• Title/Summary/Keyword: Shear actuator

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A Study on Analysis of J85 Engine V.G. Actuator Arm Shaft Crack

  • Hwang, Young-Ha;Son, Kyung-Sug;Kim, Tae-Gu
    • International Journal of Safety
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    • v.8 no.1
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    • pp.6-9
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    • 2009
  • The crack in a J85 engine V.G. actuator arm shaft for a bell crank on the engine compressor was investigated. The crack was observed in twenty two shafts during the inspection of 238 shafts. The failure analysis of shaft cracks was performed by chemical composition analysis using ICP(Inductively Coupled Plasma) and by fracture surface and microstructure analysis using FE-SEM and optical microscope. The crack initiated from the top and bottom and propagated to the center along the grain boundaries. From the chemical composition analysis, the fractography of the fracture surface and the microstructure, it was found that the failure mechanism of the shafts is the inclusion-related intergranular decohesion crack. The inclusion was found out from MnS particle by EDS(Energy Dispersive Spectroscopy). The crack initiated MnS inclusion in the grain boundary and propagated with the increase of applied shear stress during long operation. In order to prevent the fracture, NDI(Nondestructive inspection) is needed periodically as recommended.

Morphing wing using Macro Fiber Composite actuator (압전섬유작동기를 이용한 형상적응날개)

  • Na, Young-Ho;Kim, Ji-Hwan
    • Proceedings of the Korean Society For Composite Materials Conference
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    • 2005.04a
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    • pp.9-12
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    • 2005
  • Recently, research on the morphing wing is an interesting issue to develop the capability of the wing such as improving the lift and reduction of drag during the operation of an aircraft by changing the wing shape from one configuration to another. A more efficient weight reduction of the wing using smart or morphing wing concept can be achieved in comparison with the conventional flaps. In this study, it is investigated the behaviors of the morphing wing using Macro Fiber Composite (MFC) actuators. Generally, MFC is the piezocomposite actuator with the rectangular PZT fiber and epoxy matrix, and uses the interdigitated electrode to produce more powerful actuation in the in-plane direction. Furthermore, it can produce the twisting actuation as compared with the traditional PZT actuators. In the formulation, the first-order shear deformation plate theory is used, and finite element method is adopted in the numerical analysis of the model. Results show the characteristics of the static behavior of the morphing wing according to the change of the actuation voltage.

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Active Tension Control Using an ER Brake Actuator (ER브레이크 작동기를 이용한 능동 장력 제어)

  • Park, S.B.;Kim, G.W.;Cheong, C.C.
    • Journal of the Korean Society for Precision Engineering
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    • v.13 no.8
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    • pp.102-111
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    • 1996
  • This paper presents a proof-of-concept investigation on an active tension control using an ER (electro-rheological) brake actuator. Firstly, an ERF (electro-rheological fluid) which has an inherent reversible feature from Newtonian fluid to Bingham fluid upon applying an electric field is composed, and its property is tested to obtain intrinsic parameters of the Bingham model. An appropriate size of the ER brake is manufactured on the basis of the Bingham model, and dynamic characteristics of the brake are experimentally identified. After formulating a governing equation of motion of the tension control system, a sliding mode controller is designed to achieve a certain desired level of tension. Both simulation and experimental works are undertaken in order to demonstrate the efficiency and feasibility of the proposed active tension control method.

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An Experimental Study on the Structural Behavior of Steel Grid Shear Wall subjected to Axial Force and Cyclic Lateral Load (축력과 반복수평력을 받는 격자강판 내진보강벽의 구조거동에 관한 실험적 연구)

  • Park, Jung Woo;Sim, Ki Chul;Park, Jin Young;Lee, Young Hak;Kim, Heecheul
    • Journal of the Computational Structural Engineering Institute of Korea
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    • v.25 no.6
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    • pp.525-532
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    • 2012
  • The recently constructed buildings are ensuring seismic safety with enhanced design criteria. But, the buildings unapplied enhanced design criteria are very weak. In this study, steel grid shear wall is proposed as a solution of seismic retrofit to ensure safety of the existing buildings for the earthquake. And the structural performance experiments were carried out under axial force and cyclic lateral loads. The two specimens were made of a reference RC frame and steel grid shear wall in-filled RC frame. The test setup configured with two dynamic actuators, for the axial force with a 500kN capacity actuator and for the cyclic lateral load applied with the 2,000kN actuator. Compared with control specimen, the strength, stiffness, ductility, energy dissipation capacity of the seismic retrofit structures is evaluated.

Analysis of the Adsorbed Plasma Proteins in the Moving Actuator type Total Artificial Heart

  • Gyu Ha Ryu;Jon
    • Journal of Biomedical Engineering Research
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    • v.14 no.4
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    • pp.307-314
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    • 1993
  • Plasma protein adsorption is the first event in the blood-material interaction and influenc- es subsequent platelet adhesion towards thlㅈombus formation. Thiㅈomboembolic events are strongly influenced by surface characteristics of materials and fluid dynamics inside the blood pump. In vitro flow visualizaion and an amimal experiment with the moving actuator type TAH were Performed in order to investigate fluid dynamic effects on the protein adsorption. The diffel'encl level, j of shear rate inside the ventricle Lvere determined by consid- ering the direction of the major opening of four healt valves in the implanted TAH and the visualized flow patterns as well. Each ventricle of the explanted TAH was sectionalized into 12 segments according to the shear rate level. The adsorbed protein on each segment was quantified using the ELISA method after soaking in 2% (wye)SDS/PBS for two days. Adsorbed protein layer thicknesses Itvere measured by the Immunogotd method under TEM. The SEM observation show that right ventricle (RV) , immobilized with albumin, displayed different degrees of platelet adhesion on each segment, whereas the left ventricle (LV), grafted by PEO-sulronate, indicated nearly , iame platelet adhesion behavior, regardless of shear rates. The surface concentrations of adsorbed proteins in the low shear rate region are hlghel'than those in the high region, which was confirmed statistically. A modified adsorption model of plasma protein onto polyurethane surface was suggested by considering the effect of the fluid dynamic characteristics.

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Dynamic stability and nonlinear vibration of rotating sandwich cylindrical shell with considering FG core integrated with sensor and actuator

  • Rostami, Rasoul;Mohamadimehr, Mehdi;Rahaghi, Mohsen Irani
    • Steel and Composite Structures
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    • v.32 no.2
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    • pp.225-237
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    • 2019
  • In this research, the dynamic stability and nonlinear vibration behavior of a smart rotating sandwich cylindrical shell is studied. The core of the structure is a functionally graded material (FGM) which is integrated by functionally graded piezoelectric material (FGPM) layers subjected to electric field. The piezoelectric layers at the inner and outer surfaces used as actuator and sensor, respectively. By applying the energy method and Hamilton's principle, the governing equations of sandwich cylindrical shell derived based on first-order shear deformation theory (FSDT). The Galerkin method is used to discriminate the motion equations and the equations are converted to the form of the ordinary differential equations in terms of time. The perturbation method is employed to find the relation between nonlinear frequency and the amplitude of vibration. The main objective of this research is to determine the nonlinear frequencies and nonlinear vibration control by using sensor and actuator layers. The effects of geometrical parameters, power law index of core, sensor and actuator layers, angular velocity and scale transformation parameter on nonlinear frequency-amplitude response diagram and dynamic stability of sandwich cylindrical shell are investigated. The results of this research can be used to design and vibration control of rotating systems in various industries such as aircraft, biomechanics and automobile manufacturing.

Development of Biaxial Tension & Shear Tester using Stepper Motor with Harmonic Driver (감속 스텝모터를 이용한 2축 인장·전단 시험기의 개발)

  • Choi, Byung-Sun;Bae, Won-Ho;Chai, Young-Suck
    • Journal of the Korean Society of Industry Convergence
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    • v.4 no.4
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    • pp.379-386
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    • 2001
  • The lower toughness or brittle materials for mechanical test lead to the additional requirement that applied displacements be controlled with high resolution. Biaxial tension and shear tester using stepper motor with harmonic driver is shown. The device had to be high resolution so that the crack initiation process of slow extension and steady growth could be examined, Grip plates were connected to a linear bearing and actuator. The actuators consisted of stepper motors with harmonic driver connected to pre-loaded ball screw and nut assemblies. The encoders and motor controllers were connected to a personal computer so that arbitrary displacements histories could he prescribed in normal and tangential directions. The linear bearings were used to react loads perpendicular to their axes while allowing low friction, parallel movement of the attached grips. Load cells measured the reactions normal and tangential. the loads measured the reactions were recorded by the computer.

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Active control of flow over a sphere using electro-magnetic actuators (전자석 액츄에이터를 이용한 구 주위의 유동제어)

  • Park, Jin-Il;Choi, Hae-Cheon;Jeon, Woo-Pyung
    • Proceedings of the KSME Conference
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    • 2000.04b
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    • pp.497-501
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    • 2000
  • Flow over a sphere is controlled experimentally at $Re=10^5$ using electro-magnetic actuators. The electro-magnetic actuator developed in this study is composed of the permanent magnet electro-magnet membrane and slot. Eight actuators are placed inside the sphere at equally spaced intervals on a latitudinal plane and the position of the control slot is 76 from the stagnation point. Each actuator generates a periodic blowing and suction through the slot at variable frequencies of $10{\sim}140Hz$ and variable amplitudes by controlling electric signals applied to the electro-magnet. Drag on the sphere measured using a load cell is significantly reduced with control at the forcing frequencies larger than the natural shedding frequency $({\approx}14Hz\;at\;Re=10^5)$, whereas drag is slightly increased at the forcing frequency of 10Hz. It is shown from pressure measurement that the static pressure in the rear surface of the sphere is significantly increased with control, indicating that the separation is delayed due to control. Flow visualizations also show that the detaching shear layer is more attracted to the sphere center with control, the separation bubble size is significantly reduced, and motion inside the bubble is very weak, as compared to the case of uncontrolled flow.

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Influence of imperfection on the smart control frequency characteristics of a cylindrical sensor-actuator GPLRC cylindrical shell using a proportional-derivative smart controller

  • Zare, Reza;Najaafi, Neda;Habibi, Mostafa;Ebrahimi, Farzad;Safarpour, Hamed
    • Smart Structures and Systems
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    • v.26 no.4
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    • pp.469-480
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    • 2020
  • This is the first research on the smart control and vibration analysis of a Graphene nanoplatelets (GPLs) Reinforced Composite (GPLRC) porous cylindrical shell covered with piezoelectric layers as sensor and actuator (PLSA) in the framework of numerical based Generalized Differential Quadrature Method (GDQM). The stresses and strains are obtained using the First-order Shear Deformable Theory (FSDT). Rule of the mixture is employed to obtain varying mass density and Poisson's ratio, while the module of elasticity is computed by modified Halpin-Tsai model. The external voltage is applied to sensor layer and a Proportional-Derivative (PD) controller is used for sensor output control. Governing equations and boundary conditions of the GPLRC cylindrical shell are obtained by implementing Hamilton's principle. The results show that PD controller, length to radius ratio (L/R), applied voltage, porosity and weight fraction of GPL have significant influence on the frequency characteristics of a porous GPLRC cylindrical shell. Another important consequence is that at the lower value of the applied voltage, the influence of the smart controller on the frequency of the micro composite shell is much more significant in comparison with the higher ones.

A Study on the Control Characteristics of ER Valve-FHA System and Durability Test

  • Jang Sung-Cheol;Chang Tae-Hyun
    • Journal of Mechanical Science and Technology
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    • v.19 no.8
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    • pp.1621-1631
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    • 2005
  • In this paper, making the best use of the features of the electro-rheological (ER) valve, a two-port pressure control valve using ER fluids is proposed and manufactured. The ER-Valve characteristics are evaluated by changing the intensity of the electric field and the number of electrode. As only with electrical signal change to the ER-Valve in which ER fluid flowing, ER fluid flow is controlled, so development of simple ER-Valves have been tried. The ER-Valves and pressure drop check method are considered to be applied to the fluid power industry. Using the manufactured pressure control valve, a one-link manipulator with FHA (Flexible Hydraulic Actuator) is driven. As a result, it is experimentally confirmed that the pressure control valve using ER fluids is applicable to use in driving actuator. If it applies characteristics of the ER fluids, it will be able to apply in the control system for the ER Valve which occurs from industrial controller. After having durability test, shear stress increased regularly because of starch particles crushed by pump and particle size that was almost the same. Moreover, Ra of copper electrode increased about 1.56 times rather than before those of performing durability test, and Rz increased about 2.2 times.