• Title/Summary/Keyword: Sprue

Search Result 45, Processing Time 0.021 seconds

A study on the injection molding technology for thin wall plastic part (초정밀 박육 플라스틱 제품 성형기술에 관한 연구)

  • Heo, Young-Moo;Shin, Kwang-Ho
    • Design & Manufacturing
    • /
    • v.10 no.2
    • /
    • pp.50-54
    • /
    • 2016
  • In the semiconductor industry the final products were checked for several environments before sell the products. The burning test of memory and chip was implemented in reliability for all of parts. The memory and chip were developed to high density memory and high performance chip, so circuit design was also high integrated and the test bed was needed to be thin and fine pitch socket. LGA(Land Grid Array) IC socket with thin wall thickness was designed to satisfy this requirement. The LGA IC socket plastic part was manufacture by injection molding process, it was needed accuracy, stiffness and suit resin with high flowability. In this study, injection molding process analysis was executed for 2 and 4 cavities moldings with runner, gate and sprue. The warpage analysis was also implemented for further gate removal process. Through the analyses the total deformations of the moldings were predicted within maximum 0.05mm deformation. Finally in consideration of these results, 2 and 4 cavities molds were designed and made and tested in injection molding process.

A comparison of marginal fitness by dental alloys (치관 보철물 제작에 사용되는 치과용 금속의 변연 적합도 비교)

  • Kim, Nam-Joong;Hwang, Kyung-Sook;Park, Yong-Duk
    • Journal of Technologic Dentistry
    • /
    • v.25 no.1
    • /
    • pp.29-40
    • /
    • 2003
  • This study was aimed to verify a comparison by dental alloys upon the marginal fitness of dental prosthesis. Firstly, we waxed up on 45 epoxy resin dies, pressed the margin with hands, and identified the marginal fitness with microscope. And we made a single direct spruing system type of sprue by 3 dental alloys - metal crown alloys, PFM crown alloys, and gold crown alloys - each 15, total 45 waxing up, adjusting W/P ratio and invested the cast ring. Then, we made the dental prosthesis using the electric casting machine. In these processes we followed the manufacturer's instructions, in order to maintain the other conditions from the inner and outer, which included investment and burning out. After we tried on the dental prosthesis on epoxy resin dies, we have got the means of marginal gap at 9 points with same distances, around the cervical line which was checked already, using microscope($\times$300). The results of this study were as follows : 1. Metal crown alloys showed 2.9% better in marginal fitness than PFM crown alloys, and the difference was not statistically significant(P=0.497). 2. Gold crown alloys showed 31.3% better in marginal fitness than Metal crown alloys, and the difference was statistically significant(P=0.004). 3. Gold crown alloys showed 32.4% better in marginal fitness than PFM crown alloys, and the difference was statistically significant(P=0.002). 4. We saw that Gold crown alloys was the best dental alloys in the marginal fitness among the three.(P=0.049).

  • PDF

A Study on the Design/Simulation and Manufacturing for Localization of Parts in Scoop Control Assembly of Small Military Boat (소형 선박 제어 헤드 조립체의 국산화를 위한 설계/해석, 제작에 관한 연구)

  • Yeog, Gyeong-Hwan;Kim, Jae-Hyun;Jin, Chul-Kyu;Chun, Hyeon-Uk
    • Journal of the Korean Society of Industry Convergence
    • /
    • v.24 no.5
    • /
    • pp.597-608
    • /
    • 2021
  • The control head components used in small military vessels are designed to be domestically produced, prototypes, structural analysis, and casting methods are designed and cast. The control head assembly consists of a lever, an aluminum outside cover, Middle, front gear cover, back gear cover, and a zinc worm gear. In order to reverse the design of each component, 3D scanning device was used, 3D modeling was performed by CATIA, and prototype productions were carried out by 3D printer. In order to reduce the cost of components, gating system is used by gravity casting method. The SRG ratio of 1:0.9:0.6 was set by applying non-pressurized gating system to aluminum parts, 1:2.2:2.0 and pressurized gating system to zinc parts, and the shapes of sprue, runner and gate were designed. The results of porosity were also confirmed by casting analysis in order to determine whether the appropriate gating system can be designed. The results showed that all parts started solidification after filling completely. ANSYS was used for structural analysis, and the results confirmed that all five components had a safety factor of 15 more. All castings are free of defects in appearance, and CT results show only very small porosity. ZnDC1 zinc alloy worm gear has a tensile strength of 285 MPa and an elongation of 8%. The tensile strength of the four components of A356 aluminum alloy is about 137-162 MPa and the elongation is 4.8-6.5%.

A Study on the Gating System and Simulation for Gravity Casting of ZnDC1 Worm Gear (아연 합금 웜기어의 중력 주조 공정을 위한 주조 방안 설계 및 해석에 관한 연구)

  • Lee, Un-Gil;Kim, Jae-Hyun;Jin, Chul-Kyu;Chun, Hyeon-Uk
    • Journal of the Korean Society of Industry Convergence
    • /
    • v.24 no.5
    • /
    • pp.589-596
    • /
    • 2021
  • In this study, the optimum gating system was designed, and the two zinc alloy worm gears were manufactured in single process by applying a symmetrical gating system with 2 runners. The SRG ratio is set to 1 : 0.9 : 0.6, and the cross-sectional shapes such as sprue, runner and gate are designed. In order to determine whether the design of the gating system is appropriate, casting analysis was carried out. It takes 4.380 s to charge the casting 100%, 0.55 to 0.6 m/s at the gates and solidification begins after the casting is fully charged. The amount of air entrapment is 2% in the left gear and 6% in the right gear. Hot spots occurred in the center hole of the gear, and pores were found to occur around the upper part of the hole. Therefore, the design of the casting method is suitable for worm gears. CT analysis showed that all parts of worm gear were distributed with fine pores and some coarse pores were distributed around the central hole of worm gear. The yield strength and tensile strength were 220 MPa, 285 MPa, and the elongation rate was 8%. Vickers hardness is 82 HV.

Effect of different pattern size and pattern shape on castability of commercially pure titanium (납형의 크기와 형태가 티타늄의 주조성에 미치는 영향)

  • Seo, Yoon-Jeong;Oh, Gye-Jeong;Lee, Hyo-Il;Shin, Yoo-Jin;Kim, Hong-Joo;Park, Sang-Won
    • The Journal of Korean Academy of Prosthodontics
    • /
    • v.51 no.4
    • /
    • pp.261-268
    • /
    • 2013
  • Purpose: The purpose of this study was to investigate the effect of geometrically different wax pattern shapes and sizes on the castability of Grade2 Cp-Ti (commercially pure titanium). Materials and methods: Total of 40 mesh wax pattern ($61mm{\times}24mm$, 207 grids), ($61mm{\times}17mm$, 138 grids) was cast in this experiment. Depending on the geometrical shape of the wax pattern, 8 groups was organized; Flat, Semicircular, Horse-shoe and V-shape, each consisting 5 samples. Runner-bar sprue was used in all patterns. The number of completely cast grid in wax pattern served as a measure for the castability of comercially pure titanium. Results: The mean value of square count in each group was as followed; 133.20 squares in group SS (96.52%), 132.40 squares in group SH (95.94%), 132.00 squares in group SF (95.65%), 127.60 squares in SV (91.43%), 198.60 squares in group LF (95.94%), 197.80 squares in group LV (95.56%), 196.40 squares in group LS (94.88%), and 188.00 squares in group LH (90.82%). Conclusion: Within the limitations of this study the results indicate that there were no sttistically significant difference in castability of titanium regarding wax pattern shape (P>.05). However, Small size wax patterns were showing the noticeable castability more than Large size pattern.