• Title/Summary/Keyword: counterweight fill

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A Case Study of Extra Reinforcement by Road Extension work on Existing Cut Slope Reinforced with Counterweight Fill and Stabilizing Piles (압성토 및 억지말뚝으로 보강된 도로의 확장공사로 인한 추가 보강사례 연구)

  • Park, Jeong-Yong;Kim, Woo-Seong;Kim, Jae-Kyoung;Yang, Tae-Sun;Na, Kyung-Joon
    • Journal of Korean Society of societal Security
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    • v.1 no.2
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    • pp.67-72
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    • 2008
  • To confirm the stability of a cut slope in the road extension construction site, several investigations were carried out and countermeasures of slope was studied. This paper describes a study of design case of extra reinforcement on existing cut slope reinforced by preloading and piles in roads. To investigate the effect of stabilizing piles installed in a cut slope, an instrumentation system also designed, was. As a result that the stabilizing file and earth anchor are considered as the extra reinforcement, both stabilizing pile and earth anchor guarantee the stability of cut slope. However, stabilizing pile is selected in aspects of economy and continuity to the existing cut slop reinforcement including counterweight fill and stabilizing piles.

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A Study on the Lateral Movement of Bridge Abutment Using Centrifuge Test and Numerical Analysis (원심모형시험과 수치해석을 이용한 교대 측방유동에 관한 연구)

  • Yoo, Wan-Kyu;Kim, Ki-Il;Kim, Byoung-Il
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.11 no.5
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    • pp.1799-1804
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    • 2010
  • In regard to fill loading structures such as bridge abutments and retaining walls on soft ground, the soft ground undergoes excessive deformation, which causes the lateral movement of the ground, resulting in increased risk of much damage. In this study, a centrifuge model test was conducted to check the possibility of lateral movement of a bridge abutment during back filling in a field, and a numerical analysis considering the lateral movement of the bridge abutment under the influence of the counterweight fill method applied during construction was carried out by using MIDAS/GTS as the FEM(Finite Element Method) program. The results of this study showed that the lateral movement of the abutment can exceed the allowable lateral movement value(15mm), and that the counterweight fill method was effective for the stability of the lateral movement.

Case Study of the Stability of a Large Cut-Slope at a Tunnel Portal (터널 입구부 대절토 사면 안정성 사례 연구)

  • Park, Dong Soon;Bae, Jong-Soem
    • The Journal of Engineering Geology
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    • v.25 no.1
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    • pp.115-129
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    • 2015
  • The cut-slope of a large-sectional tunnel portal is recognized as a potential area of weakness due to unstable stress distribution and possible permanent displacement. This paper presents a case study of a slope failure and remediation for a large-scale cut-slope at a tunnel portal. Extensive rock-slope brittle failure occurred along discontinuities in the rock mass after 46 mm of rainfall, which caused instability of the upper part of the cut-slope. Based on a geological survey and face mapping, the reason for failure is believed to be the presence of thin clay fill in discontinuities in the weathered rock mass and consequent saturationinduced joint weakening. The granite-gneiss rock mass has a high content of alkali-feldspar, indicating a vulnerability to weathering. Immediately before the slope failure, a sharp increase in displacement rate was indicated by settlement-time histories, and this observation can contribute to the safety management criteria for slope stability. In this case study, emergency remediation was performed to prevent further hazard and to facilitate reconstruction, and counterweight fill and concrete filling of voids were successfully applied. For ultimate remediation, the grid anchor-blocks were used for slope stabilization, and additional rock bolts and grouting were applied inside the tunnel. Limit-equilibrium slope stability analysis and analyses of strereographic projections confirmed the instability of the original slope and the effectiveness of reinforcing methods. After the application of reinforcing measures, instrumental monitoring indicated that the slope and the tunnel remained stable. This case study is expected to serve as a valuable reference for similar engineering cases of large-sectional slope stability.

A Case Study on the Slope Collapse and Reinforcement Method of the Phyllite Slope (천매암 지역에서의 비탈면 붕괴 원인규명 및 보강대책 사례연구)

  • Cho, Younghun;Lim, Daesung;Chun, Byungsik
    • Journal of the Korean GEO-environmental Society
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    • v.11 no.8
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    • pp.83-93
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    • 2010
  • The purpose of this study is to present emergency rehabilitation, cause and the countermeasure of reinforcement about reinforced retaining wall and the slope collapse of the phyllite ground. The study area is broken easily because this area has rock mass discontinuity such as stratification, foliation, joint and fold. And this area consists of the ground where it happens easily to the failure of structure like reinforced retaining wall because of the phyllite ground sensitive to weathering. Counterweight fill in front of reinforced retaining wall was performed as emergency rehabilitation about displacement of reinforced retaining wall and the failure at the rear of slope on phyllite ground. After that, additional displacement didn't occur. Boring and geophysical exploration were launched to present emergency rehabilitation and develop the long-term method of reinforcement. This could grasp anticipated range of the failure section and identify internal and external factors of the cause of the slope collapse. Several methods of reinforcement were suggested by conducting the numerical analysis. When conducting design and construction of major structures at the ground which has complex discontinuities, the precise site investigation should be conducted. During construction, immediate action for over-displacement should be taken by performing the periodic measurement.