• Title/Summary/Keyword: repairing

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Improvement of Durability in Concrete Structures Using CRM (내화학성 적층보강공법(CRM)을 활용한 콘크리트 구조물의 내구성능 향상)

  • Kim, Chun-Ho;Kim, Sang-Doh;Kim, Nam-Wook
    • Journal of the Korea institute for structural maintenance and inspection
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    • v.17 no.6
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    • pp.145-152
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    • 2013
  • As a typical construction material, concrete has been used in building all kinds of structures since the late $19^{th}$ century. Although it was recognized to secure durability as long as the regulations on design and construction have been reasonably complied, the trends of life-shortening and deterioration have frequently occurred due to all kinds of the external effects that have been experienced during the procedures of using the structures. To make matters even worse, deterioration of the concrete structures according to deterioration can not be controlled any more. Finally, the reality is that repair and maintenance are necessary in the maintenance aspect of the concrete structure. In this study, CRM(Chemical Resistance of Laminating Reinforcement Method), which had been developed to reinforce the surface of concrete and specially improve chemical resistance performance, has been applied to enhance the existing repairing and maintenance method. Therefore, the result has been drawn with comparison and analysis of the specimens applied with the general repairing and maintenance method and CRM through a variety of durability test in this study. With the result of the test, durability of the specimen applied with CRM has been more improved than the existing repairing and maintenance method, which is judged as because of the laminating effect due to reinforcement of epoxy impregnated of alkali-resistance fiber and double layered fiber reinforced seat.

Development of CFS Jacketing Retrofit Method for Rectangular High Strength Concrete Columns by Cross Sectional Shape Modification (4각형 고강도 콘크리트 기둥 단면 변형을 통한 CFS Jacketing 보강방법 개발)

  • Lee, Jong-Gil;Kim, Jang-Ho Jay;Park, Seok-Kyun;Kim, Jin-Keun
    • Journal of the Korea institute for structural maintenance and inspection
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    • v.14 no.6
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    • pp.153-161
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    • 2010
  • Numerous past studies have shown that safety and serviceability of many concrete infrastructures and buildings built in 1970's have far less strength capacities than their original intended design capacities, thereby requiring repair and strengthening. Currently, aged concrete structures are being repaired using various methods developed in the past. Unfortunately, these methods do not consider the specific conditions that these members are under, but they merely attach repairing materials on the external surface for random strength improvements. Therefore, in order to improve repair and strengthening methods by considering composite behavior between repairing material and structural member, enhanced construction methodologies are needed. Also, the enhanced repairing and strengthening methods must be able to be implemented on structural members constructed using high performance concrete to meet the present construction demand of building mammoth structures. Therefore, in this study, a repairing and strengthening method for retrofitting high strength concrete (HSC) columns that can effectively improve column performance is developed. A square HSC column's cross-sectional shape is converted to an octagonal shape by attaching precast members on the surface of the column. Then, the octagonal column surface is surface wrapped using Carbon Fiber Sheets (CFS). The method allows maximum usage of confinement effect from externally jacketing CFS to improve strength and ductility of repaired HSC columns. The research results are discussed in detail.

A Survey on the Break-down and Repair of the Power Tillers in Korea (동력경운기(動力耕耘機) 이용실태(利用實態) 조사분석(調査分析)(II) -고장(故障) 및 수리(修理)에 관(關)하여-)

  • Hong, Jong Ho;Lee, Chai Shik
    • Journal of Biosystems Engineering
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    • v.6 no.1
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    • pp.28-38
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    • 1981
  • A survey has been conducted to investigate the presents of breaks down and repair of power tiller for efficient use. Eight provinces were covered for this study. The results are summarized as follows. A. Frequency of breaks down. 1) Power tiller was breaken down 9.05 times a year and it represents a break down every 39.1 hours of use. High frequency of breaks down was found from the fuel and ignition system. For only these system, the number of breaks down were 2.02 and it represents 23.3% among total breaks down. It was followed by attachments, cylinder system, and traction device. 2) For the power tiller which was more than six years old, breaks down accured 37.7 hours of use and every 38.6 hours for the power tiller which was purchased in less than 2 years. 3) For the kerosene engine power tiller, breaks down occured every 36.8 hours of use, which is a higher value compared with diesel engine power tiller which break down every 42.8 hours of use. The 8HP kerosene engine power tiller showed higher frequency of break down compared with any other horse power tiller. 4) In October, the lowest frequency of break down was found with the value of once for every 51.5 hours of use, and it was followed by the frequency of break down in June. The more hours of use, the less breaks down was found. E. Repair place 1) 45.3% among total breaks down of power tiller was repaired by the owner, and 54.7% was repaired at repair shop. More power tiller were repaired at repair shop than by owner of power tiller. 2) The older the power tiller is, the higher percentage of repairing at the repair shop was found compared with the repairing by the owner. 3) Higher percentage of repairing by the owner was found for the diesel engine power tiller compared with the kerosene engine power tiller. It was 10 HP power tiller for the kerosene power tiller and 8 HP for the diesel engine power tiller. 4) 66.7% among total breaks down of steering device was repaired by the owner. It was the highest value compared with the percentage of repairing of any other parts of power tiller. The lowest percentage of repairing by owner was found for the attachments to the power tiller with the value of 26.5%. C. Cause of break down 1) Among the total breaks down of power tiller, 57.2% is caused by the old parts of power tiller with the value of 5.18 times break down a year and 34.7% was caused by the poor maintenance and over loading. 2) For the power tiller which was purchased in less than two years, more breaks down were caused by poor maintenance in comparison to the old parts of power tiller. 3) For the both 8-10 HP kerosene and diesel engine power tiller, the aspects of breaks down was almost the same. But for the 5 HP power tiller, more breaks down was caused by over loading in comparison to the old parts of power tiller. 4) For the cylinder system and traction device, most of the breaks down was caused by the old parts and for the fuel and ignition system, breaks down was caused mainly by the poor maintenance. D. Repair Cost 1) For each power tiller, repair cost was 34,509 won a year and it was 97 won for one hoar operation. 2) Repair cost of kerosene engine power tiller was 40,697 won a year, and it use 28,320 won for a diesel engine power tiller. 3) Average repair cost for one hour operation of kerosene engine power tiller was 103 won, and 86 won for a diesel engine power tiller. No differences were found between the horse power of engines. 4) Annual repair cost of cylinder system was 13,036 won which is the highest one compared with the repair cost of any other parts 362 won a year was required to repair the steering device, and it was the least among repair cost of parts. 5) Average cost for repairing the power tiller one time was 3,183 won. It was 10,598 won for a cylinder system and 1,006 won for a steering device of power tiller. E. Time requirement for repairing by owner. 1) Average time requirements for repairing the break down of a power tiller by owner himself was 8.36 hours, power tiller could not be used for operation for 93.58 hours a year due to the break down. 2) 21.3 hours were required for repairing by owner himself the break down of a power tiller which was more than 6 years old. This value is the highest one compared with the repairing time of power tiller which were purchased in different years. Due to the break down of the power tiller, it could not be used for operation annually 127.13 hours. 3) 10.66 hours were required for repairing by the owner himself a break down of a diesel engine power tiller and 6.48 hours for kerosene engine power tiller could not be used annually 99.14 hours for operation due to the break down and it was 88.67 hour for the diesel engine power tiller. 4) For both diesel and kerosene engine power tiller 8 HP power tiller required the least time for repairing by owner himself a break down compared with any other horse power tiller. It was 2.78 hours for kerosene engine power tiller and 8.25 hours fur diesel engine power tiller. 5) For the cylinder system of power tiller 32.02 hours were required for repairing a break down by the owner himself. Power tiller could not be used 39.30 hours a year due to the break down of the cylinder system.

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Crack Repairing Injection Method of Concrete Structure Using Injection Port and Removable Injector Integrated with Elastic Storage Hall and Smart Valve(TPS Method) (탄성 저장관과 스마트 밸브가 일체화된 주입 포트와 이동식 주입기를 이용한 콘크리트 구조물의 균열보수 주입공법 (TPS 공법)(건설신기술 제 822호))

Case Study on the Vertical Capacity of the Repaired Large Diameter Rock-Socketed Stool Pipe Pile (보수된 대구경 암반 소켈강관말뚝의 연직지지력에 관한 사례연구)

  • 최용규;김승종;김병희;이광욱;김상일
    • Proceedings of the Korean Geotechical Society Conference
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    • 1999.03a
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    • pp.185-192
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    • 1999
  • It had found that, as a result of cross-hole tonic logging test, concrete was not filled partially within the bottom 2.0 m of the large diameter (Ø= 2,500mm) rock socketed pile, MP20-P11(socket diameter (Ø= 2,200mm), which was a pile among piles group supporting a pier of Kwangan Grand Bridge. The pile was repaired by the combined cement grout injected through the pipes for the cross-hole sonic logging test and the bore holes for core samples. A month after the cement grouting, repairing was checked by coring and cross-hole sonic logging then 3 times of grouting and 2 times of coring were, in turns, peformed, then repairing was completed successfully. The vertical compressive capacity of the repaired large diameter socketed pile was evaluated by several formulas and software ROCKET, and was more conservative than design load (1,882 ton) of MP20-P11. It is expected that, in the case of the battered socketed piles, it could be more reasonable to analyze the behaviors of a battered pile using 3-D model. A 3-D analysis will be peformed in the future study.

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A Study of Analysis and Countermeasure of the Collapsed inclined shaft by a Heavy Rain (집중호우로 인한 OO터널 사갱 붕괴 원인 분석 및 대책에 관한 연구)

  • Yoon, Tae-Gook;Lee, You-Suk;Oh, Hyuk-Hee;Kim, Dong-Soo;Lee, Song
    • Proceedings of the Korean Geotechical Society Conference
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    • 2003.03a
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    • pp.241-248
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    • 2003
  • In August 2002, side wall of OO tunnel, at the Bonghwa, Kungbuk province, Korea, was collapsed by abruptly applied heavy soil and water pressure to side wall from a inclined shaft when there was a heavy rain. These days, Inclined shaft is used for the purpose of reducing construction time, using ventilation system, using the out of carrying equipment and mucking when we construct tunnel in the world. Recently constructed tunnel has the source of inclined shafts, but the more time elapse, we lose the source of the inclined shaft such as exact position, condition, and the fact that whether inclined shaft is exist or not. Therefore, this study inspected the interior's appearance, analyzed structure to evaluate the reason of collapsing side wall and this study also performed the repairing work. Finally, we show improving maintenance method to prevent that similar accident that might be happened.

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Reliability Assessment of Reinforced Concrete Beams Strengthened by CFRP Laminates (CFRP 적층판으로 보강된 철근콘크리트보의 신뢰성평가)

  • 조효남;최영민
    • Proceedings of the Computational Structural Engineering Institute Conference
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    • 1994.10a
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    • pp.160-166
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    • 1994
  • In general, the problems of strengthening and repairing of deteriorated or damaged reinforced concrete members are usually worked out in situ by externally bounding steel plates using epoxy resins, which has been recognized to be one of effective and convenient methods. But the disadvantages of strengthening/repairing concrete members with externally bonded steel plates include ; (a) deterioration of the bond at the steel-concrete interface caused by the corrosion of steel ; (b) difficulty in manipulating the plate at the construction site ; (c) improper formation of joints, due to the limited delivery lengths of the steel plates ; and etc. Therefore these difficulties eventually have led to the concept of replacing the steel plates by fiber-reinforced composite sheets which are characterized by their light weight, extremely high stiffness, excellent fatigue properties, and outstanding corrosion resistance. In the paper, for the reliability assessment of reinforced concrete beams externally strengthened by carbon fiber plastic(CFRP) laminates, an attempt is made to suggest a limit state model based on the strain compatibility method and the concept of fracture mechanics. And the reliability of the proposed models is evaluated by using the AFOSM method. The load carrying capacity of the deteriorated and/or damaged RC beams is considerably increased. Thus, it may be stated that the post-strengthening of concrete beams with externally bonded CFRP materials may be one of very effective way of increasing the load carrying capacity and stiffeness characteristics of existing structures.

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