• Title/Summary/Keyword: motor and reducer

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A Study on the Design of Horizontal Traverse Units in an Automatic Object Changer Unit to Establish a Flexible Production System (Part 2) (유연생산 시스템 구축을 위한 공작물 자동교환 유닛의 수평 이송 기구 설계에 관한 연구(파트 2))

  • Park, Hoo-Myung;Sung, Jae-Kyung;Lee, Yong-Joong;Ha, Man-Kyung
    • Journal of the Korean Society of Manufacturing Process Engineers
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    • v.7 no.2
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    • pp.52-59
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    • 2008
  • The objective of this study is to develop an automatic object changer unit to improve processing problems existed in the conventional horizontal machining center. To achieve this goal, this study designed a horizontal transfer as the second project continued to the first project that designed a upward and downward traverse unit. A horizontal traverse unit shows a symmetric structure and consists of frame, which consists of four unit tools, motor and reducer, which are fixed at a frame, operation unit with pinions, first traverse unit, and second traverse unit. Constraint conditions based on the operation mechanism with these elements were configured and obtained following results after modeling a model for a traverse motor. In the kinematic expression of sliding motion with one degree of freedom, the sliding motion is constrained. Also, the rack 3 installed at a frame is used to configure possible kinematic constraint conditions of the rack 2 according to the rolling motion of the pinion 2 in the first traverse unit. In addition, the moment of inertia that is a type of kinetic energy in a converted horizontal traverse unit in the side of the reducer can be applied to introduce the moment of inertia of a converted horizontal traverse unit in the side of the reducer by using the sum of kinetic energy in the rack and pinion, which is a part of the horizontal traverse unit. Also, the equation of motion of the converted upward and downward traverse unit in the side of the motor using the equation of motion of the motor. Furthermore, the horizontal traverse unit predetermines the mass of the first and second traverse unit and applied load including the radius and reduction ratio of the pitch circle in the pinion 1 and applied load to the rack 2. Then, a proper motor can be determined using several parameters in the upward and downward traverse unit in order to verify such predetermined specifications. In future studies later this study, a simulation that verifies the results of the previous two stages of studies using a finite element method.

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A Study on Structural Safety and Advanced Efficiency for a Drywell Type Reducer (누유방지형 감속기의 구조적 안전성 및 토크효율 향상에 관한 연구)

  • Oh, Sang-Yeob
    • Transactions of the Korean Society of Mechanical Engineers A
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    • v.35 no.11
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    • pp.1399-1406
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    • 2011
  • The reducer of the mixer is one of the main parts of the processor used for water and wastewater treatment. In this study, an advanced reducer with a drywell structure was developed in order to prevent oil leakage during operation in the field. During the development of the advanced reducer prototype, a mockup, a metal mold, and a cast were made using CAD and a CNC machine. The structural safety of the reducer prototype's lower housing (drywell structure) was checked using the ALGOR commercial FEM analysis code, which yielded a von Mises stress of about 123 N/mm2, which is below the yield stress of 250 N/$mm^2$, and a natural frequency of about 650-700 Hz. In addition, the torque transmission efficiency for the advanced prototype was 95.87%, which is about 8% more than that found in a previous study, 88.45%, and the sound level was below 75 dB. Furthermore, no oil leakage or abnormal sound or vibration occurred. Therefore, an optimally designed advanced reducer prototype has been successfully developed.

A Study on Noise Reduction for the Driving System of a Forklift (지게차 구동부의 소음 진동 저감에 대한 연구)

  • Kim, Woo-Hyung;Hong, Il-Hwa;Chung, Jin-Tai
    • Transactions of the Korean Society for Noise and Vibration Engineering
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    • v.18 no.1
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    • pp.80-86
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    • 2008
  • In this study. the noise sources were identified and the noise and vibration were reduced for an industrial forklift. To identify the noise sourses, noise signals were measured by a microphone on a driver seat and these signals were analyzed with a waterfall plot. For this purpose, the gear mesh frequencies from the gear box of a reducer were not only investigated but noise/vibration sourses of an electric motor were also examined. Furthermore, the frequency response functions were obtained to confirm the vibration and noise sourses. It was found that severe vibration and noise were generated in the casing and the connecting part of the reducer. The severe vibration and noise could be reduced by a structure modification.

Study on the Shift Characteristics of a 2speed Manual Transmission apply to V-Blet (V-blet를 적용한 2단 수동변속기의 변속특성에 관한 연구)

  • Youm, Kwang-wook
    • Journal of the Korean Institute of Gas
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    • v.24 no.6
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    • pp.55-60
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    • 2020
  • As research and development of eco-friendly vehicles are expanding worldwide, additional devices of vehicles are reduced or deleted to increase the mileage, or research is being conducted to reduce weight. Among them, the multi-stage transmission that was applied to the internal combustion engine vehicle was deleted and replaced with a reducer, and the initial driving power is secured by increasing the torque through the control of the motor output value. However, since frequent motor speed change can result in a load increase, this study attempts to develop a compact and lightweight manual two-stage reducer with a general reducer structure. Therefore, a two-speed transmission with two gear ratio was designed by inserting a large gear and a small gear in a structure with a parallel shaft to connect the gears with a V-belt in the form of a parallel shaft reducer, and setting the gear ratio of the low and high gears respectively. In addition, power performance according to the rotational speed and load of the transmission was checked through a test, and the heat generation characteristics generated during driving were checked to verify the validity of the transmission.

Speed reducer be indicated a power using of elastic strain (탄성 변형을 이용한 동력이 표시되는 감속기)

  • Noh, S.Y.;Nam, W.K.;Kang, H.K.;Kim, N.I.;Kim, Y.T.;Oh, S.H.
    • Journal of Power System Engineering
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    • v.10 no.4
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    • pp.181-186
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    • 2006
  • In this paper, a noncontact type torque meter using silicone rubber to measure the exact torque value and reduce a vibration and a noise, was developed. When planetary gear speed reducer runs, torque, RPM etc.. of motor change according to load or speed change. So, it needs a device to detect load's change or to diagnose the state of thewhole drive department by monitoring these result values. The noncontact type torque meter using silicone rubber that we're trying to develop this time is low-cost and can measure RPM and torque value simply. Also, it caculate a power using this value and indicate them on screen.

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A Revolute Robot Manipulator with a New Structure (새로운 구조의 다관절 로봇 매니퓰레이터)

  • Choi, Hyung-Sik;Kim, Young-Sik;Baek, Chang-Yul
    • Transactions of the Korean Society of Mechanical Engineers A
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    • v.28 no.5
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    • pp.539-546
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    • 2004
  • Conventional robot manipulators actuated by motors with the speed reducer such as the harmonic drive have weakness in the load capacity, since the speed reducer does not have enough strength. To overcome this, a new type of the robot actuator based on the four-bar-link mechanism driven by the ball screw was proposed and constructed. Also, a new type of a revolute-jointed robot manipulator composed of the developed actuators was developed. The base axis is actuated by the motor with the conventional speed reducer, but the other axes are actuated by the proposed actuators. The kinematics and dynamics of the robot were analyzed, and the performance test of the robot was made. Through the test results, the performance of superior load capacity versus the robot weight is shown.

The driving system design of walking robot which uses the automotive window motor (자동차용 윈도우 모터를 이용한 보행로봇 구동부 설계)

  • YOUM, K.W.;HAM, S.H.;OH, S.H.
    • Journal of the Korean Society of Mechanical Technology
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    • v.13 no.4
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    • pp.137-141
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    • 2011
  • Driving mechanism, the central part of a robot, was designed in this study. Power for the motive drive was acquired by directly connecting the motor shaft in worm shape of the low-end DC motor, car window motor, to a decelerator. The decelerator consists of a worm gear to receive power from the motor shaft, a pinion gear to be connected in line with the worm gear, and an output shaft to be engaged to the pinion gear. Motion driving is achieved by the power from the motor shaft with the designed gears, transferred to the deceleration mechanism and to the output gear.

An Experimental Study on Motor Noise Reduction of Electric Power Steering (전동식 파워스티어링 모터소음 저감을 위한 실험적 연구)

  • You, C.J.
    • Journal of Power System Engineering
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    • v.12 no.6
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    • pp.83-87
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    • 2008
  • EPS(Electric Power Steering) system, which has replaced the hydraulic steering system(HPS or HPAS) in many passenger cars recently, have many merits such as low energy consumption, easy mounting, light weight and improvement of environmental pollution. However, EPS system has the problem of motor noise when motor is rotated, which can make a driver feel uncomfortable. There are many techniques to solve those problems, but they are not clear. It is necessary to evaluate the mechanical noise in steering systems, because an EPS has vibration sources such as at the motor gear reducer, manual gears and intermediate joints. In this paper, reduction technique of EPS motor noise is introduced.

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A Study on Tooth Profile Modification of Planetary Reducer for 120kW Class Monorail (120kW급 모노레일용 유성기어감속기의 치형수정에 관한 연구)

  • Jeong, Yeong-Sik;Kim, Nam-Kyung;Xu, Zhezhu;Lyu, Sung-Ki
    • Journal of the Korean Society of Manufacturing Process Engineers
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    • v.11 no.6
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    • pp.195-200
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    • 2012
  • In this study, parameters and requirements of an 120kW class monorail planetary gearbox was analysed and the adaptive planetary gearbox design was selected. The specification of the sun gear, planetary gear and carrier was set and the profile & lead was optimized. The mechanical efficiency of the optimized one and the original one was observed. Dynamo-tester system was used to observe the mechanical efficiency of the planetary gearbox. A dynamo unit was connected with the planetary gearbox which straightened through the motor by a coupling. The standard tooth shape planetary gearbox and modified tooth shape planetary gearbox were used as test pieces and the rotation speed was set from 600 to 6000rpm with 600rpm, 2.5min one step. In order to check the mechanical efficiency of the planetary gearbox, the tests were done as follows. 1) The power loss between driving motor and dynamo tester. 2) Temperature variation by different rotation speeds. 3) Noise variation by different rotation speeds.

Analysis of 2 step gear reducer in machine tool spindle (공작기계 주축용 2단 치차 감속기 해석)

  • 장영도;장희락;여진욱
    • Proceedings of the KAIS Fall Conference
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    • 2001.11a
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    • pp.99-103
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    • 2001
  • Though the research and the development in the field of machine tool was focused on high precision and high speed machine these days, traditional gear reduction device has been used to increase the cutting force which was transmitted from power source, motor In this study, analysis of 2 step gear reducer used in machining center spindle was carried out by using APM WinMachine which is commercial software for the analysis of machine element and system. For the analysis of this device, first of all, the analysis of power source and the transmitting of it were carried out. Then, machine elements like gear, shaft, bearing, and the forth, was analyzed in the view point of life time, static strength, stiffness, fatigue failure, etc. Consequently, we can estimate them and introduce new idea of the design modification of reduction device by this study.