74$ at direction a and b. There was significant differences between autoclave groups at direction a and b (P=.000). 2. In reuse group, the means and sd. of ISQ value before reuse were $85.40{\pm}0.62,\;85.50{\pm}0.57$ at direction a and b. There was no significant difference between reuse groups at direction a and b (P>.05). 3. There was a weak positive correlation between the number of reuse and ISQ value at direction a and b (${\gamma}=.207$ and .246, P<.01). Conclusion: Within the limitations of this study, the following conclusions were drawn. Till ninth reuse of $Smartpeg^{TM}$, the ISQ measurement stability did not be affected. After twice autoclave sterilization of $Smartpeg^{TM}$ the ISQ measurement stability was affected.

Comparison of removal torque between prefabricated and customized abutment screw (기성품과 맞춤형 임플란트 지대주 나사의 풀림 토크 비교)

  • Jamiyandorj, Otgonbold;Kim, Jee-Hwan;Kim, Mu-Seong;Park, Young-Bum;Shim, June-Sung
    • The Journal of Korean Academy of Prosthodontics
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    • v.50 no.4
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    • pp.243-248
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    • 2012
  • Purpose: The purpose of this study is to compare the removal torque between prefabricated and customized implant abutment screw. Materials and methods: Three types of implant system (Osstem, Astra, Zimmer) were used. For each system, prefabricated abutment screw (control group) and customized abutment screw (test group) were used to connect the fixture and the abutment (n = 6). Digital torque gauze was used to control the tightening torque and the screws were tightened under each manufacturer's recommendation. 10 minutes after the connection the same tightening torque was applied, and 5 minutes after the second connection, the removal torque was measured. This procedure was repeated 10 times. In the cyclic loading test, 10 minutes after the first connection to the 6 groups (n = 3), the same tightening torque was applied, and a total of 1,000,000 time loading was applied at 30 degree angle to long axis with 50 N load. Repeated measures of ANOVA test (${\alpha}$=.05) was used as statistics to evaluate the effect of repeated loading number on the removal torque. Independent t-test was used to evaluate the difference in removal torque after cyclic loading. Results: The removal torque significantly decreased as the number of loading repetition increased (P<.05). In the 10 time repetition test, there was no significant difference between the prefabricated and customized implant abutment screw of the 3 implant system (P<.05). Also in the cyclic loading test, there was no significant difference between the prefabricated and customized implant abutment screw of the 3 implant system (P<.05). Conclusion: Within the limitation of this study, there was no significant difference in the removal torque between the prefabricated abutment screw and customized abutment screws.

Modeling Paddlewheel-Driven Circulation in a Culture Pond (축제식 양식장에서 수차에 의한 순환 모델링)

  • KANG Yun Ho
    • Korean Journal of Fisheries and Aquatic Sciences
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    • v.34 no.6
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    • pp.643-651
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    • 2001
  • Paddlewheel-driven circulation in a culture pond has been simulated based on the depth integrated 2 dimensional hydrodynamic model. Acceleration by paddlewheel is expressed as shaft force divided by water mass discharged by paddlewheel blades. The model has been calibrated and applied to culture ponds as following steps:- i) The model predicted velocities at every 10 m along longitudinal direction from the paddlewheel. The model was calibrated comparing the results with the measured values at mass correction factor $\alpha$ and dimensionless eddy viscosity constant $\gamma$, respectively, in a range $15\~20$ and 6. ii) Wind shear stress was simulated under conditions of direction $0^{\circ}C,\;90^{\circ}C\;and\;180^{\circ}C$ and speed 0.0, 2.5, 5.0 and 7.5 m/s. Change rate of current speed was <$1\%$ at wind in parallel or opposite direction to the paddlewheel-driven jet flow, while $4\%$ at orthogonal angle. iii) The model was then applied to 2 culture ponds located at the Western coast of Korea. The measured and predicted currents for the ponds were compared using the regression analysis. Analysis of flow direction and speed showed correlation coefficients 0.8928 and 0.6782 in pond A, 0.8539 and 0.7071 in pond B, respectively. Hence, the model is concluded to accurately predict circulation driven by paddlewheel such that it can be a useful tool to provide pond management strategy relating to paddlewheel operation and water quality.

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The study of shear bond strength of a self-adhesive resin luting cement to dentin (상아질에 대한 자가 접착 레진 시멘트의 전단결합강도에 관한 연구)

  • In, Hee-Sun;Park, Jong-Il;Choi, Jong-In;Cho, Hye-Won;Dong, Jin-Keun
    • The Journal of Korean Academy of Prosthodontics
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    • v.46 no.5
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    • pp.535-543
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    • 2008
  • Purpose: The objective of this study was to compare the bonding characteristics of a new self-adhesive resin cement to dentin, which does not require bonding and conditioning procedure of the tooth surface, and conventional resin cement. The effect of phosphoric acid etching prior to application of self-adhesive resin cement on the shear bond strength was also evaluated. Material and methods: Fortyfive non-carious human adult molars extracted within 6 months were embedded in chemically cured acrylic resin. The teeth were ground with a series of SiC-papers ending with 800 grit until the flat dentin surfaces of the teeth were exposed. The teeth were randomly divided into 3 experimental groups. In group 1, self-adhesive resin cement, RelyX Unicem (3M ESPE, Seefeld, Germany) was bonded without any conditioning of teeth. In group 2, RelyX Unicem was bonded to teeth after phosphoric acid etching. For group 3, Syntac Primer (Ivoclar Vivadent AG, Schaan, Liechtenstein) was applied to the teeth before Syntac adhesive (Ivoclar Vivadent AG, Schaan, Liechtenstein) and Helibond (Ivoclar Vivadent AG, Schaan, Liechtenstein) followed by conventional resin cement, Variolink II (Ivoclar Vivadent AG, Schaan, Liechtenstein). To make a shear bond strength test model, a plastic tuble (3 mm diameter, 3 mm height) was applied to the dentin surfaces at a right angle and filled it with respective resin cement, and light-polymerized for 40 seconds. All the specimens were stored in distilled water at $37^{\circ}C$ for 24 hours before test. Universal Testing Machine (Z020, Zwick, Ulm, Germany) at a cross head speed of 1 mm/min was used to evaluate the shear bond strength. The failure sites were inspected under a magnifier and Scanning Electron Microscope. The data was analyzed with One way ANOVA and Scheffe test at ${\alpha}$= 0.05. Results: (1) The shear bond strengths to dentin of RelyX Unicem was not significantly different from those of Variolink II/Syntac. (2) Phosphoric acid etching lowered the shear bond strength of RelyX Unicem significantly. (3) Most of RelyX Unicem and Variolink II showed mixed fractures, while all the specimens of RelyX Unicem with phosphoric acid etching demonstrated adhesive failure between dentin and resin cement. Conclusion: Shear bond strength to dentin of self-adhesive resin cement is not significantly different from conventional resin cement, and phosphoric acid etching decrease the shear bond strength to dentin of self-adhesive resin cement.

INFLUENCE OF THREE DIFFERENT PREPARATION DESIGNS ON THE MARGINAL AND INTERNAL GAPS OF CEREC3 CAD/CAM INLAYS (세 가지 다른 인레이 와동 형태가 CEREC3 CAD/CAM의 변연 및 내면 간극에 미치는 영향)

  • Seo, Deog-Gyu;Yi, Young-Ah;Lee, Yoon;Roh, Byoung-Duck
    • Restorative Dentistry and Endodontics
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    • v.34 no.3
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    • pp.177-183
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    • 2009
  • The aim of this study was to evaluate the marginal and internal gaps in CEREC3 CAD/CAM inlays of three different preparation designs. CEREC3 Inlays of three different preparation designs (n=10) were fabricated according to Group I-conventional functional cusp capping/shoulder preparation, Group II-horizontal reduction of cusps and Group III-complete reduction of cusps/shoulder preparation. After cementation of inlays. the bucco-lingual cross section was performed through the center of tooth. Cross section images of 20 magnifications were obtained through the stereomicroscope. The gaps were measured using the Leica application suite software at each reference point. Statistical analysis was performed using one-way ANOVA and Tukey's test (${\alpha}<0.05$). The marginal gaps ranged from 80.0 to $97.8{\mu}m$ for Group I, 42.0 to $194.8{\mu}m$ for Group II, 51.0 to $80.2{\mu}m$ for Group III. The internal gaps ranged from 90.5 to $304.1{\mu}m$ for Group I, 80.0 to $274.8{\mu}m$ for Group II, 79.7 to $296.7{\mu}m$ for Group III. The gaps of each group were the smallest on the margin and the largest on the horizontal wall. For the CEREC3 CAD/CAM inlays, the simplified designs (groups II and III) did not demonstrate superior results compared to the traditional cusp capping design (group I).