• 제목/요약/키워드: TMS320C32

검색결과 113건 처리시간 0.023초

DSP를 이용한 가라오케용 고음질 멀티채널 오디오 시스템 (High Quality Multi-Channel Audio System for Karaoke Using DSP)

  • 김태훈;박양수;신경철;박종인;문태정
    • 한국음향학회지
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    • 제28권1호
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    • pp.1-9
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    • 2009
  • 본 논문에서는 멀티채널 라이브 가라오케의 구현에 관한 내용을 담고 있다. TI사의 32비트 floating 연산 DSP인 TMS320C6713를 이용하여 6 채널의 MP3 복호화 및 템포/키 변환을 실시간으로 구현하였다. 6채널은 전면 L/R 악기, 후면 L/R 악기, 멜로디, 우퍼로 구성되며, 4 채널로 동작 시에는 후면 L/R 대신 드럼 L/R이 추가될 수 있다. 최종 출력 데이터는 5.1 채널 스피커에 맞춰서 출력된다. 템포 변환을 위하여 SOLA알고리즘을 적용시켰으며 시간영역에서 인터폴레이션(interpolation)과 데시메이션 (decimation)으로 키 변환을 수행하였다. 드럼 악기가 추가될 경우에는 일반악기와 분리하여 키 변환 시에 드럼 채널을 제외시키고, SOLA (Synchronized Overlap and Add) 수행 시에도 SOLA처리 단위인 프레임 사이즈를 다르게 두어 고음질의 템포 변환이 가능하도록 하였으며, 실시간 처리를 위하여 최적화를 하였다 6 채널을 이용하여 다양한 채널 구성이 가능하며 본 논문의 멀티채널 오디오 시스템은 고음질의 라이브 반주가 필요한 어느 곳에서나 효과적으로 적용될 수 있다.

Z축 운전구조를 갖는 선형 영구자석형 동기 전동기 운전제어에 관한 연구 (A study of control system on Permanent Magnet Linear Synchronous Motor with Z-axis operation structure)

  • 이진하;최철;박한웅;김철우
    • 전력전자학회:학술대회논문집
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    • 전력전자학회 2003년도 춘계전력전자학술대회 논문집(2)
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    • pp.654-658
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    • 2003
  • In this study a control system with variable gain schedule using real speed and moving direction is proposed to control a Permanent Magnet Linear Synchronous Motor (PMLSM) with Z-axis operation structure. The implementation of the controller is designed on the DSP TMS320C32 board. PMLSM is operated by using 4-point absolute positions profile with each velocity, acceleration and deceleration. The direction of the initial angle action for starting is set from the lower limit point to the upper limit point on PMLSM operation stroke. The effectiveness of a control system with variable gain schedule is demonstrated by some experimental results.

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추진제어장치 특성 연구 (The study of propulsion control system)

  • 권일동;김동명;정은성;이상준;최종묵
    • 한국철도학회:학술대회논문집
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    • 한국철도학회 2005년도 춘계학술대회 논문집
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    • pp.291-298
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    • 2005
  • This paper describes the characteristic feather of propulsion system adopting mass production. The train formation is composed of 4 cars by 2 Motor cars and 2 Train cars. Acceleration rate must be 3.0 km/h/s or more when the car starts up to 35km/h by 16ton of passenger load. The system information supervision is easy because the system is controlled to perfect digital circuits, all information of an action is stored in a memory and is managed. The control system is composed of a fully digital circuit and a high level software such as C language. The DSP TMS320C31 is used for main processor and has the capability of 50MHz, 32bit floating point operation and has a C compiler. Therefore, the implementation of control algorithm and the change of function are easy. VVVF inverter using IGBT conducted variable combined test, environment test using chamber, interface test and field test etc.

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Optimal Efficiency Control for Induction Motor Drives

  • Kim Sang-uk;Choi Jin-ho;Kim Bo-youl;Kim Young-seok
    • 전력전자학회:학술대회논문집
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    • 전력전자학회 2001년도 Proceedings ICPE 01 2001 International Conference on Power Electronics
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    • pp.428-433
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    • 2001
  • This paper presents the control algorithm for maximum efficiency drives of an induction motor system with the high dynamic performance. This system uses a simple model of the induction motor that includes equations of iron losses. The model, which only requires the parameters of induction motor, is referred to a field-oriented frame. The minimum point of the input power can be obtained at the steady state condition. The reference torque and flux currents for the vector control of induction motors are calculated by the optimal efficiency control algorithm. The drive system with the proposed efficiency optimization controller has been implemented by a 32 bit floating point TMS320C32 DSP chip. The results show the effectiveness of the control strategy proposed for the induction motor drive.

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Synthesis and Experimental Implementation of DSP Based Backstepping Control of Positioning Systems

  • Chang, Jie;Tan, Yaolong
    • Journal of Power Electronics
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    • 제7권1호
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    • pp.1-12
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    • 2007
  • Novel nonlinear backstepping control with integrated adaptive control function is developed for high-performance positioning control systems. The proposed schemes are synthesized by a systematic approach and implemented based on a modern low-cost DSP controller, TMS320C32. A baseline backstepping control scheme is derived first, and is then extended to include a nonlinear adaptive control against the system parameter changes and load variations. The backstepping control utilizes Lyapunov function to guarantee the convergence of the position tracking error. The final control algorithm is a convenient in the implementation of a practical 32-bit DSP controller. The new control system can achieve superior performance over the conventional nested PI controllers, with improved position tracking, control bandwidth, and robustness against external disturbances, which is demonstrated by experimental results.

Vector Control of Induction Motors using Optimal Efficiency Control

  • Kim, Sang-uk;Chi, Jin-ho;Kim, Young-seok
    • Journal of Power Electronics
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    • 제2권1호
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    • pp.67-75
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    • 2002
  • This paper presents the control algorithm for maximum efficiency drives of an induction motor system with the high dynamic performance. This system uses a simple model of the induction motor that includes equations of the iron losses. The model, which only requires the parameters of the induction motor, is referred to a field-oriented frame. The minimum point of the input power can be obtained at the steady state condition. The proposed optimal efficiency control algorithm calculates the reference torque and flux currents for the vector control of the induction motors. A 32 bit floating point TMS320C32 DSP chip implements the drive system with the efficiency optimization controller. The results show the effectiveness of the control strategy Proposed for the induction motor drive.

비선형 부하에서 커패시터 전류 궤환을 통한 고성능 UPS 설계 (A Design of a High Performance UPS with Capacitor Current Feedback for Nonlinear Loads)

  • 이우철;이택기
    • 조명전기설비학회논문지
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    • 제26권5호
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    • pp.71-78
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    • 2012
  • This paper presents a digital control solution to process capacitor current feedback of high performance single-phase UPS for non-linear loads. In all UPS the goal is to maintain the desired output voltage waveform and RMS value over all unknown load conditions and transient response. The proposed UPS uses instantaneous load voltage and filter capacitor current feedback, which is based on the double regulation loop such as the outer voltage control loop and inner current control loop. The proposed DSP-based digital-controlled PWM inverter system has fast dynamic response and low total harmonic distortion (THD) for nonlinear load. The control system was implemented on a 32bit Floating-point DSP controller TMS320C32 and tested on a 5[KVA] IGBT based inverter switching at 11[Khz]. The validity of the proposed scheme is investigated through simulation and experimental results.

PLC의 시퀀스 제어를 위한 BIT 연산 프로세서의 구현 (An Implementation of Bit Processor for the Sequence Logic Control of PLC)

  • 유영상;양오
    • 대한전기학회:학술대회논문집
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    • 대한전기학회 1999년도 하계학술대회 논문집 G
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    • pp.3067-3069
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    • 1999
  • In this paper, A bit processor for controlling sequence logic was implemented, using a FPGA. This processor consists of program memory interface. I/O interface, parts for instruction fetch and decode, registers, ALU, program counter and etc. This FPGA is able to execute sequence instruction during program fetch cycle, because of divided bus system, program bus and data bus. Also this bit processor has instructions set that 16bit or 32bit fixed width, so instruction decoding time and data memory interface time was reduced. This FPGA was synthesized by pASIC 2 SpDE and Synplify-Lite synthesis tool of Quick Logic company. The final simulation for worst cases was successfully performed under a Verilog HDL simulation environment. And the FPGA programmed for an 84 pin PLCC package. Finally, the benchmark was performed to prove that Our FPGA has better performance than DSP(TMS320C32-40MHz) for the sequence logic control of PLC.

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100kV급 비상발전기용 통합제어기 (Unified Controller for 100kVA Emergency Generator)

  • 정창용;조정구;백주원;이종주;김용주;유동욱
    • 대한전기학회:학술대회논문집
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    • 대한전기학회 1999년도 하계학술대회 논문집 F
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    • pp.2801-2803
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    • 1999
  • An unified controller for emergency generator is presented to control AVR and Governor and l00kVA power conditioner. This controller is operated to compensate current harmonics and asymmetries caused by nonlinear load and unbalance loads. The power conditioner shapes the source current sinusoidal in phase with source voltage and allows the generator to maximum power even to the single phase load. Also this power conditioner allows that three phase generator synchronizes with single phase main source and load sharing. An l00kVA generator system was built and the unified controller is realized with DSP(TMS320C32PCMA). Experimental results for many load conditions are presented to verify the performance of the unified controller.

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DSP-Based Direct Source Current Control for Three-Phase Four-Wire Power Coditioner

  • Jeong, C.Y.;Cho, J.G.;Baek, J.W.;Yoo, D.W.;Song, E.H.
    • 전력전자학회:학술대회논문집
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    • 전력전자학회 1998년도 Proceedings ICPE 98 1998 International Conference on Power Electronics
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    • pp.871-875
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    • 1998
  • A DSP-based source current control for power conditioner is presented to compensate current harmonics and asymmetries of three-phase four-wire emergency generators caused by nonlinear and/or unbalanced loads. There-phase voltage type converter with split-dc-capacitor is adopted as the power circuit and a new direct source current control method is suggested, which simplifies the controller. The proposed control method shapes the generator current sinusoidally inphase with the voltage and allows the generator to supply maximum power even to single phase loads. An IGBT base lookVA prototype with the controller realized with a DSP (TMS320C32) is built and tested to verify the performance of the power conditioner.

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