• Title/Summary/Keyword: Rotor performance

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Development of Performance Analysis 80 kW High-efficiency Permanent Magnet Generator for Radar System Power Supply (레이더 체계 전원공급용 80 kW급 고효율 영구자석형 발전기 개발 및 성능분석)

  • Ryu, Ji-Ho;Cho, Chong-Hyeon;Chong, Min-Kil;Park, Sung-Jin;Kang, Kwang-Hee
    • Journal of the Korea Institute of Military Science and Technology
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    • v.22 no.1
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    • pp.60-71
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    • 2019
  • Electrical power supply is needed to operate the radar system in the field. In addition, it should not cause performance deterioration under the environmental factors due to characteristics of military equipment, and should not cause malfunction due to electromagnetic waves generated in radar, and then should not cause malfunction in radar equipment. Therefore, By applying a permanent magnet to the rotor of the generator, light weighting and high efficiency of generator were achieved. As a result, electrical performance test of the generator, the rated output power was 80.8 kW, the maximum output power was 88.1 kW, and the output power efficiency was 98.1 % under the full load condition. When the load capacity of the generator was changed from no load to full load, the maximum voltage variation was 3.6 % and the frequency variation was 0.3 %. As a result of the transient response test for measuring the output power of the generator according to the load characteristics change, the maximum voltage variation of 7.9 %, frequency variation of 0.5 % were confirmed, and the transient response time was 2.1 seconds. Environmental tests were conducted in accordance with MIL-STD-810G and MIL-STD-461F to evaluate the operability of the generator groups. Normal operation of radar system generator group was confirmed under high temperature and low temperature environment conditions. Electromagnetic tests were conducted to check if electromagnetic wave generated from both radar system and generator group in operation caused any performance deterioration to each other. As a result, it was confirmed that the performance deterioration due to electromagnetic wave inflow, radiation, and conduction did not occur. It is expected that it should be possible to provide high efficiency power supply and stable power supply by applying to various military system as well as radar system.

A LQR Controller Design for Performance Optimization of Medium Scale Commercial Aircraft Turbofan Engine (II) (중형항공기용 터보팬 엔진의 성능최적화를 위한 LQR 제어기 설계 (II))

  • 공창덕;기자영
    • Journal of the Korean Society of Propulsion Engineers
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    • v.2 no.3
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    • pp.99-106
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    • 1998
  • The performance of the turbofan engine, a medium scale civil aircraft which has been developing in Rep. of Korea, was analyzed and the control scheme for optimization the performance was studied. The dynamic and real-time linear simulation was performed in the previous study The result was that the fuel scedule of the step increase overshoot the limit temperature(3105 $^{\cire}R$) of the high pressure turbine and got small surge margine of the high pressure compressor. Therefore a control scheme such as the LQR(Linear Quadratic Regulator) was applied to optimizing the performance in this studies. The linear model was expected for designing controller and the real time linear model was developed to be closed to nonlinear simulation results. The system matrices were derived from sampling operating points in the scheduled range and then the least square method was applied to the interpolation between these sampling points, where each element of matrices was a function of the rotor speed. The control variables were the fuel flow and the low pressure compressor bleed air. The controlled linear model eliminated the inlet temperature overshoot of the high pressure turbine and obtained maximum surge margins within 0.55. The SFC was stabilized in the range of 0.355 to 0.43.

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Fundamental Studies on the Development of Axial-Flow Combine(I) -Evaluation of the Design Parameters of Grain-Straw Separator- (축류(軸流) 콤바인의 개발(開發)에 관(關)한 기초(基礎) 연구(硏究)(I) -조선별장치(粗選別裝置)의 설계변수(設計變數)의 평가(評價)-)

  • Lee, S.K.;Kim, S.T.;Choi, K.H.
    • Journal of Biosystems Engineering
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    • v.11 no.2
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    • pp.31-40
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    • 1986
  • Cylindrical and conical types of grain-straw separation equipment which has a stationary crimped sieve drum with rotating inner rotor were constructed. The developed equipments were tested to investigate the characteristics of separating performance under various mechanical conditions and crop conditions. As increase of the inclination of equipment and decrease of pitch of cover vane, the grain recovery was increased while straw rejection was decreased. The grain recovery and overall efficiency were decreased as the rotor speed and feeding velocity were increased for both varieties of rice, moisture contents, and test equipments. Conical prototype equipment performed higher straw rejection, lower grain recovery, and lower power requirement. However, separation performance of conical type equipment was more widely varied with various test conditions compared to cylindrical one. The performance of both equipments showed relatively insensitive to crop feedrate and crop properties, such as variety, moisture content, and grain-to-straw ratio.

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Control and Analysis of an Integrated Bidirectional DC/AC and DC/DC Converters for Plug-In Hybrid Electric Vehicle Applications

  • Hegazy, Omar;Van Mierlo, Joeri;Lataire, Philippe
    • Journal of Power Electronics
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    • v.11 no.4
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    • pp.408-417
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    • 2011
  • The plug-in hybrid electric vehicles (PHEVs) are specialized hybrid electric vehicles that have the potential to obtain enough energy for average daily commuting from batteries. The PHEV battery would be recharged from the power grid at home or at work and would thus allow for a reduction in the overall fuel consumption. This paper proposes an integrated power electronics interface for PHEVs, which consists of a novel Eight-Switch Inverter (ESI) and an interleaved DC/DC converter, in order to reduce the cost, the mass and the size of the power electronics unit (PEU) with high performance at any operating mode. In the proposed configuration, a novel Eight-Switch Inverter (ESI) is able to function as a bidirectional single-phase AC/DC battery charger/ vehicle to grid (V2G) and to transfer electrical energy between the DC-link (connected to the battery) and the electric traction system as DC/AC inverter. In addition, a bidirectional-interleaved DC/DC converter with dual-loop controller is proposed for interfacing the ESI to a low-voltage battery pack in order to minimize the ripple of the battery current and to improve the efficiency of the DC system with lower inductor size. To validate the performance of the proposed configuration, the indirect field-oriented control (IFOC) based on particle swarm optimization (PSO) is proposed to optimize the efficiency of the AC drive system in PHEVs. The maximum efficiency of the motor is obtained by the evaluation of optimal rotor flux at any operating point, where the PSO is applied to evaluate the optimal flux. Moreover, an improved AC/DC controller based Proportional-Resonant Control (PRC) is proposed in order to reduce the THD of the input current in charger/V2G modes. The proposed configuration is analyzed and its performance is validated using simulated results obtained in MATLAB/ SIMULINK. Furthermore, it is experimentally validated with results obtained from the prototypes that have been developed and built in the laboratory based on TMS320F2808 DSP.

Development and Verification of Active Vibration Control System for Helicopter (소형민수헬기 능동진동제어시스템 개발)

  • Kim, Nam-Jo;Kwak, Dong-Il;Kang, Woo-Ram;Hwang, Yoo-Sang;Kim, Do-Hyung;Kim, Chan-Dong;Lee, Ki-Jin;So, Hee-Soup
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.50 no.3
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    • pp.181-192
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    • 2022
  • Active vibration control system(AVCS) for helicopter enables to control the vibration generated from the main rotor and has the superb vibration reduction performance with low weight compared passive vibration reduction device. In this paper, FxLMS algorithm-based vibration control software of the light civil helicopter tansmits the control command calculated using the signals of the tachometer and accelerometers to the circular force generator(CFG) is developed and verified. According to the RTCA DO-178C/DO-331, the vibration control software is developed through the model based design technique, and real-time operation performance is evaluated in PILS(processor in-the loop simulation) and HILS(hardware in-the loop simulation) environments. In particular, the reliability of the software is improved through the LDRA-based verification coverage in the PIL environments. In order to AVCS to light civil helicopter(LCH), the dynamic response characteristic model is obtained through the ground/flight tests. AVCS configuration which exhibits the optimal performance is determined using system optimization analysis and flight test and obtain STC certification.

Implementation of Super High-speed Permanent Magnet Synchronous Machine Drive (영구 자석 동기 전동기의 초고속 운전에 관한 연구)

  • Kim, Myoung-Ho;Yim, Jung-Sik;Sul, Seung-Ki;Lim, Sung-Il
    • The Transactions of the Korean Institute of Power Electronics
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    • v.13 no.5
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    • pp.329-335
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    • 2008
  • Recently, super high-speed motor drives have been available due to the development of power electronics technology And they are used in various fields of industry because of their advantages. This paper describes the control algorithm for a permanent magnet synchronous motor(PMSM) drive at the speed of 118,000r/min using DSP and IGBT inverter. Hall sensors are implemented to measure the rotor position and speed, and a speed observer is used to reduce the performance deterioration caused by the low resolution of hall sensors. To enhance the output power capacity in the high-speed operating region, a flux weakening controller which also can work as an anti-wind up controller is used. Computer simulations and experiments are peformed to validate the proposed method.

Compact Anode Design with the Heat Capacity Performance in Rotating Anode X-ray Tube for Digital Radiography

  • Lee, Seok Moon
    • Applied Science and Convergence Technology
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    • v.24 no.5
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    • pp.136-141
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    • 2015
  • We studied the compact anode design to develop 100 kW rotating anode X-ray tube with large focal spot 1.2 mm, small focal spot 0.6 mm and tube voltage 150 kV for large hospital digital radiography using computer thermal simulation. The larger thermal radiation effect in a high vacuum can reduce the temperature of anode so the method to increase the surface area of anode is investigated. The anode has the multi-tier shape at the back side of TZM body of anode and also bigger diameter of anode. The number of multi-tiers was varied from 6 to 15 and the diameter of anode was also varied from ${\Phi}74$ to ${\Phi}82$. From ANSYS transient thermal simulation result, we could obtain $1056.4^{\circ}C$ anode maximum temperature when applying 100 kW input power at 0.1 second on target focal track which is less than $1091^{\circ}C$ of the conventional 75 kW X-ray tube with reduced anode weight by 15.5% than the conventional anode. The compact anode of reduced anode weight is able to improve the unwanted noise when the rotor is rotating at high-speed and also reduce the rotational torque which the cost effective stator-coil is possible. It is believed that the anode with 15 ea multi-tiers using ${\Phi}82$ can satisfy with the specification of the anode heat capacity. From the results of this paper, it has been confirmed that the proposed compact anode can be used as the anode of 100 kW rotating anode X-ray tube for digital radiography.

Development of a Model-Based Motor Fault Detection System Using Vibration Signal (진동 신호 이용 모델 기반 모터 결함 검출 시스템 개발)

  • ;A.G. Parlos
    • Journal of Institute of Control, Robotics and Systems
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    • v.9 no.11
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    • pp.874-882
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    • 2003
  • The condition assessment of engineering systems has increased in importance because the manpower needed to operate and supervise various plants has been reduced. Especially, induction motors are at the core of most engineering processes, and there is an indispensable need to monitor their health and performance. So detection and diagnosis of motor faults is a base to improve efficiency of the industrial plant. In this paper, a model-based fault detection system is developed for induction motors, using steady state vibration signals. Early various fault detection systems using vibration signals are a trivial method and those methods are prone to have missed fault or false alarms. The suggested motor fault detection system was developed using a model-based reference value. The stationary signal had been extracted from the non-stationary signal using a data segmentation method. The signal processing method applied in this research is FFT. A reference model with spectra signal is developed and then the residuals of the vibration signal are generated. The ratio of RMS values of vibration residuals is proposed as a fault indicator for detecting faults. The developed fault detection system is tested on 800 hp motor and it is shown to be effective for detecting faults in the air-gap eccentricities and broken rotor bars. The suggested system is shown to be effective for reducing missed faults and false alarms. Moreover, the suggested system has advantages in the automation of fault detection algorithms in a random signal system, and the reference model is not complicated.

Development of aerodynamic noise prediction technique for high efficiency and low noise design of unmanned aerial vehicle propeller (멀티로터형 무인항공기 프로펠러의 고효율 및 저소음 설계를 위한 공력 소음 예측 기법 개발)

  • Gwak, Doo Young;Lee, Soogab
    • The Journal of the Acoustical Society of Korea
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    • v.36 no.2
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    • pp.89-99
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    • 2017
  • Multi-rotor type UAV (Unmanned Aerial Vehicle)s are expanding their applications not only for military purposes but also for private industries such as aerial photography and unmanned delivery vehicles. For wider use of unmanned aerial vehicles, studies should be carried out to improve aerodynamic efficiency and reduce noise of propellers, which can be achieved based on techniques of predicting aerodynamic performance and noise in a given environment. In this study, aerodynamic and noise prediction techniques were developed for a small unmanned aerial vehicle propeller, and it was verified by comparing it with actual measurement results. Thrust and torque due to the change of r/min and the frequency spectral prediction at a given position secured the reliability of the prediction method, which provides a basis for the shape design of the propeller.

A Study on the Redesign of the Two-Stage Axial Compressor for Helicopter Engines (헬리콥터용 2단 축류압축기의 재설계에 관한 연구)

  • Kim, Jin-Han;Choi, Chang-Ho;Kim, Chul-Taek;Yang, Sooseok;Lee, Daesung
    • The KSFM Journal of Fluid Machinery
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    • v.4 no.1 s.10
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    • pp.7-13
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    • 2001
  • In developing a multistage compressor, the stage matching is one of the critical design issues. The mismatching can be often observed even if each stage has been proven good and then used as part of a compression system. A good matching among the stages can be achieved by changing various design parameters (i.e., passage cross sectional areas, blades angles, stagger angles, curvature, solidity, etc.). Therefore, designers need to find out what parameters must be changed and how much. In this study, a method to search the design parameters for optimum stage matching has been used based on an 1-D mathematical model of a compressor, which uses the data obtained from the preliminary test to identify the design parameters. This methodology is applied with a two-stage axial compressor, which was originally designed for a helicopter gas turbine engine. After identifying design parameters using preliminary test data, an optimization process has been employed to achieve the best matching between the stages (i.e., maximum efficiency of the compressor at its operation modes within a given range of the rotor speed under given restrictions for required stall margins and mass flow). 3-D flow calculations have been performed to confirm the usefulness of the corrections based on the 1-D mathematical model. Calculational results agree well with the experimental data in view of the performance characteristics. Some promising results were produced through the methodology proposed in this paper in conjunction with flow calculations.

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