• Title/Summary/Keyword: Supply Air Injection Angle

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Numerical simulation of turbulent air-flow in a closed engine room with heat source in a ship (열원이 있는 밀폐된 선박 기관실에서의 난류기류에 관한 수치적 연구)

  • 박찬수
    • Journal of Advanced Marine Engineering and Technology
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    • v.22 no.1
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    • pp.100-107
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    • 1998
  • Ventilation of the marine engine room is very important for the health of the workers as well as the nomal operation of machines. To find proper ventilation conditions of this engine room, numerical simulation with standard k-.epsilon. model was carried out. In the present study, the marine engine room is considered as a closed space with a heat source and forced ventilation ducts. The injection angle of air supply is found to be important. Injection with downword angle depresses recirculation flow, causing a strong steam in the wider space of the room. Ventilation and removal of the released heat are promoted with this pattern. There is a possibility of local extreme heating at the upper surface of engine when supply and exhaust ports of air are in bilateral symmetry. The effect of the increase of exhaust port area on ventilation decreases as the number of supply port increases.

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Heat transfer of Mixed convection in rectangular space with constant heat flux (일정 열유속의 열원을 갖는 사각공간의 혼합대류 열전달)

  • 조대환
    • Journal of Advanced Marine Engineering and Technology
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    • v.23 no.4
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    • pp.552-558
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    • 1999
  • Ventilation of the marine engine room is very important for the health of the workers as well as the normal operation of machines. To find proper ventilation conditions of this engine room numerical simulation with a standard k-$\varepsilon$model was carried out. In the present study the marine engine room is considered as a closed space with a heat source and forced ventilation ducts. The injection angle of air supply is found to be important. Injection with a downward angle depresses recirculation flow causing a strong stream in the wider space of the room Ventilation and removal of the released heat are promoted with this pattern, There is a possibility of local extreme heating at the upper surface of the engine when supply and exhaust ports of air are in bilateral symmetry.

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Stabilization Characteristics of Diffusion Flame with Auxiliary Fuel Supply through a Bluff Body (보조연료의 공급이 확산화염의 보염특성에 미치는 영향)

  • An, J.G.;Song, K.K.
    • Journal of the Korean Society of Combustion
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    • v.1 no.1
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    • pp.11-18
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    • 1996
  • The stabilization characteristics of diffusion flame formed behind a bluff body with fuel injection slits was experimentally investigated by varying main fuel injection angles and auxiliary fuel injection conditions. The flame stability limits, temperature and length of recirculation zone, direct and schlieren photographs of flames were measured in order to study the stabilization mechanism of the diffusion flame. The results of this investigation are as follows. The stability limits can be improved by the condition of the kind and quanity of the injected auxiliary fuel. The length and temperature decrease with injection of auxiliary fuel, and these phenomena are remarkable when LPG is injected into the recirculation zone. When the LPG is injected into the recirculation zone, flame remains sooty. Fluctuation of fuel and main stream is generated actively by air injection.

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Study on the Spray Characteristics of a Port Fuel Injector for a Gasoline Engine (가솔린엔진용 포트분사식 인젝터의 분무특성에 관한 연구)

  • Lee, Sang-In;Lee, Sung-Won;Park, Sung-Young
    • Journal of ILASS-Korea
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    • v.15 no.2
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    • pp.61-66
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    • 2010
  • Fuel spray characteristics of the gasoline engine injector has been studied experimentally. To provide fundamental performance data of 4-hole and 12-hole injectors, spray fuel-mass distribution, wall wetting fuel amount and visualization of injectors have been tested and measured with various fuel supply pressure conditions. Spray visualization has been performed to analyze spray formation, spray angle, stream width and penetration length. Test result shows that wall wetting is greatly influenced by the induction air amount and spray atomization. Spray visualization shows that the 12-hole injector has robust performance characteristics with various fuel supply pressure conditions compared with the 4-hole injector. 4-hole injector generates relatively less wall-wetting fuel amount than 12-hole injector does.

Spray Visualization of the Gas Turbine Vaporizer (가스터빈 기화기의 분무 가시화 연구)

  • Jo, Sungpil;Joo, Milee;Choi, Seongman;Rhee, Dongho
    • Journal of ILASS-Korea
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    • v.24 no.3
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    • pp.130-136
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    • 2019
  • Spray visualization of a vaporizer fuel injection system of a micro turbo jet engine was experimentally studied. The fuel heating by combustion was simulated by the high pressure steam generator and combustor inlet air from the centrifugal compressor was simulated by compressed air stored in the high pressure air tank. Spray visualization was performed with single vaporizer, and then six vaporizers which are same number of micro turbojet engine were used. As a results, the spray characteristics of the vaporizer were understood with pressure difference of the combustor inlet air and the fuel supply pressure. Spray angles with three types of vaporizer configuration were measured. In the results, guide vane configuration has a wider spray angle than the straight tube and smooth curve tube with a swirler, so it is expected that the fuel will be effectively distributed inside the combustor flame tube.

Failure Case Studies of Sensors for Electronic Controlled Engine in LPG Vehicle (LPG 자동차에서 전자제어엔진용 센서의 고장사례에 관한 연구)

  • Kim, Chung-Kyun;Lee, Il-Kwon
    • Journal of the Korean Institute of Gas
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    • v.14 no.4
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    • pp.56-62
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    • 2010
  • The purpose of this paper analyzes and investigates the failure case studies of electronic control sensors for a LP gas engine. The malfunction of crank angle sensor, which controls a fuel injection volume of LP gas, displays an irregular and non-uniform pulse wave form. The pulse form, which is related to the noise of the crank angle sensor, displays at the rectangular peak with a saw-toothed shape and is intermittently generated with a level of 2.46V noise signal. The malfunction of No. 1 TDC sensor in which is caused from the internal disorder affects to the reduction of engine power and engine stop suddenly. If the malfunction of oxygen sensor is occurred due to a wiring problem of a sensor connector, the LP gas vehicle may produce a shaking and disharmony of an engine because of no signal supply from the oxygen sensor. The air cleaner replica produces the clogging of continuous supply of fresh air. This may cause the retardation of vehicle acceleration and engine disharmony intermittently.

Humidification of Air Using Water Injector and Cyclonic Separator (관 내 삽입 인젝터와 사이클론을 이용한 공기 가습)

  • Kim, Beom-Jun;Kim, Sung-Il;Byun, Su-Young;Kim, Min-Soo;Kim, Hyun-Yoo;Kwon, Hyuck-Ryul
    • Transactions of the Korean Society of Mechanical Engineers B
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    • v.34 no.5
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    • pp.491-498
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    • 2010
  • Humidification of PEM fuel cells is necessary for enhancing their performance and lifetime. In this study, a humidification system was designed and tested; the system includes an air-supply tube (inner diameter: 75 mm) through which a nozzle can be directly inserted and a cyclonic separator for the removal of water droplets. Three types of nozzles were employed to study the influence of injection pressure, air flow rate, and spray direction on the humidification performance. To evaluate the humidification performance, the concept of humidification efficiency was defined. In the absence of an external heat source, latent heat for evaporation will be supplied by the own enthalpies of water and air. Thus, the amount of water sprayed from the nozzle is the most critical factor affecting the humidification efficiency. Water droplets were efficiently removed by a cyclonic separator, but re-entrainment occurred at high air flow rates. The absolute humidity and humidification efficiency were $21.29\;kJ/kg_{da}$ and 86.57%, respectively, under the following conditions: nozzle type PJ24; spray direction angle $90^{\circ}$; injection pressure 1200 kPa; air flow rate 6000 Nlpm.