• Title/Summary/Keyword: overhaul

Search Result 164, Processing Time 0.041 seconds

Optimization for the Design Parameters of Electric Locomotive Overhaul Maintenance Facility (전기 기관차 중수선 시설의 설계 변수 최적화)

  • Um, In-Sup;Cheon, Hyeon-Jae;Lee, Hong-Chul
    • Journal of the Korean Society for Railway
    • /
    • v.13 no.2
    • /
    • pp.222-228
    • /
    • 2010
  • In this paper, we propose a optimization approach for the Electric Locomotive Overhaul Maintenance Facility (ELOMF), which aims at the simulation optimization so as to meet the design specification. In simulation design, we consider the critical path and sensitivity analysis of the critical (dependent) factors and the design (independent) parameters for the parameter selection and reduction of the metamodel. Therefore, we construct the multi-objective non-linear programming. The objective function is normalized for the generalization of design parameter while the constraints are composed of the simulation-based regression metamodel for the critical factors and design factor's domain. Then the effective solution procedure based on the pareto optimal solution set is proposed. This approach provides a comprehensive approach for the optimization of Train Overhaul Maintenance Facility(TOMF)'s design parameters using the simulation and metamoels.

Estimation of the Overhaul Cycle Time for KTX Wheelset Bearing by RCF Test (RCF 시험을 통한 KTX 윤축베어링의 분해 정비 주기 평가)

  • Sim, Dae-Sop;Heo, Tae-Hyeon;Park, Young-il;Kim, Hong Seok;Shin, Ki-Hoon;Cheong, Seong Kyun
    • Journal of the Korean Society of Safety
    • /
    • v.31 no.1
    • /
    • pp.13-18
    • /
    • 2016
  • KTX wheelset bearings have thus far been maintained in accordance with the maintenance system of French national railway company, SNCF. The overhaul cycle time (OCT) of KTX wheelset bearings is now 1.4 million km in mileage. This value, however, has not been validated in Korea that has much different railway environments with France. In fact, it is impossible to validate OCT of wheelset bearings directly because they are disassembled and cleaned only when some faults are detected. In this paper, the accuracy of the current OCT value was evaluated indirectly by investigating the effect of grease lubricants on the bearing life. Five grease samples (one new and four aged greases) were used in this study. Four aged greases of different conditions were obtained from four wheelset bearings whose mileages were about 0.3, 1.2, 1.3, and 1.8 million km, respectively. Each grease sample was then injected into the RCF (Rolling Contact Fatigue) tester and fatigue lifetime was experimentally estimated. In addition, the wt% of Fe in each grease sample was analysed. The experiment results reveal that the bearing lifetime is inversely proportional to the mileage of grease sample while the wt% of Fe increases with the mileage of grease sample. Based on the experimental results, it can be concluded that the current OCT value is appropriate for the first overhaul of wheelset bearings. However, further validation is required to determine the second and third OCT values.

A case study on the vibration by fluid induced instability at large steam turbine-generator (대형 터빈-발전기에서의 유체 불안정진동 해소사례)

  • Han, Seung-Woo;Noh, Chel-Woo;Kim, In-Chul;Joo, In-Gouk;Kim, Myong-Shik
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
    • /
    • 2007.11a
    • /
    • pp.1066-1071
    • /
    • 2007
  • This case study refers to turbine-generator with retrofitted turbine rotor. Vibration problem occurring after the retrofit was mainly due to high vibration from exciter side. However, repeated test run and operation during scheduled maintenance caused high vibration from generator bearing, and post-overhaul test run before turbine vibration correction caused oil whip on the bearing. This case study shows how to analyze vibration condition of high turbine generator vibration detected during the post-overhaul test run and vibration condition of offline and online data to reflect it on establishing maintenance schedule and overhaul correction procedure. Vibration data could be acquired during steady load operation or even with varying speed and load. Each data is important for machinery condition evaluation. This case study shows that the vibration data during extreme condition is the key factor in analysis, which helps to find the machinery problem.

  • PDF

A Case Study on the Vibration by Fluid Induced Instability at Large Steam Turbine-generator (대형 터빈-발전기에서의 유체 불안정진동 해소사례)

  • Han, Seung-Woo;Roh, Cheol-Woo;Yoo, Mu-Sang;Kim, In-Chul;Joo, In-Gouk;Kim, Myong-Shik
    • Transactions of the Korean Society for Noise and Vibration Engineering
    • /
    • v.18 no.2
    • /
    • pp.238-246
    • /
    • 2008
  • This case study refers to turbine-generator with retrofitted turbine rotor. Vibration problem occurring after the retrofit was mainly due to high vibration from exciter side. However, repeated test run and operation during scheduled maintenance caused high vibration from generator bearing, and post-overhaul test run before turbine vibration correction caused oil whip on the bearing. This case study shows how to analyze vibration condition of high turbine generator vibration detected during the post-overhaul test run and vibration condition of offline and online data to reflect it on establishing maintenance schedule and overhaul correction procedure. Vibration data could be acquired during steady load operation or even with varying speed and load. Each data is important for machinery condition evaluation. This case study shows that the vibration data during extreme condition is the key factor in analysis, which helps to find the machinery problem.

Come fly with ME: The Impact of 3PLs within the aircraft Manufacturing, Repair and Overhaul Industry in the United Arab Emirates

  • Hassan, Fatima;Annabi, Carrie Amani
    • The Journal of Industrial Distribution & Business
    • /
    • v.10 no.4
    • /
    • pp.13-24
    • /
    • 2019
  • Purpose - This research explores the impacts of third-party logistics (3PLs) within the aircraft Maintenance, Repair and Overhaul (MRO) industry in the United Arab Emirates (UAE) to explore the role of collaborative relationships for improving outsourcing. Globalization and time based competition have changed business environments and challenged the conventional management strategies that are related to core competencies and operational models. Organizations are forced to devise innovative practices in which logistics outsourcing to 3PLs offers significant advantages. Research design, data, and methodology - This case study was conducted within a leading global aircraft MRO organization whose reach spans across Europe, the Middle East, Asia and the Americas. The methods used face to face semi-structured interviews, validated through further focus group discussions. Results - These findings highlight the effectiveness of collaborative relationships on their role to improve outsourcing and also demonstrated that MROs gain several advantages from 3PL arrangements. However, any gaps in outsourcing management elevates potential risks to organizations as well, which could result in reputational, operational and financial losses. Conclusions - Although generalizability is not possible due to the case study approach, generality suggests that in order to reduce reputational, operational and financial risks, enhanced collaboration with 3PLs is recommended to optimize outsourcing arrangements.

Consideration for Heat Exchanger Performance Evaluation with reduced spend fuel pool heat due to the long-term over-haul maintenance (장기 예방정비로 인한 사용후연료저장조 열원 감소가 열교환기 성능평가에 미치는 영향 고찰)

  • Park, Chan;Lee, Sung Ho
    • Transactions of the Korean Society of Pressure Vessels and Piping
    • /
    • v.16 no.1
    • /
    • pp.56-64
    • /
    • 2020
  • The safety related heat exchangers have been evaluated for their performance during the operation of the nuclear power plant. The evaluation program for the safety related heat exchanger was developed in 2010 and used by KHNP based on EPRI TR-10739 algorithms. The spend fuel pool heat exchanger is one of the safety related heat exchanger in the nuclear power plant and also evaluated for their performance. Recently the performance evaluation for the spend fuel pool heat exchanger was not available because of the decreased heat in the spend fuel pool due to the long term overhaul. This paper analyzes the main cause of evaluation failure in the evaluation process and suggests the criteria for the heat exchanger performance evaluation during the long term overhaul.

A Research on the Determining Model of the Optimizing Maintenance Interval in TBM for the Preventive Maintenance of Facilities (설비예방보전을 위한 TBM의 최적보전주기 설정모델 연구)

  • Kwon Oh-Woon;Lee Hong-Chul
    • Proceedings of the Korean Operations and Management Science Society Conference
    • /
    • 2003.05a
    • /
    • pp.105-117
    • /
    • 2003
  • The purpose of this research aimed at performing the easy design. and also the easy on-the-job application or the maintenance interval determination methodology by presenting the determining model or the optimizing maintenance interval in TBM for the preventive maintenance or facility TBM(time-based maintenance) as the preventive maintenance requires the adequate determination or the maintenance interval. The maintenance interval or TBM shall be applied differently for the each interval such as He patrol inspection, maintenance, overhaul inspection. exchange. And it is based on the composition level of equipment. The already informed theories or interval determination methodology for the patrol inspection. repair. and overhaul inspection are difficult for adopting because or the several restriction problems in applying the maintenance schemes as the theory So, the model for determining the optimizing exchange interval or part, maintenance interval of auxiliary machine, unit equipment etc. was presented to apply in the maintenance easily and appropriately.

  • PDF

Comparison of AMO System between Korea and US (우리나라와 미국의 승인된 정비조직 제도 비교)

  • Joe, Hyunmyung
    • Journal of Aerospace System Engineering
    • /
    • v.10 no.2
    • /
    • pp.27-33
    • /
    • 2016
  • For the continued airworthiness of aviation products, aviation authority requires that every manufacturer should provide ICA(Instruction of Continued Airworthiness) to their users, and the users should follow it by themselves or using another approved maintenance agent. To reduce the cost and improve performance quality of maintenance activities, lots of users tries to outsource this job. To perform maintenance or repair of other owned air products, an air carrier and aviation maintenance companies should obtain AMO(approval of maintenance organization). It means AMO is a postulation to enter MRO(Maintenance Repair and Overhaul) market. For that, this paper discusses the comparison of requirements and procedures of AMO system between Korea and US to help understand the AMO system, and then, tries to point out what improvement should be made to Korean AMO system to be more effective, efficient and safe.

Study on the Development of Condition Monitoring Technology for Turbine Lubricating Systems in Power Plants (발전용 터빈 윤활계통 기계시스템의 상태진단기술 개발연구)

  • 신규식;김재평;남창현;백수곤;권오관;안효석;윤의성;손동구
    • Tribology and Lubricants
    • /
    • v.10 no.4
    • /
    • pp.51-58
    • /
    • 1994
  • Condition monitoring technology has recently been received much attention in the light of its significance on the maintenance of complex machineries such as turbines in power plants. Currently, turbines in power plants are maintained by scheduled overhaul based on the manufacturer's recommendations and the utility's experience. Although this preventive maintenance is known to be very effective, operators have less access to identify failure of elements when it happens between overhaul period. Therefore, in this study, a development of a on-line condition monitoring system through wear debris analysis of lubricating oils is aimed with a view to detecting abnormal wear behaviour of bearings and other wet-components at an early stage, allowing better outage scheduling and minimizing forced outages. For field application purposes, the on-line system developed was installed on the turbine of the No.4 unit at Ulsan Power Plant and its performance has been evaluated on site.