• Title/Summary/Keyword: replacement time

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Assessment of Environmental Impacts and $CO_2$ Emissions from Soil Remediation Technologies using Life Cycle Assessment - Case Studies on SVE and Biopile Systems - (전과정평가(LCA)에 의한 토양오염 정화공정의 환경영향분석 및 $CO_2$ 배출량 산정 - SVE 및 Biopile 시스템 중심으로 -)

  • Jeong, Seung-Woo;Suh, Sang-Won
    • Journal of Korean Society of Environmental Engineers
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    • v.33 no.4
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    • pp.267-274
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    • 2011
  • The environmental impacts of 95% remediation of a total petroleum hydrocarbon-contaminated soil were evaluated using life cycle assessment (LCA). LCA of two remediation systems, soil vapor extraction (SVE) and biopile, were conducted by using imput materials and energy listed in a remedial system standardization report. Life cycle impact assessment (LCIA) results showed that the environmental impacts of SVE were all higher than those of biopile. Prominent four environmental impacts, human toxicity via soil, aquatic ecotoxicity, human toxicity via surface water and human toxicity via air, were apparently found from the LCIA results of the both remedial systems. Human toxicity via soil was the prominent impact of SVE, while aquatic ecotoxicity was the prominent impact of biopile. This study also showed that the operation stage and the activated carbon replacement stage contributed 60% and 36% of the environmental impacts of SVE system, respectively. The major input affecting the environmental impact of SVE was electricity. The operation stage of biopile resulted in the highest contribution to the entire environmental impact. The key input affecting the environmental impact of biopile was also electricity. This study suggested that electricity reduction strategies would be tried in the contaminated-soil remediation sites for archieving less environmental impacts. Remediation of contaminated soil normally takes long time and thus requires a great deal of material and energy. More extensive life cycle researches on remedial systems are required to meet recent national challenges toward carbon dioxide reduction and green growth. Furthermore, systematic information on electricity use of remedial systems should be collected for the reliable assessment of environmental impacts and carbon dioxide emissions during soil remediation.

A Study on the Estimation for the Guaranteed Strength and Construction Quality of the Combined High Flowing Concrete in Slurry Wall (지하연속벽용 병용계 고유동 콘크리트의 시공 품질 및 보증강도 평가에 관한 연구)

  • Kwon, Yeong-Ho
    • Journal of the Korea Concrete Institute
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    • v.18 no.6 s.96
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    • pp.811-817
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    • 2006
  • The primary purpose of this study is to estimate the guaranteed strength and construction quality of the combined high flowing concrete which is used in the slurry wall of underground LNG storage tank. The required compressive strength of this type of concrete become generally known as a non economical value because it is applied the high addition factor for variation coefficients and low reduction factor under water concrete. Therefore, after estimation of the construction quality and guaranteed strength in actual site work, this study is to propose a suitable equation to calculate the required compressive strength in order to improve its difference. Application results in actual site work are shown as followings. The optimum nix design proportion is selected that has water-cement ratio 51%, sand-aggregate ratio 48.8%, and replacement ratio 42.6% of lime stone powder by cement weight. Test results of slump flow as construction quality give average 616~634mm. 500mm flowing time and air content are satisfied with specifications in the rage of 6.3 seconds and 4.0% respectively. Results of strength test by standard curing mold show that average compressive strength is 49.9MPa, standard deviation and variation coefficients are low as 1.66MPa and 3.36%. Also test results by cored cylinder show that average compressive strength is 66.4MPa, standard deviation and variation coefficients are low as 3.64MPa and 5.48%. The guaranteed strength ratio between standard curing mold and cored cylinder show 1.23 and 1.32 in the flanks. It is shown that applied addition factor for variation coefficients and reduction factor under water concrete to calculate the required compressive strength is proved very conservative. Therefore, based on these results, it is proposed new equation having variation coefficients 7%, addition factor 1.13 and reduction factor 0.98 under water connote.

Comparative study on effects of volume-controlled ventilation and pressure-limited ventilation for neonatal respiratory distress syndrome (신생아 호흡곤란 증후군에서 volume-controlled ventilation과 pressure-limited ventilation의 효과에 관한 비교연구)

  • Kim, Jae Jin;Hwang, Mun Jung;Lee, Sang Geel
    • Clinical and Experimental Pediatrics
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    • v.53 no.1
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    • pp.21-27
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    • 2010
  • Purpose : In contrast with traditional time-cycled, pressure-limited ventilation, during volume-controlled ventilation, a nearly constant tidal volume is delivered with reducing volutrauma and the episodes of hypoxemia. The aim of this study was to compare the efficacy of pressure-regulated, volume controlled ventilation (PRVC) to Synchronized intermittent mandatory ventilation (SIMV) in VLBW infants with respiratory distress syndrome (RDS).Methods : 34 very low birth weight (VLBW) infants who had RDS were randomized to receive either PRVC or SIMV with surfactant administration : PRVC group (n=14) and SIMV group (n=20). We compared peak inspiratory pressure (PIP), duration of mechanical ventilation, and complications associated with ventilation, respectively with medical records. Results : There were no statistical differences in clinical characteristics between the groups. After surfactant administration, PIP was significantly lower during PRVC ventilation for 48hrs and accumulatevive value of decreased PIP was higher during PRVC ventilation for 24hrs (P<0.05). Duration of ventilation and incidence of complications was no significant difference. Conclusion : PRVC is the mode in which the smallest level of PIP required to deliver the preset tidal volume in VLBW infants with RDS, adaptively responding to compliance change in lung after surfactant replacement.

A Dynamic Behavior Evaluation of the Curved Rail according to Lateral Spring Stiffness of Track System (궤도시스템의 횡탄성에 따른 곡선부 레일의 동적거동평가)

  • Kim, Bag-Jin;Choi, Jung-Youl;Chun, Dae-Sung;Eom, Mac;Kang, Yun-Suk;Park, Yong-Gul
    • Proceedings of the KSR Conference
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    • 2007.11a
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    • pp.517-528
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    • 2007
  • Domestic or international existing researches regarding rail damage factors are focused on laying, vehicle conditions, driving speed and driving habits and overlook characteristics of track structure (elasticity, maintenance etc). Also in ballast track, as there is no special lateral spring stiffness of track also called as ballast lateral resistance in concrete track, generally, existing study shows concrete track has 2 time shorter life cycle for rail replacement than ballast track due to abrasion. As a result of domestic concrete track design and operation performance review, concrete track elasticity is lower than track elasticity of ballast track resulting higher damage on rail and tracks. Generally, concrete track has advantage in track elasticity adjustment than ballast track and in case of Europe, in concrete track design, it is recommended to have same or higher performance range of vertical elastic stiffness of ballast track but domestically or internationally review on lateral spring stiffness of track is very minimal. Therefore, through analysis of service line track on site measurement and analysis on performance of maintenance, in this research, dynamic characteristic behaviors of commonly used ballast and concrete track are studied to infer elasticity of service line track and experimentally prove effects of track lateral spring stiffness that influence curved rail damage as well as correlation between track elasticity by track system and rail damage to propose importance of appropriate elastic stiffness level for concrete and ballast track.

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Thrombolytic Therapy for Thrombosis of Prosthetic Mitral Valve - A Case Report - (인공 승모판막에 생긴 혈전의 혈전용해 치료 - 1례 보고 -)

  • Kang, Shin-Kwang;Kim, Si-Wook;Won, Tae-Hee;Ku, Kwan-Woo;Na, Myung-Hoon;Yu, Jae-Hyun;Lim, Seung-Pyung;Lee, Young;Jeong, Jin-Ok
    • Journal of Chest Surgery
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    • v.35 no.11
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    • pp.826-830
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    • 2002
  • Prosthetic valve thrombosis(PVT) may be a life-threatening complication requiring prompt intervention. This is a case report of thrombolytic therapy for thrombosis of prosthetic mitral valve. A 47 year-old male admitted to the emergency room for abrupt onset of dyspnea. He had undergone mitral valve replacement(On-Ⅹ valve, 29mm) for mitral stenosis 8 months ago. The patient's international normalized ratio(INR) on admission was 1.09. The mechanical clicks were muffled and rales were heard in both lung fields. A transesophageal echocardiography(TEE) revealed prosthetic valve thrombosis with increased transvalvular pressure gradient(34 mmHg). The patient's condition needed to intubation for mechanical ventilation due to hemodynamic compromise, however his wife and relatives refused the surgical intervention due to financial problems. The patient was transferred to the cardiac care unit and we decided to perform thrombolytic therapy. A bolus of 1,500,000 IU of urokinase was given, followed by a drip of 1,500,000 IU for 1 hour. The patient did not improved hemodynamically; therefore, we gave 100 mg of tissue plasminogen activator(t-PA) for over 2 hours. During that time mechanical clicks were audible and hemodynamics of the patient improved progressively. A TEE showed disappearance of thrombus and decreased pressure gradient(1.7 mmHg) after 6 hours of thrombolytic therapy. The patient was recovered without any neurologic sequale and was discharged with administration of warfarin.

Clinical Experiences of redo-CABG (관상동맥우회 재수술의 임상적 고찰)

  • Lim, Sang-Hyun;Kwak, Young-Tae;Lee, Sak;Chang, Byung-Chul;Kang, Meyun-Shick;Cho, Bum-Koo;Yoo, Kyung-Jong
    • Journal of Chest Surgery
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    • v.35 no.11
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    • pp.779-784
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    • 2002
  • Recently, the number of coronary artery bypass surgery(CABG) is increasing according to the increasing incidence of coronary artery disease. However, CABG is not a definite corrective surgery; therefore, in some patients, redo-CABG may be required. We retrospectively reviewed our redo-CABG experiences to help future redo-CABG. Material and Method: From January 1991 to April 2001, 14 cases of redo-CABG were performed in Yonsei Cardiovascular Center(M:F=12:2) and mean age was 61,7 $\pm$ 7.1(47-72) years. Mean time from 1st. CABG to redo-CABG was 121.9 $\pm$ 50.5(6.1-179.6) months. Thirteen cases were conventional on-pump CABG and one case was off-pump CABG. In two patients, mitral valve re-replacement and mitral valve repair were performed each. All redo-CABG were performed through mid-sternotomy. During redo-CABG, left internal mammary artery and saphenous vein grafts were used in 6 patients, left internal mammary artery and left radial artery grafts were used in 2 patients, left internal mammary artery and gastroepiploic artery were used in one patient and only greater saphenous veins were used in 5 cases(In one case, cephalic vein was also used). The number of mean distal anastomosis was 2.1 $\pm$ 0.9(1-4). Result: There were no operative death and no perioperative myocardial infarctions and cerebrovascular accidents or other heart related complications. Mean follow up duration was 40.1 $\pm$ 38.6(1.1-118.5) months. During follow up period, angina was re-developed in one patient 13 months after operation. Two patients died of end-stage renal failure 14.8 months and 116.3 months after redo-CABG, respectively. During follow up period, coronary angiography was performed in 3 patients, and all grafts were patent. At last follow up, mean Canadian class was 1.3. Kaplan-Meier survival at 9 years was 90.0 $\pm$ 9.5% and event free survival at 9 years was 71.4 $\pm$ 6.9%. Conclusion: After redo-CABG, all patients improved their angina symptom and daily activity. And long-term survival after redo-CABG was excellent. Therefore, if patients have indications for redo-CABG, thenredo-CABG must be strongly recommended and performed.

Risk Factor Analysis for Spinal Cord and Brain Damage after Surgery of Descending Thoracic and Thoracoabdominal Aorta (하행 흉부 및 흉복부 대동맥 수술 후 척수 손상과 뇌손상 위험인자 분석)

  • Kim Jae-Hyun;Oh Sam-Sae;Baek Man-Jong;Jung Sung-Cheol;Kim Chong-Whan;Na Chan-Young
    • Journal of Chest Surgery
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    • v.39 no.6 s.263
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    • pp.440-448
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    • 2006
  • Background: Surgery of descending thoracic or thoracoabdominal aorta has the potential risk of causing neurological injury including spinal cord damage. This study was designed to find out the risk factors leading to spinal cord and brain damage after surgery of descending thoracic and thoracoabdominal aorta. Material and Method: Between October 1995 and July 2005, thirty three patients with descending thoracic or thoracoabdominal aortic disease underwent resection and graft replacement of the involved aortic segments. We reviewed these patients retrospectively. There were 23 descending thoracic aortic diseases and 10 thoracoabdominal aortic diseases. As an etiology, there were 23 aortic dissections and 10 aortic aneurysms. Preoperative and perioperative variables were analyzed univariately and multivariately to identify risk factors of neurological injury. Result: Paraplegia occurred in 2 (6.1%) patients and permanent in one. There were 7 brain damages (21%), among them, 4 were permanent damages. As risk factors of spinal cord damage, Crawford type II III(p=0.011) and intercostal artery anastomosis (p=0.040) were statistically significant. Cardiopulmonary bypass time more than 200 minutes (p=0.023), left atrial vent catheter insertion (p=0.005) were statistically significant as risk factors of brain damage. Left heart partial bypass (LHPB) was statistically significant as a protecting factor of brain (p=0.032). Conclusion: The incidence of brain damage was higher than that of spinal cord damage after surgery of descending thoracic and thoracoabdominal aorta. There was no brain damage in LHPB group. LHPB was advantageous in protecting brain from postoperative brain injury. Adjunctive procedures to protect spinal cord is needed and vigilant attention should be paid in patients with Crawford type II III and patients who have patent intercostal arteries.

Arthroscopic Pull-out Suture Repair of Posterior Root Tear of the Medial Meniscus - Minimum 5 Years Follow-up Results - (내측 반월상 연골판 후방 부착부 파열의 관절경적 견인 봉합술 - 최소 5년 추시결과 -)

  • SaKong, Hyub;Shin, Hong Kwan;Lee, Young-Kook;Bae, Ki Cheor;Cho, Chul Hyun;Lee, Kyung Jae;Son, Eun-Seok;Kim, Doo Han
    • Journal of the Korean Arthroscopy Society
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    • v.16 no.2
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    • pp.153-159
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    • 2012
  • Purpose: This study aims at evaluating our results with a 5-year follow up of arthroscopic pull-out suture repair of posterior root tear of the medial meniscus. Materials and Methods: This study enrolled 30 cases who underwent a arthroscopic pull-out suture repair to treat the posterior root tear of the medial meniscus from January 2001 to May 2005 and followed up at least 5 years. The average follow-up period was 76 months (range, 60-90 months). Clinical results by use of the Lysholm knee score and radiographic grade by use of the Kellgren-Lawrence classification were evaluated and second-look arthroscopy was done in all cases. The clinical results were compared with trauma history, obesity, varus deformity and time to operation. Results: At the last follow up, the Lysholm knee score improved from 55 points to 86 points. For the radiological results, 23 cases displayed maintenance or improvement of the medial joint space on the follow up X-ray, but 7 cases displayed decrease of the medial joint space, and 1 case was lately performed total knee replacement due to progressive osteoarthritic change. Conclusion: Arthroscopic pull-out suture repair has a good result at 27 cases (90%) in minimum 5 years follow-up. The clinical improvement was significantly reduced in more severe varus angle.

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Changing Aspects of the Wall Types of Hahoe Village (하회마을 담장 형태의 변화양상)

  • Kim, Dong-Hyun;Lee, Won-Ho
    • Journal of the Korean Institute of Landscape Architecture
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    • v.45 no.5
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    • pp.87-96
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    • 2017
  • This study focuses on the Andong Hahoe Village and seeks to identify the shape of the walls since the 1970s. The change of walls can be divided into four periods based on characteristics of materials, shape and distribution. The following is a summary of the results: First, In the 1970s, when Andong Hahoe Village was not designated as a cultural heritage, roof tiles hung on the earthen walls in the middle of the village were major forms. On the outside of the village, rice straw and pine needles were put on the earthen walls or bush clover walls were put in place around if walls were not built. Second, after being designated as a cultural heritage in the 1980s, readjustments for cultural heritages were carried out at the primary stage. However, the distribution of cultural heritages and major changes were not determined at this time since readjustments were mainly focused on the renovation of derelict houses or maintenance of infrastructures. Third, in the past the use of stone bricks for the Hahoe Village site had been difficult, but in the 1990s, replacements with soil-stone walls were identified and the usage of roof tiles increased. The portion of earthen walls, which used to be the major form in the prior era, decreased and this seems to have continued until the 2000s. Fourth, via a field survey, it was found that most of Hahoe village walls consisted of soil cement bricks mixed with cement, steel, lime, gravel. etc. Also, the scope of straw-stricken walls and bush clover walls were reduced to a section of area outside of the village. Fifth, from the 1970s to the present, there were changes to the walls in Hahoe Village including an increase in usages of new materials and an expansion of houses with tiled roofs on top in accordance with the replacement of walls of existing houses. Relevant reasons for this have been identified, such as the fading value of Fungsui(風水) and lack of original records, insufficient awareness and expertise in non-building areas, and the relationship between residents on repairing the wall.

Material Characteristics and Deterioration Assessment of the Stone Buddhas and Shrine in Unjusa Temple, Hwasun, Korea (화순 운주사 석조불감의 재질특성과 풍화훼손도 평가)

  • Park, Sung-Mi;Lee, Myeong-Seong;Choi, Seok-Won;Lee, Chan-Hee
    • Journal of Conservation Science
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    • v.24
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    • pp.23-36
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    • 2008
  • The stone Buddhas and Shrine of Unjusa temple (Korea Treasure No. 797) in Hwasun formed in Koryo Dynasty are unique style which the Buddha faces each other the back parts of south and north within the stone Shrine. The stone Buddhas and Shrine are highly evaluated in historical, artistic and academic respects. But, the stone properties have been exposed in the open system various aspects of degradations weathered for a long time without specific protective facilities. The rock materials of the stone Buddhas and Shrine are about 47 blocks, and total press load is about 56.6 metric ton. The host rocks composed mainly of white grey hyaline lithic tuff and rhyolitic tuff breccia. In addition, biotite granite used as part during the restoration works. The chemical index of alteration for host tuffaceous rocks and the replacement granites range from 52.1 to 59.4 and 50.0 to 51.0, respectively. Weathering types for the stone Buddhas and Shrine were largely divided with physical, chemical and biological weathering to make a synthetic deterioration map according to aspects of damage, and estimate share as compared with surface area. Whole deterioration degrees are represented that physical weathering appeared exfoliation. Chemical weathering is black coloration and biological weathering of grey lichen, which show each lighly deterioration degrees. According to deterioration degree by direction of stone Buddhas and Shrine, physical weathering mostly appeared by 39.1% on the sorthern part, and chemical weathering is 61.2% high share on the western part. Biological weathering showed 38.3% the largest distribution on the southern part. Therefore, it is necessary to try hardening for the parts with serious cracks or exfoliations, remove secondary contaminants and organisms through regular cleaning. Also necessary to make a plan to remove moisture of the ground which causes weathering, and estimate that need established and scientific processing through clinical demonstration of conservation plan that chooses suitable treatment.

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