• Title/Summary/Keyword: screw conveyor

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Development of Air-jet Washer for the Agaricus Bisporus (공기분사에 의한 양송이 버섯 세척기 개발)

  • Park, H.M.;Cho, K.H.;Hong, S.G.;Lee, S.H.
    • Journal of Biosystems Engineering
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    • v.34 no.3
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    • pp.167-174
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    • 2009
  • This study was conducted to develop an agaricus bisporus washing machine which uses compressed air to remove foreign materials attached on the surface of agaricus bisporus. A prototype of the washing machine was constructed, and performance of removing foreign materials was tested. Research results are as follows: 1. Several transferring methods including PE roller rotation, brush roller rotation, PE screw rotation, vibration plate, and belt conveyor were evaluated. Roller, screw, and vibration methods caused damages on the surface of the products, but belt conveyor method caused the least damages. 2. For air jet, a stationary nozzle type and a rotational type were evaluated. The best air jet nozzle was the jet-type nozzle, and the rotational type was more effective than stationary type nozzle. 3. With the conveyer belt, box type moving method and the rotational air jet nozzle, the washing machine showed the best performance when higher than 5.4${\times}$105 Pa of air jet pressure and lower than 0.047 m/s of moving speed was used. Working performance of the system was 650 kg/h, and the damaging rate was 1.2 %.

A Treatability Study on the Soil Washing Device for the Remediation of Oil-Contaminated Soil (유류 오염토양 복원을 위한 토양세척 장비의 적용성 연구)

  • Kong, Jun;Choi, Sang-Il
    • Journal of Korea Soil Environment Society
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    • v.3 no.3
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    • pp.109-116
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    • 1998
  • Treatability tests of a soil washing device were performed for the remediation of eil-contaminated soil. The contaminant-containing soil with water was first fed into a oc-current screw conveyor and then into a counter-current washer. Surfactant was introduced into the washer and feeding soil was continuously separated on the basis of #40 mesh at the same time. A washing efficiency of 97.9% was achieved by the the soil washing device optimized.

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Development of Automatic Packing System of One Station for Fasteners(II) : Packing System Manufacture and Performance Test (원 스테이션 파스너 자동포장기 개발(II) : 제작 및 성능검증)

  • Kim, Yong-Seok;Jeong, Chan-Se;Yang, Soon-Young
    • Journal of the Korean Society of Manufacturing Technology Engineers
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    • v.20 no.5
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    • pp.653-658
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    • 2011
  • In general, the purpose of packaging fasteners is a series of management activities to maintain the condition at the time of production until they get delivered to the end user. An automatic packing system for fasteners is consisted of bucket conveyor, slide feeder, vision inspection system, box-magazine conveyor system and automatic packing machine. Also, the automatic packing machine is consisted of six modules including charging device, clamping/opening device, sealing/cutting device, feeding/air-shower device, supplying/adjusting device and device frame, etc. In this paper, we proposed an automatic packing mechanism of the one station concept for packing work of fastener objects where the continuous batch work is performed in a finite space. The proposed one-station packing mechanism has been optimized through mechanical, dynamical, structural and fluid analyses. And it had been manufactured as the prototype of automatic packing machine. The field test for validation of performance was performed directly at the production line of bolt and screw. In the field test, this packing machine showed an efficiency of about 4.5 times the manual operation. It also showed 30% reduction in the consumption of packing materials compared to the manual operation. This automatic packing machine for fastener objects will be commercialized soon.

Automation of Tire Tread Extruder Line Using Cameras (카메라를 이용한 타이어 트레드 압출라인 자동화)

  • Pyo, Choon-Seon;Lyou, Joon
    • Journal of Institute of Control, Robotics and Systems
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    • v.19 no.3
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    • pp.262-267
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    • 2013
  • This paper describes a vision based automation case study for the tire tread extruder line. To accurately measure the thread widths, two cameras with laser line illumination have been installed near the takeaway conveyer. The overall tread extruder line is then automated by controlling the speeds of take away conveyor and screw motor such that a difference between measured widths and the targeted data is minimized. By doing this, the conventional tread extruder line has been replaced by the developed automated computer system and with only one operator, increasing the production efficiency and reducing safety accidents.

Development of an Automated Measurement System for Dilution Process and Spraying Amount of Disinfectant

  • Kim, Jung-Chul;Chung, Sun-Ok;Cho, Byoung-Kwan;Chang, Hong-Hee;Kim, Suk;Chang, Dongil
    • Journal of Biosystems Engineering
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    • v.38 no.4
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    • pp.228-239
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    • 2013
  • Purpose: The objectives of this study were to develop an automated disinfectant dilution system, and an automated data management system for spraying amount for resolving uncertainty problem. Methods: Proper diluting rate was made by a controlled volume pump for liquid disinfectant and a screw conveyer pump for solid disinfectant. The water capacity of disinfecting system of 400 L was controlled by two water level sensors. The water quantity of water tank was controlled by the signals which were produced by the water level sensors. Signals were processed by Labview Programming, and ON/OFF of solenoid valve that was used for controlling water supplying to water tank, was controlled by SSR. The operating time of pumps for disinfectant was controlled quantitatively. A turbine flowmeter was used for development of automated measurement system for spraying amount of disinfectant. In order to save the flowmeter data and to control the spraying system, a multi-function data logger was used, and it was processed and saved in Excel file by a program developed in this study. Results: Labview 2010 was used for programming to control the automated measurement system for spraying amount of disinfectant. Results showed that the relationship between flowmeter value and time had a significant linear relationship such as 0.99 of $R^2$. Generally, 6.74 L/s of diluted disinfectant is sprayed for a vehicle passing through the disinfection system (about 15 seconds). Test results showed that average error between the measured spraying amount and the flowmeter data was 50 mL, and the range of error was 1.3%. Since the amount and time of spraying could be saved in real-time by using the spreadsheet files which could not be modified arbitrarily, it made possible to judge objectively whether the disinfection spraying was performed or not. Test results of spraying liquid and solid disinfectant showed that the errors between the measured discharge rate and the theoretical one were ranged within 3-4% for various dilution rates. Conclusions: The disinfection system developed would be working accurately. The automated spraying data base management system satisfied the purpose of this study. The automated dilution process system developed in this study could discharge liquid and solid disinfectant with accurate dilution rate, relatively.

Improvement of a Rice Seed Pelleting Machine for Direct Seeding in Rice Cultivation(I) - Construction and its performance - (직파용 벼 펠렛종자 제조장치 개선 연구(I) - 장치 제작과 성능분석 -)

  • 유대성;유수남;최영수
    • Journal of Biosystems Engineering
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    • v.28 no.5
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    • pp.403-410
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    • 2003
  • To enhance the performance of a rice seed pelleting machine and the quality of rice-seed pellets made, improvement of the rice seed pelleting machine developed previously(Park, 2002) was tried and its performance was evaluated. As compared with the previous pelleting machine, a feeding mechanism of pellet materials to the forming rolls was changed from screw conveyor to hydraulic cylinder for proper feeding, rings were installed among rows of semi-spherical forming grooves on the forming rolls for reducing pellet materials loss and seeds damage, and discharging air nozzles were added for complete discharging of the pellets made. Through performance tests, capacity, pelleting ratio, and seed loss ratio of the pelleting machine were investigated at the mixing ratios of soil to rice seed of 6 : 1, 7 : 1, and 8 : 1, and rotating speeds of the forming rolls of 7 rpm, 10 rpm, and 13 rpm. As results of performance evaluation, pelleting ratios were in the range of 77 ∼ 89 %, and maximum pelleting ratio increased by 18 % in comparison with that of the previous machine. Maximum capacity was about 110 kg/h(about 63,000 pellets/h), which was increased by 70 % in comparison with that of the previous machine. But, ratios of seed loss were in the range of 24 - 49 %, which were not improved.

Development of a Rice Seed Pelleting Machine for Direct Seeding in Rice Cultivation (직파용 벼 펠렛종자 제조장치 개발)

  • 박종수;유수남;최영수;유대성
    • Journal of Biosystems Engineering
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    • v.27 no.5
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    • pp.381-390
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    • 2002
  • Direct seeding of rice-seed pellets is expected to be an alternative for solving problems in current direct seeding cultivation of rice. but mass production of rice-seed pellets is prerequisite for practical application. Design. construction and performance evaluation of an experimental rice seed pelleting machine were carried out for mass production of rice-seed pellets. The pelleting machine intended to make a ball type rice-seed pellet, which have 3∼5 rice seeds and diameter of which is 12 mm. Pellet materials ; rice seeds, soil, and binder were mixed and kneaded by the mixer. The designed rice seed pelleting machine fed pellet materials by screw conveyor to forming rolls and made rice-seed pellets. Capacity, ratio of perfect rice-seed pellets, seed and pellet material loss were investigated as mixing ratio of soil to rice seed and feeding rate of pellet materials. The pelleting machine showed up to 37,000 pellets/h of pelleting rate, 61∼71% of weight ratio of perfect rice-seed pellets to pellet materials supplied, 17∼48% of seed loss ratio. Average weight and average diameter of the pellets were 1.66 g and 12.0 mm. respectively. More than 3 rice seeds were included in most pellets at 6 : 1 of mixing ratio of soil to rice seed. And compression strength of the pellets was in the range of 88-130 N. To improve performance of the pelleting machine, improvements of the forming rolls, feeding mechanism, and discharging mechanism for reducing loss of pellet materials and seeds damage are needed.

Development of Grain Heater Using Engine Exhaust Gas (내연기관(內燃機關) 배기(排氣)가스를 이용(利用)한 곡물가열기(穀物加熱機) 개발(開發))

  • Suh, S.R.;Harris, F.D.
    • Journal of Biosystems Engineering
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    • v.10 no.2
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    • pp.1-11
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    • 1985
  • A double pipe grain heater using engine exhaust gas as a heat source was developed. The performance of the grain heater was examined with soybeans as a test material experimentally and numerically using a mathematical model constructed. The following conclusions were drawn: 1. The modified screw conveyor used in the grain heater has a characteristic of decreasing capacity with increasing speed at speeds above 60 rpm. Operation with speeds below 60 rpm is recommended. 2. Heating soybeans by the heater at soybean flow rate up to 100 kg/hr, inlet temperature of the exhaust gas to the heater are recommended as above $400^{\circ}C$, $300^{\circ}C$, and $200^{\circ}C$ roughly for a 2, 5, and 10 kW engine, respectively. 3. Temperature increments of soybean by the heater at soybean flow rates ranged from 25 to 100 kg/hr are in the ranges of $6^{\circ}C-35^{\circ}C$, $15^{\circ}C-88^{\circ}C$, and $15^{\circ}C-140^{\circ}C$ with exhaust gas from a 2, 5, and 10 kW engine, respectively, at an exhaust temperature of $500^{\circ}C$. 4. Thermal efficiency of the heater at soybean flow rates ranged from 25 to 100 kg/hr are in the ranges of 35-37%, 28-34%, and 20-29% with exhaust gas from a 2, 5, and 10 kW engine, respectively. 5. The grain heater can be used to heat the other grain, also, without any bad effect from the exhaust gas used as a heat source.

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A Study on the Durability of Manure Composting Facilities (축분 퇴비화 시설 내구성에 관한 조사연구)

  • Hong, Ji-Hyung
    • Journal of Animal Environmental Science
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    • v.16 no.1
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    • pp.13-20
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    • 2010
  • Manure compost is a main product from animal wastes in Korea. Solid manure is usually treated by aerobic composting at manure composting facilities for land reinforcement. Agricultural use of manure compost as organic fertilizer resources, mainly manure compost, is now recommended in Korea. This study investigated the evaluation of durability about the manure composting machinery and structures which was controlled by aeration and periodic agitating. The questionnaire addressed three main topics as follows: operating practices, machinery and maintenance of the manure composting facilities are being operated. A total of the 22 manure composting facilities in an agricultural cooperative were surveyed. The results obtained in this survey were summarized as follow: The major causes of manure composting apparatus trouble were corrosion and wear, overloading and foreign matter etc. The highly trouble frequency of the agitator, packer and conveyor were chain, agitating blade and shaft, motor and screw vane, respectively. These analytical results can be used as basic information to establish the maintenance control methods and durability standard of manure composting facility.

Shear behavior of foam-conditioned gravelly sands: Insights from pressurized vane shear tests

  • Shuying Wang;Jiazheng Zhong;Qiujing Pan;Tongming Qu;Fanlin Ling
    • Geomechanics and Engineering
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    • v.34 no.6
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    • pp.637-648
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    • 2023
  • When an earth pressure balance (EPB) shield machine bores a tunnel in gravelly sand stratum, the excavated natural soil is normally transformed using foam and water to reduce cutter wear and the risk of direct muck squeezing out of the screw conveyor (i.e., muck spewing). Understanding the undrained shear behavior of conditioned soils under pressure is a potential perspective for optimizing the earth pressure balance shield tunnelling strategies. Owing to the unconventional properties of conditioned soil, a pressurized vane shear apparatus was utilized to investigate the undrained shear behavior of foam-conditioned gravelly sands under normal pressure. The results showed that the shear stress-displacement curves exhibited strain-softening behavior only when the initial void ratio (e0) of the foam-conditioned sand was less than the maximum void ratio (emax) of the unconditioned sand. The peak and residual strength increased with an increase in normal pressure and a decrease in foam injection ratio. A unique relation between the void ratio and the shear strength in the residual stage was observed in the e-ln(τ) space. When e0 was greater than emax, the fluid-like specimens had quite low strengths. Besides, the stick-slip behavior, characterized by the variation coefficient of measured shear stress in the residual stage, was more evident under lower pressure but it appeared to be independent of the foam injection. A comparison between the results of pressurized vane shear tests and those of slump tests indicated that the slump test has its limitations to characterize the chamber muck fluidity and build the optimal conditioning parameters.