• 제목/요약/키워드: Pump Case

검색결과 519건 처리시간 0.029초

대형 tank 구조물 개선에 따른 진동변화 고찰 (Investigation for Change of Pump's Vibration Modes on Oil Tank)

  • 양경현;조철환;조성태;송오섭
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2007년도 춘계학술대회논문집
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    • pp.36-40
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    • 2007
  • It uses a tank to store, purify and feed lube oil in power plants, which is made by steel plate. Several pumps to feed lube oil are installed on the top plate of the oil tank. In this case if pumps on the top plate are removed or added, the dynamic characteristics of the structure will be changed. In this paper, we present that we analyze in detail the similar case with a finite element model for tank & pump structure coupled with oil and that we set plan to change mode shapes on the top plate of the tank.

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회전날개 길이를 이용한 제로터 펌프/모터의 배제용적에 관한 연구 (An Analysis on Volumetric Displacement of Gerotor Pump/Motor Using Vane Length)

  • 김성동;김대명;함영복;한철호
    • 유공압시스템학회논문집
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    • 제8권2호
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    • pp.8-16
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    • 2011
  • It is hard and complicated to analytically derive the volumetric-displacement formula of a gerotor pump/motor. Analytical formulas for calculating the volumetric-displacement are derived in this work, which is relatively easy and based upon vane lengths. The vane lengths mean the distances from axis of inner rotor or outer rotor to contact points between inner and outer rotors. Two kinds of formula were studied for two different kinematic motions of rotors. The first one is the case that outer rotor is fixed in space and inner rotor is in mixed motion of planetary revolution and rotation with respect to the spinning axis. And the second is the case that both inner and outer rotors simultaneously rotate. The proposed formula is verified through comparison with volumetric-displacement obtained from numerical CAD calculation.

복합 화력 Condensate Pump 의 고진동 사례 분석 및 대책 (A Case Study on High Vibration in a Condensate Pump for Combined Cycle Power Plants)

  • 최성필;류석주;하현천
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2001년도 춘계학술대회논문집
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    • pp.510-513
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    • 2001
  • Several kinds of vibration problems have been frequently encountered in industrial vertical pumps in spite of their widespread use for long time. In fact, vibration problems of the vertical pumps are so complicated and difficult with compared to those of the horizontally mounted pumps that more careful attention should be taken for solving the vibration problems. This paper introduces a case study experienced from troubleshooting for excessive vibration occurred in a vertical-type condensate pump for combined cycle power plants. Subsynchronous whirl vibration was caused by the instability of the guide bearing whose lubricant is water. A newly modified guide bearing has solved the vibration problem, which should be the best countermeasure.

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스크류펌프의 유량특성과 적용 (Flowrate characteristics and application of screw pump)

  • 임종순
    • 유체기계공업학회:학술대회논문집
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    • 유체기계공업학회 2004년도 유체기계 연구개발 발표회 논문집
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    • pp.614-625
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    • 2004
  • The main purpose of this study is to get flowrate coefficient 'q' and to study characteristics of flowrate of screw pump. This study is based on Muskin's formula and depends on the computer simulation. The results of study are as follows. 1. Flowrate coefficient will reduce according to increase of inclination. The larger the pitch ratio is and the smaller the diameter ratio is, the more coefficient reduces. 2. As a rule, the coefficient increases according to reduction of the diameter ratio, but the coefficient tends to reduce when the ratio is less than 0.45. So, in actual application, it is recommended that the ratio should be above 0.45. 3. If the pitch ratio increases, the coefficient increases in case of small inclination and decreases in case of large inclination. 4. The coefficient increases according to number of windings. Especially, singles winding is not used in actual application because it has too small coefficient. 5. The coefficient decreases when the influent water level falls. Flowrate is almost zero when the water level is below $40\%$ of Filling Points.

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지열 시스템의 도입이 지중온도환경에 미치는 영향에 대한 해석적 검토 (Numerical Analysis of the Effect of Ground Source Heat Pump Systems on the Underground Temperature)

  • 남유진
    • 설비공학논문집
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    • 제25권8호
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    • pp.427-431
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    • 2013
  • Ground heat pump systems utilize the annually stable underground temperature to supply heat for space heating and cooling. The underground temperature affects not only the underground ecosystem, but also the performance of these systems. However, in spite of the widespread use of these systems, there have been few researches on the effect of the systems on underground temperature. In this research, case studies with numerical simulation have been conducted, in order to estimate the effect of ground heat pump systems on underground temperature. The simulation was coupled with the ground water-ground heat transfer model and the ground surface heat transfer model. In the result, it was found that the underground change depends on the heat transfer from the ground surface, the heat exchange rate, and the heat conductivity of soil.

열펌프 시스템의 규모 결정을 위한 온돌난방부하 특성 (Characteristics of Ondol Heating Load for the Determination of Heat Pump Power)

  • 노정근;백은기;송현갑
    • Journal of Biosystems Engineering
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    • 제28권3호
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    • pp.217-224
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    • 2003
  • To find out heating load and to determine the power of heat pump compressor for the Ondol room heating the COP of heat pump, the variation of Ondol room air temperature, the variation of ambient temperature and power consumption of heat pump are analyzed. The results from this study were summarized as follows: 1. The COP of the heat pump in close loop decreased as the ambient air temperature. The COP was 2.26 when the temperature difference of condenser was $20\pm3^{\circ}C$. 2. The Ondol surface temperature was $25\pm3^{\circ}C$ when the hot water of $40^{\circ}C$ was supplied from hot water storage tank to the Ondol and the temperature difference between the Ondol surface and the room air temperature was $7~8^{\circ}C$. 3. The ratio of thermal conduction heating load to total heating load in Ondol heating space was found to be 83% and ratio of ventilation heating load was 17%. Therefore, the thermal conduction heating load was confirmod to be a major heating load in Ondol heating space. 4. In case of the ambient temperature of $3.2^{\circ}C$, the efficiency of heat exchange of Ondol heating system was 85%. 5. The heating load per Ondol heating surface area and volume of Ondol room space were theoretically analyzed. In case of the room temperature of $20^{\circ}C$ and the ambient temperature of $-3.2~3.8^{\circ}C$, the heating load per Ondol surface area was 115.8~167.6kJ/h ㆍ㎥ and per Ondol mom space volume was 50.2~72.7kJ/h ㆍ㎥. 6. The compressor power of heat pump fur the Ondol room heating could be determined with the heating load analyzed in this study In case of the Ondol room air temperature of 17~2$0^{\circ}C$ and the ambient temperature of -5~3.8$^{\circ}C$, the compressor power of heat pump per Ondol surface area was analyzed to be $2.3\times10^{-2}psm^2$, and per volume of Ondol room space $1.0\times10^{-2}1.4\times10^{-2}ps/m^2$ps.

터보 분자 펌프(Turbomolecular pump)내의 자유 분자 유동에 관한 수치 해석적 연구 (A Numerical Study of a Free Molecular Flow in the Turbomolecular Pump)

  • 황영규;허중식
    • 설비공학논문집
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    • 제8권2호
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    • pp.219-229
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    • 1996
  • In the free molecular flow range, the pumping performance of a turbomolecular pump has been predicted by calculation of the transmission probability employing the integral method and the test particle Monte-Carlo method. The velocities of molecules incident upon a moving blade are given by the random numbers, which are sampled from the Maxwell molecular velocity distribution function. The present results agree quantitatively with the previous known numerical results. For a multi-stage pump, the velocity profile of molecules between two blade rows is not Maxwell distribution. In this case, the Monte-Carlo method is employed to calculate the overall transmission probability for the entire set of blade rows. When the results of the approximate method combining the single stage solutions are compared with those of the Monte-Carlo method for the pump having six rows at C=0.6, the approximate method overestimates as much as 36% in the maximum compression ratio and 19% in the maximum pumping speed than does the Mote-Carlo method.

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Study on the Performance Characteristics of Centrifugal Pump with Drag-reducing Surfactant Additives

  • Wang, Lu;Li, Feng-Chen;Dong, Yong;Cai, Wei-Hua;Su, Wen-Tao
    • International Journal of Fluid Machinery and Systems
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    • 제4권2호
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    • pp.223-228
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    • 2011
  • The performance characteristics of centrifugal pump were measured experimentally when running with tap water and drag-reducing surfactant (Octadecyl dimethyl amine oxide (OB-8)) solutions. Tests have been performed on five cases of surfactant solutions with different concentrations (0ppm (tap water), 200ppm, 500ppm, 900ppm and 1500ppm) and four different rotating speeds of pump (1500rpm, 2000rpm, 2500rpm and 2900rpm). Compared with tap water case, the experimental results show that the total pump heads for surfactant solution cases are higher. And the pump efficiency with surfactant solutions also increases, but the shaft power for surfactant solutions cases decreases compared to t hat for tap water. There exists an optimal temperature for surfactant solutions, which maximizes the pump efficiency.

Study for the Increase of Micro Regenerative Pump Head

  • Horiguchi, Hironori;Wakiya, Keisuke;Tsujimoto, Yoshinobu;Sakagami, Masaaki;Tanaka, Shigeo
    • International Journal of Fluid Machinery and Systems
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    • 제2권3호
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    • pp.189-196
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    • 2009
  • The effect of inlet and outlet blade angles on a micro regenerative pump head was examined in experiments. The pump head was little increased by changing the blade angles compared with the original pump with the inlet and outlet blade angles of 0 degree. The effect of the axial clearance between the impeller and the casing on the pump head was also examined. The head was increased largely by decreasing the axial clearance. The computation of the internal flow was performed to clarify the cause of the increase of the pump head due to the decrease of the clearance. The local flow rate in the casing decreased as the leakage flow rate through the axial clearance decreased due to the decrease of the clearance. It was found that the larger head in the smaller clearance was just caused by the smaller local flow rate in the casing. In the case of the smaller clearance, the smaller local flow rate caused the smaller circumferential velocity near the front and rear sides of the impeller. This caused the increase of the angular momentum in the casing and the head.

펌프제어밸브를 사용한 취수펌프장에서의 수격현상 (Waterhammer for the Intake Pumping Station with the Pump Control Valve)

  • 김경엽;오상현
    • 한국유체기계학회 논문집
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    • 제4권4호
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    • pp.16-21
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    • 2001
  • The field tests on the waterhammer were carried out for PalDang intake pumping station of the metropolitan water supply 5th stage project. The pumping station was equipped with the pump control valve as the main surge suppression device and the surge relief valve as auxiliary. However, the pump control valve had not been early controlled in the planned closing mode, and the slamming occurred to the valve which abruptly closed during the large reverse flow. Because the pressure wave caused by the pump failure was superposed on the slam surge, the upsurge increased so extremely that the shaft of the valve was damaged. It was desirable that the surge relief valve was installed in the pumping station or near the pump exit for the delay of response. After reforming the oil dashpot of the pump control valve, the sliming disappeared and the measured pressure was in fairly good agreement with the results of simulation. In case of three pumps for ${\phi}2,600$ pipeline being simultaneously tripped, the pressure head in the pumping station increased to 95.6 m, and the upsurge caused by the emergency stop of four pumps for ${\phi}2,800$ pipeline was 89.6m. We concluded that the pumping station acquired the safety and reliability for the pressure surge.

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