• 제목/요약/키워드: LPi (liquefied petroleum injection)

검색결과 7건 처리시간 0.019초

Performance and Emissions Characteristics of a Converted Liquefied Petroleum Gas (LPG) Engine with Mixer and Liquid Propane Injection (LPi) System

  • Choi, Gyeung-Ho;Kim, Jin-Ho;Cho, Ung-Lae;Chung, Yon-Jong;Han, Sung-Bin
    • 에너지공학
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    • 제14권3호
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    • pp.187-193
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    • 2005
  • In this study, the performance and emission characteristics of a liquefied petroleum gas (LPG) engine converted from a diesel engine were examined by using mixer system and liquid propane injection (LPi) system. A compression ratio of 21 for the base diesel engine, was modified to 8, 8.5, 9 and 9.5. The engine performance and emissions characteristics are analyzed by investigating engine power, brake mean effective pressure (BMEP), brake specific fuel consumption (BSFC), volumetric efficienry, CO, THC and NOx. Experimental results showed that the LPi system generated higher power and lower emissions than the conventional mixer fuel supply method.

개조된 LPG엔진에서 Mixer와 LPi 연료공급방식의 엔진성능 및 배기특성 (Engine Performance and Emissions Characteristics in an LPG Engine Converted with Mixer and LPi System Fuel Supply Methods)

  • 최경호;김진호;조웅래;한성빈
    • 대한기계학회논문집B
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    • 제28권9호
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    • pp.1075-1080
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    • 2004
  • In this study, performance and emissions characteristics of an liquefied petroleum gas (LPG) engine converted from a diesel engine were examined by using mixer system and liquid propane injection (LPi) system fuel supply methods. A compression ratio for the base diesel engine, 21, was modified into 8, 8.5, 9 and 9.5. The cylinder head and the piston crown were modified to roe the LPG in the engine. Ignition timing was controlled to be at minimum spark advance for best torque (MBT) each case. Engine performance and emissions characteristics are analyzed by investigating engine power, brake mean effective pressure (BMEP), brake specific fuel consumption (BSFC), volumetric efficiency, CO, THC and NOx. Experimental results showed that the LPi system generates higher power and lower emissions than the conventional mixer fuel supply method.

Top-Feed Type 인젝터의 액상분사 LPG연료 분사장치 적용 (Top-Feed Type Port Fuel Injector for Liquefied Petroleum Gas Liquid Phase Injection)

  • 염기태;박정서;배충식;박정남;김성근
    • 한국자동차공학회논문집
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    • 제15권6호
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    • pp.30-37
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    • 2007
  • The injection and spray characteristics of top-feed type injector was investigated under liquid phase injection fueled with liquefied petroleum gas (LPG). Different pressures and temperatures of fuel injection system were tested to identify the injection characteristics after hot soaking. MIE-scattering technique was used for verification of successful liquid phase injection after hot soaking. In case of bottom-feed type injector, the injection was accomplished at every experimental condition. In case of top-feed type injector, when the pressure of LPG was over 1.2 MPa, the injection was not executed. However, under the pressure were 1.2 MPa, the liquid phase injection after hot soaking was accomplished. The engine with top-feed type fuel injection equipment was restarted successfully after hot soaking.

Effect of Hydrogen Enriched LPG Fuelled Engine with Converted from a Diesel Engine

  • Choi, Gyeung-Ho;Lee, Jae-Cheon;Chung, Yon-Jong;Caton, Jerald;Han, Sung-Bin
    • 에너지공학
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    • 제15권3호
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    • pp.139-145
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    • 2006
  • The purpose of this study is to obtain low-emission and high-efficiency in LPG engine with hydrogen enrichment. The objective of this paper is to clarify the effects of hydrogen enrichment in LPG fuelled engine on exhaust emission, thermal efficiency and performance. The compression ratio of 8 was selected to avoid abnormal combustion. To maintain equal heating value of fuel blend, the amount of LPG was decreased as hydrogen was gradually added. The relative air-fuel ratio was increased from 0.8 to 1.3, and the ignition timing was controlled to be at MBT (minimum spark advance for best torque)

LPi 시스템 자동차의 인젝터, 공회전 액추에이터 및 개스킷 고장사례 연구 (Study for Failure Examples of Injector, Idle Speed Actuator and Gasket in LPi System Vehicle)

  • 이일권;조승현;김한구;김승철
    • 한국가스학회지
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    • 제16권3호
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    • pp.48-53
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    • 2012
  • 이 논문의 목적은 LPG 자동차의 액상 분사시스템에 관련된 고장사례를 연구하는 것이다. LPi 분사시스템인 인젝터를 점검한 결과, 인젝터에 카본이 누적되어 운전 중에 간헐적으로 연료를 분사하는 인젝터의 미세한 홀을 막아 연비를 5% 정도 떨어뜨리는 것으로 확인되었다. 엔진의 공회전을 조절하는 시스템인 공회전 조절장치 부품과 엔진에 공기를 공급하는 시스템인 스로틀 보디에 카본이 퇴적되어 공기의 흐름을 간섭함으로써 연비가 7% 악화된 것을 확인되었다. 엔진의 흡기 매니폴드 개스킷의 일부가 찢어져, 실린더 헤드와 실린더 블록의 밀착성이 약화되어 흡기행정에서 외부의 공기가 이 틈새로 간헐적으로 유입되면서 증가된 공기량만큼 연료량의 증가를 가져와 엔진의 회전수가 증가하여 부조화 현상이 발생되어 정상적인 상태보다 연비가 3% 정도 악화된 것으로 확인되었다. 이러한 고장사례는 운전중에 엔진의 출력 성능을 떨어뜨리고, 자동차의 연비를 악화시키는 요인이 된다. 따라서 품질확보에 철저하게 대처하여 고장현상을 최소화 하여야 할 것으로 판단된다.

Charged Cable Model (CCM) 정전기 방전(ESD)에 의한 전자제어장치의 손상 (Charged Cable Model (CCM) ESD Damage to ECU)

  • 하명수;정재민
    • 한국자동차공학회논문집
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    • 제21권2호
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    • pp.159-165
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    • 2013
  • ESD damage by Charged Cable Model (CCM) is introduced. Due to its own impedance characteristic unlike Human Body Model (HBM) or Machine Model (MM) electric component can be destroyed even though it is located after typical protection circuit. Possible mechanism of ESD damage to automotive electric control unit (ECU) in vehicle environment by CCM discharge was investigated. Based on investigation, field-returned vehicle whose ECU is expected to be damaged by CCM discharge was tested to reproduce it and similar electric component destruction inside ECU was observed. Suggestions to reduce the possibility of ESD damage by CCM are introduced.

LPI 차량용 연료필터 상부 하우징 냉간 단조 성형 공정에서 sink 현상 예측 및 개선 (Prediction of Sink Phenomenon during Forging Process and Improvement of LPI Fuel Filter Housing Forging Product)

  • 김준영;박상민;홍석무
    • 한국산학기술학회논문지
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    • 제18권6호
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    • pp.395-399
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    • 2017
  • 자동차에 사용되는 LPI 연료필터 하우징 제품은 기존 다이캐스팅 공정에서 냉간 단조 공정으로 개발하여 경량화 및 내구성을 향상하였다. 하지만 T자형 단조 형상이기 때문에 제품을 생산하였을 경우 제품의 싱크 문제가 발생하게 된다. 이로 인해 제품의 후처리 가공 문제가 발생한다. 본 연구에서는 이러한 문제를 개선하기 위해 성형 해석 시뮬레이션을 이용해 문제를 예측하고 개선방안에 대해 연구했다. 성형 해석 시뮬레이션을 이용하여 문제를 개선하기 위해 완전 성형이 가능한 최적 블랭크의 부피를 결정하였다. 그리고 최적의 블랭크 부피에 맞춰 성형 해석 시뮬레이션을 수행하였고 싱크 현상을 가시화했다. 싱크 현상을 개선하기 위해 냉간 단조 공정 진행 시 싱크 부 밑 부분에 패드를 받침으로 싱크 현상을 개선하였다. 적정한 패드력을 구하기 위해 파라미터 스터디를 진행하였고, 적정한 패드력으로 공정 진행 시 싱크 문제를 개선하였다. 그리고 실제 산업 현장에 적용하여 싱크 문제 개선에 대한 검증을 수행했다.