• Title/Summary/Keyword: Rocket noise

Search Result 50, Processing Time 0.025 seconds

Ground Vibration Test for Korea Sounding Rocket - III (KSR-III의 전기체 모달 시험)

  • 우성현;김영기;이동우;문남진;김홍배
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
    • /
    • 2002.05a
    • /
    • pp.441-447
    • /
    • 2002
  • KSR-III(Korea Sounding Rocket - III), which is being developed by Space Technology R&D Division of KARI(Korea Aerospace Research Institute) will be launched in late 2002. It is a three-stage, liquid propellant rocket which can reach 250 km altitude and will carry out observation of ozone layer and scientific experiments, such as microgravity experiment, and atmospheric measurement. KSR-III is believed to be an intermediate to the launch vehicle capable of carrying a satellite to its orbit. Space Test Department of KARI performed GVT(Ground Vibration Test) fer KSR-III EM at Rocket Test Building of KARI. GVT is very important for predicting the behavior of rocket in its operation, developing flight control program and performing aerodynamic analysis. This paper gives an introduction of rocket GVT configuration and information on test procedures, techniques and results of It. In this test. to simulate free-free condition, test object hung in the air laterally by 4 bungee cords specially devised. For the excitation of test object, pure random signal by two electromagnetic shakers was used and total 22 frequency response functions were achieved. Polyreference parameter estimation was performed to identify the modal parameters with MIMO(Multi-Input-Multi-Output) method. As the result of the test, low frequency mode shapes and modal parameters below 60Hz were identified

  • PDF

Experience Cases of Combustion Instability in Development of Gas Generator for Liquid Rocket Engine (액체로켓엔진 가스발생기 개발에서의 연소불안정 경험 사례)

  • Kim, Munki;Lim, Byoungjik;Kim, Seong-Ku;Kim, Jong-Gyu;Choi, Hwan-Seok
    • Proceedings of the Korean Society of Propulsion Engineers Conference
    • /
    • 2017.05a
    • /
    • pp.61-64
    • /
    • 2017
  • The gas-generator open cycle is adapted for liquid rocket engine of Korea Space Launch Vehicle-II. The combustion instability can interfere with combustion performance and cause a noise and vibration or carry the potential for serious damage. This study introduces the experience cases of combustion instability in development of the gas generator for liquid rocket engine.

  • PDF

Analysis and Test of Dynamic Responses of Rocket Payload Section Induced by Acoustic Excitation (음향 가진에 의한 로켓 탑재부의 동적 응답 해석 및 시험)

  • Park, S.H.;Jeong, H.K.;Seo, S.H.;Jang, Y.S.;Yi, Y.M.;Cho, K.R.
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
    • /
    • 2005.05a
    • /
    • pp.717-720
    • /
    • 2005
  • Acoustic loads generated by a rocket propulsion system cause severe random vibrations on payloads. In developing a new launch vehicle, a random vibration level must be specified before the detailed design of payloads or electronic equipments. This paper deals with prediction procedures of a random vibration level on payload section of KSLV-I. The prediction is based on statistical energy analysis. In order to verify the prediction methodology, test and analysis on a sub-scale payload section are performed. The predicted results subject to very high level of acoustic loads show a good agreement with the test results performed in the high intensity acoustic chamber. The predicted random vibration level on payload section of KSLV-I is also presented in this paper.

  • PDF

Acoustic Analysis of Exhaust Supersonic Jet From a Rocket Motor Using 2-D Axis-symmetric Computational Analysis (2차원 축대칭 전산해석을 이용한 초음속 로켓 제트 음향 해석)

  • Yang, Young-Rok;Jeon, Hyuck-Soo
    • Journal of the Korean Society for Aeronautical & Space Sciences
    • /
    • v.48 no.9
    • /
    • pp.725-730
    • /
    • 2020
  • This study was conducted to reduce the computation time required for the computational acoustic analysis of the supersonic rocket jet plume. In order to reduce the computation time, computational acoustic analysis was performed assuming that the supersonic jet plume is a two-dimensional axis-symmetric problem. The results of computational acoustic analysis showed similar results to the acoustic load measurement results. Through this study, it was confirmed that the acoustic load prediction of the supersonic rocket jet plume can be predicted using a two-dimensional axis-symmetric computational analysis.

A Study on the Combustion Instability of the Hybrid Rocket Motor with a Diaphragm (다이아프램이 설치된 하이브리드 로켓 모터의 연소불안정 연구)

  • Lee, Jungpyo;Kim, Youngnam;Kim, Jinkon;Moon, Heejang
    • Journal of the Korean Society of Propulsion Engineers
    • /
    • v.17 no.6
    • /
    • pp.1-10
    • /
    • 2013
  • In this paper, the main cause on excitation of the combustion instability which may occur in the hybrid rocket motor with a diaphragm was studied. Hybrid rocket motor propulsion tests considering various experimental conditions such as with a diaphragm or not, a diameter of diaphragm, oxidizer mass flow rate, fuel length, etc were performed, and the combustion visualization for the inside of a hybrid rocket motor with a diaphragm was performed. With these experimental results, it was confirmed that the main cause of a large excitation was the hole-tone, and it was shown that the hole-tone model can be predicted experimental primary pressure oscillation frequency quite well.

Measurement of Damping Ratio of Fuel Sloshing in a Baffled Liquid Propellant Tank of KSR-III Rocket (KSR-III 로켓의 액체 연료 탱크 내에서 발생하는 슬로싱 현상의 배플에 의한 감쇄율 측정)

  • Park, Soon-Hong;Yoo, Joon-Tae;Yi, Yeong-Moo
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
    • /
    • 2002.11b
    • /
    • pp.172-175
    • /
    • 2002
  • Sloshing of fuel in a liquid propellant tank is an important part of the dynamic and the stability analysis of the rocket. Baffles are installed in a propellant tank to reduce the instability due to sloshing. Multi degree of spring-mass-damper model was used to model sloshing of fuel in an axisymmetric tank. The natural frequencies and damping ratios are estimated. In order to verify the estimated natural frequencies and damping ratios, tests are performed for the real propellant tank of KSR-III with single ring baffle. Results of fuel sloshing analysis are compared with those of tests.

  • PDF

Measurment of Damping Ratio of Fuel Sloshing in Baffled Liquid Propellant Tank of KSR-III Rocket (KSR-III 로켓의 액체 연료 탱크 내에서 발생하는 슬로슁 현상의 배플에 의한 감쇄율 측정)

  • Park, Soon-Hong;Yoo, Joon-Tae
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
    • /
    • 2002.11a
    • /
    • pp.323.2-323
    • /
    • 2002
  • Sloshing of fuel in a liquid propellant tank is an important part of the dynamic and the stability analysis of the rocket. Baffles are installed in a propellant tank to reduce the instability due to sloshing. Multi degree of spring-mass-damper model was used to model sloshing of fuel in an axisymmetric tank. The natural frequencies and damping ratios are estimated. In order to verify the estimated natural frequencies and damping ratios, tests are performed for the real propellant tank of KSR-III with single ring baffle. Results of fuel sloshing analysis are compared with those of tests.

  • PDF

An effect of design parameters of water injection silencer on the characteristics of noise generated by Liquid Rocket Engine (물분사형 소음기의 설계 변수가 액체로켓엔 소음특성에 미치는 영향)

  • Park, Hee-Ho;Cho, Byoung-Sun;Kim, Yoo;Ji, Pyung-Sam;Kim, Seon-Jin
    • Journal of the Korean Society of Propulsion Engineers
    • /
    • v.2 no.2
    • /
    • pp.83-87
    • /
    • 1998
  • To reduce the supersonic jet noise from the liquid rocket engine, water injetion silencers were designed and tested. Test variables were the mass flow rate of water jet, the length of primary pipe and the diameter of expansion pipe. Followings are the results of this study. 1. From the same mass flow rate of water, longer primary pipe was more effective to reduce the noise. 2. Noise level was significantly reduced with increasingly water flow rate. 3. The optimum water flow rate was 10~12 times of the propellant flow rate. 4. By installing expansion pipe, noise level was reduced approximately 30㏈ compared to without expansion pipe

  • PDF