• 제목/요약/키워드: spring-back

검색결과 295건 처리시간 0.021초

자동차 Panel의 Spring back에 대한 연구 (The spring back of Automobile body panel)

  • 최영환;유종근
    • 한국소성가공학회:학술대회논문집
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    • 한국소성가공학회 2002년도 금형가공 심포지엄
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    • pp.148-153
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    • 2002
  • Spring back is the typical deformation of pressing process. This phenomenon much affects productivity and especially Incurs the unexpected result of assembling process. We have been searching for the various of the spring back to minimize spring back effect, because it is inevitable.

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Optimization of spring back in U-die bending process of sheet metal using ANN and ICA

  • Azqandi, Mojtaba Sheikhi;Nooredin, Navid;Ghoddosian, Ali
    • Structural Engineering and Mechanics
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    • 제65권4호
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    • pp.447-452
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    • 2018
  • The controlling and prediction of spring back is one of the most important factors in sheet metal forming processes which require high dimensional precision. The relationship between effective parameters and spring back phenomenon is highly nonlinear and complicated. Moreover, the objective function is implicit with regard to the design variables. In this paper, first the influence of some effective factors on spring back in U-die bending process was studied through some experiments and then regarding the robustness of artificial neural network (ANN) approach in predicting objectives in mentioned kind of problems, ANN was used to estimate a prediction model of spring back. Eventually, the spring back angle was optimized using the Imperialist Competitive Algorithm (ICA). The results showed that the employment of ANN provides us with less complicated and time-consuming analytical calculations as well as good results with reasonable accuracy.

건설기계 Cabin Sunroof 형상비드 배치에 따른 스프링백 개선 (Spring-back Improvement According to the Shape Bead Arrangement of Cabin Sunroof in Construction Equipment)

  • 배기현
    • 소성∙가공
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    • 제30권2호
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    • pp.69-73
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    • 2021
  • This paper addresses the product shape modification for spring-back reduction in the sheet metal forming process of the cabin sunroof which is applied to the construction equipment. Initially, the anisotropic material properties are measured in order to calculate the degree of spring-back by the numerical simulation of the sheet metal forming process. To reduce the spring-back of the stamped part, several design modifications are suggested according to the geometrical bead arrangement on the planar region. The degrees of spring-back are confirmed for various product designs with different use of the geometrical bead. Finally, the spring-back improvement was validated by manufacturing the tryout product with the modified die set for the optimized product shape.

외연적 유한요소법을 이용한 KC-100 전방착륙장치 Spin-up, Spring-back 하중 해석 (Spin-up, Spring-back Load Analysis of KC-100 Nose Landing Gear using Explicit Finite Element Method)

  • 박일경;김성준;안석민
    • 한국항공운항학회지
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    • 제19권4호
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    • pp.51-57
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    • 2011
  • The spin-up and the spring-back are most severe load cases in the aircraft landing gear design. These load cases are caused by reciprocal action of complex physical phenomenon such as the friction between a tire and ground, inertia of the rotation of a tire and the flexibility of a landing gear structure. Generally, the empirical formula or the theoretical formula is used to calculate the spin-up and spring-back load in the early stage of the development program of the aircraft landing gear. After the materialization of the design of a landing gear, spin-up and spring-back load are acquired by the free drop test. In this study, the spin-up and the spring-back load of the rubber shock absorber type KC-100 nose landing gear are calculated by the explicit finite element analysis. Through this analysis, more accurate and realistic spin-up and spring back loads could be applied to the early phase of the development of the aircraft landing gear.

일체형원자로 SMART의 나선형 증기발생기 전열관 코일링 시 스프링백 최소화 방안 (Minimization of the Spring back in the Coiling Process of the Helical Steam Generator Tubes of Integral Reactor SMART)

  • 김용완;김종인;장문희
    • 대한기계학회:학술대회논문집
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    • 대한기계학회 2000년도 추계학술대회논문집A
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    • pp.837-842
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    • 2000
  • In the coiling process of helical steam generator tubes of integral reactor SMART, a considerable amount of spring back, which induces dimensional inaccuracy and difficulty in fabrication, has been arised. In this research, an analytical model was derived to evaluate the amount of the spring back for steam generator tubes. The model was developed on the basis of beam theory and elastic-perfectly plastic material property. This model was extended to consider the effect of plastic hardening and the effect of the tensile force on the spring back phenomena. Parametric studies were performed for various design variables of steam generator tubes in order to minimize the spring back in the design stage. A sensitivity analysis has shown that the low yield strength, the high elastic modulus, the small helix diameter, and the large tube diameter result in a small amount of the spring back. The amount of the spring back can be controlled by the selection of adequate design values in the basic design stage and reduced to an allowable limit by the application of the tensile force to the tube during the coiling process.

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마그네슘합금 ZK 60의 결정립 크기에 따른 스프링백 특성 분석 (Experimental Analysis on the Effect of Grain Size of ZK60 Sheet on the Spring-Back Characteristics)

  • 강성훈;박희대;권용남;이정환
    • 한국소성가공학회:학술대회논문집
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    • 한국소성가공학회 2008년도 추계학술대회 논문집
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    • pp.398-400
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    • 2008
  • In this work, an air-bending test using magnesium alloy ZK60 sheet was carried out at the various temperatures from room temperature to $300^{\circ}C$ in order to investigate the effect of grain size on the spring-back characteristic. It was found out from experiments that the amount of spring-back was nearly zero at all temperature range when the specimens with grain sizes of 14.66 and $60.71{\mu}m$ were bent by $90^{\circ}$. On the other hand, the spring-back amount dramatically increased at room temperature and phenomenon of spring-go was observed at high temperature when the specimen with submicro grain size of $0.98{\mu}m$ was bent by $90^{\circ}$. From this kind of different spring-back characteristics according to the grain size, it was confirmed that the grain size of material is one of the important factors which have an effect on the spring-back.

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나선형 증기 발생기 튜브의 정밀성형을 위한 스프링백 제어 연구 (A Study on the Control of Spring Back for the Precision Forming of the Steam Generator Helical Tube)

  • 서영성;김용완;김종인
    • 소성∙가공
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    • 제11권3호
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    • pp.238-245
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    • 2002
  • The spring back taking place after the coiling process of steam generator tube leads to the dimensional inaccuracy. In order to reduce the spring back, tension force was applied to the one end of the tube during forming. In this work, parametric study using FEM was performed to find the appropriate magnitude of tension force. The force that induces minimum spring back was found by simultaneously taking account if spring back amount, cross-sectional ovality, and thickness of the tube wall after deformation. In addition, stress relieving by heat treatment was also simulated as an alternative to the former method. The latter was found to be more effective under the given constraints.

두께가 얇은 냉간단조품의 스프링백 거동 및 저감설계 (Behavior and Reduction of Spring-back in a Thin Cold-Forged Product)

  • 김대원;신영철;최호준;윤덕재;이근안;김연구;임성주
    • 소성∙가공
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    • 제21권7호
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    • pp.397-402
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    • 2012
  • The flange hub is a main component in an automotive steering system. In general, the flange hub are fabricated by mechanical machining, which is a process where material waste is inevitable. It is well-known that a net-shape cold forging cannot only reduce material waste but can also improve the mechanical strength of the final product. Thus, a forging process design was conducted for production of a flange hub. Significant spring-back occurs around the flange due to its small thickness in conjunction with the residual stresses after forging. In order to achieve the required dimensional accuracy, a process design with appropriate spring-back control is needed. In this study, a modification of the forging die was designed based on FE analysis with the purpose of spring-back compensation. Four kinds of different die designs were evaluated and the optimum design has two times less spring-back than the initial design. The compensation angle of the optimum design is 0.5 degrees. The results have been experimentally confirmed by cold forging of a flange hub and comparing the amount of spring-back between the actual component and the FE analysis.

조향장치용 요크 자동다단 정밀냉간단조 공정에서 발생하는 스프링백의 수치적 및 실험적 검증 (Numerical and Experimental Study on Spring Back in Automatic Multi-Stage Precision Cold Forging Process of a Steering Yoke)

  • 김광민;김민철;황태민;정석환;정완진;전만수
    • 소성∙가공
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    • 제28권3호
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    • pp.115-122
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    • 2019
  • In this paper, finite element analysis of an automatic five-stage precision cold forging process of a yoke, a steering part of a passenger's car, is conducted with emphasis on spring back analysis at the yoke-forming stage and its experimental verification is subsequently made. An elastoplastic finite element method with MINI-element technique employed for the analysis of the entire process is explained. There is emphasis that the thin film of material formed between the punch and die in the stage may result to some errors especially in elastoplastic finite element analysis of spring back due to frequent remeshing. The numerical robustness of the spring back analysis in regards to remeshing is hence shown first through investigation into its effect on the predicted spring back. Experimental measurement of displacement due to spring back is carried out for comparison with the predicted results, and they are in a qualitative agreement with each other.

A Spring Back Calculation Model for the Sensitivity Analysis of Tube Design Parameters of Helical Steam Generator

  • Kim, Yong-Wan;Kim, Jong-In;Huh, Hyung;Park, Jin-Seok;Kim, Ji-Ho
    • 한국원자력학회:학술대회논문집
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    • 한국원자력학회 1999년도 추계학술발표회요약집
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    • pp.355.2-355
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    • 1999
  • The spnng back phenomena occurring in the coiling process of a steam generator tube induces the dimensional inaccuracy and makes the coiling procedure difficult. In this research, an analytical model was developed to evaluate the amount of the spring back for SMART steam generator tubes. The model was developed on the basis of beam theory and elastic-perfectly plastic material property. This model was extended to consider the effect of plastic hardening and the effect of the tensile force on the spring back phenomena. Parametric studies were performed for various design variables of steam generator tubes in order to minimize the spring back in the design stage. A sensitivity analysis has shown that the low yield strength, the high elastic modulus, the small helix diameter, and the large tube diameter result in a small amount of the spring back. The amount of the spring back can be controlled by the selection of adequate design values in the basic design stage and reduced to an allowable limit by the application of the tensile force to the tube during the coiling process.rocess.

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